CLCE600RW0 Crosley Washer Dryer Combo - Instructions
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Dryer cut off before the clothes were dry.
All the symptoms indicated the thermister (located in the exhaust air stream of the dryer) was the problem. Pulled the lower panel off the dryer. Took out the two lower screws holding the door panel on so I could pull the front panel out just enough to get a screwdriver on the screws holding the thermister on. Unhooked the two wires connected to it and hooked them to the new thermister(no need to observe polarity). Put the new thermister in, screwed the door panel back down, put the lower panel on and started drying clothes.
Parts Used:
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Don from RUIDOSO, NM
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
16 of 22 people
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dryer was making terrible clunking noise when running
This is a stacker washer/dryer combination. Took off the back panel of the dryer, but found out the front needed to come off instead,to replace the blower wheel. This took more time than replacing the wheel. Was pretty easy to get to the wheel and replace. The center part had broken so replaced wheel and clamp. The push in fastner was broke, which held in the lint screen part. Was easy to install this. Dryer sounds as good as it did when it was new. It was very easy to find the correct part and shipping was overnight! Great service.
Parts Used:
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Marlene from Laurel, NE
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers, Wrench (Adjustable)
14 of 17 people
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Burning odor, melted terminal block
0) Turned off breaker at panel and disconnected power cord from 240v wall outlet
1) Removed screws that hold electrical cover plate on back of dryer.
2) Lifted the top of dryer using putty knife on 2 top edges of lid. This lifts up like a cars hood.
3) Removed the screws that attach the power cord to the terminal block and disconnected power cord
4) Removed screws that attach terminal block to dryer
5) Removed melted terminals by prying out of terminal block. Note metal lip on terminal has to be lifted in order to slide connector out. Also unscrewed ground wire from terminal block to dryer.
6) Drew diagram of what color wires go to what terminals
7) Cut terminals off of wires and connected new terminals. Crimped closed and used butane solder torch to solder connection between terminal and wire
8) Reconnected terminals to terminal block by sliding in. **Note, had to file down the edges of the terminals using moto-tool to make it fit as they are connected together using break-away tabs that leave a large piece of metal connected not allowing to fit in terminal block
9) Reconnected terminal block to dryer and reconnected ground wire.
10) Reconnected power cord to terminal block with screws
11) Replaced cover over wiring terminal block
12) Reconnected power cored to 240ac wall outlet
13) Turned breaker back on
1) Removed screws that hold electrical cover plate on back of dryer.
2) Lifted the top of dryer using putty knife on 2 top edges of lid. This lifts up like a cars hood.
3) Removed the screws that attach the power cord to the terminal block and disconnected power cord
4) Removed screws that attach terminal block to dryer
5) Removed melted terminals by prying out of terminal block. Note metal lip on terminal has to be lifted in order to slide connector out. Also unscrewed ground wire from terminal block to dryer.
6) Drew diagram of what color wires go to what terminals
7) Cut terminals off of wires and connected new terminals. Crimped closed and used butane solder torch to solder connection between terminal and wire
8) Reconnected terminals to terminal block by sliding in. **Note, had to file down the edges of the terminals using moto-tool to make it fit as they are connected together using break-away tabs that leave a large piece of metal connected not allowing to fit in terminal block
9) Reconnected terminal block to dryer and reconnected ground wire.
10) Reconnected power cord to terminal block with screws
11) Replaced cover over wiring terminal block
12) Reconnected power cored to 240ac wall outlet
13) Turned breaker back on
Parts Used:
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DAVID from DURHAM, NC
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
12 of 13 people
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fill hose got a hole in it
had to remove cover plate from under dryer and remove the top of washer to access the fill tube. horn part of fill tube is held in with one screw and plastic pin, the end with clamp that fits on the fill valve is very difficult to reach. could only get a grip on the clamp with 90 degree needle nose pliers. NOTE: washer cabinet has very sharp edges and cut my arm in several places trying to reach clamp. suggest wear long sleeve shirt.
Parts Used:
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keith from ROBERTSDALE, AL
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Difficulty Level:Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers
12 of 14 people
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Wretched screeching noise
Make sure you order a new belt and a new drum glide with the rear drum bearing assembly. If your bearing is worn out, so are the belt and drum glide!
1) Use a flat screw driver or putty knife to release the blind clips that hold the front side of the top of the dryer cabinet down
2) Swing dryer top up and remove two screws that hold the face of the cabinet.
3) Unplug the wiring harness and remove the cabinet face.
4) Remove the 3 screws that hold the drum to the bearing assembly (accessed from inside the drum. This makes it easier to remove the drum as the bearing assembly can be difficult to remove before you see how it snaps together
5) Reach under the drum and take the belt off the motor pulley, then remove the drum
6) Remove the old bearing assembly from the socket (slide up then out)
7) Remove the two screws that hold the bearing socket to the dryer
8) Fasten the new socket to the dryer (you'll need help doing this unless you have REALLY long arms because you have to reach inside the driver and the back of the dryer at the same time)
9) Grease the socket with the supplied high temp grease
10) Bolt the new bearing assembly to the drum and put the new belt around the drum
11) Put the drum back in and snap the bearing socket in and down
12) Guide the new belt around the motor pulley & tensioner
13) Glue the new drum glide / felt piece to the front cabinet
14) Put the cabinet back together
1) Use a flat screw driver or putty knife to release the blind clips that hold the front side of the top of the dryer cabinet down
2) Swing dryer top up and remove two screws that hold the face of the cabinet.
3) Unplug the wiring harness and remove the cabinet face.
4) Remove the 3 screws that hold the drum to the bearing assembly (accessed from inside the drum. This makes it easier to remove the drum as the bearing assembly can be difficult to remove before you see how it snaps together
5) Reach under the drum and take the belt off the motor pulley, then remove the drum
6) Remove the old bearing assembly from the socket (slide up then out)
7) Remove the two screws that hold the bearing socket to the dryer
8) Fasten the new socket to the dryer (you'll need help doing this unless you have REALLY long arms because you have to reach inside the driver and the back of the dryer at the same time)
9) Grease the socket with the supplied high temp grease
10) Bolt the new bearing assembly to the drum and put the new belt around the drum
11) Put the drum back in and snap the bearing socket in and down
12) Guide the new belt around the motor pulley & tensioner
13) Glue the new drum glide / felt piece to the front cabinet
14) Put the cabinet back together
Parts Used:
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Paul from Broadalbin, NY
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
9 of 9 people
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Felt around drum holder worn and torn.
1. Removed face of dryer (drum 'holder')
2. Disconnected door switch wires
3. Tore off existing felt
NOTE: The length of the felt that I recieved from PartSelect was incorrect (too short). Since the existing felt was worn and torn at the top, I replaced only a length that matched the length of the new felt.
4. Used a razor blade-type gasket remover/scraper to remove the exisitng glue
5. Applied new glue (which comes with the felt) onto the felt and let it set up
NOTE: In hindsite, I would apply the glue to the drum holder instead, as the glue otherwise soaks into the felt. If applied to the drum holder instead, the glue will spread out and provide more surface area for adherence.
6. Installed the new felt, starting at one end and working my way around to the other end, being careful not to stretch it
7. Trimmed the remainder of the existing felt (see first NOTE)
8. Scraped the drum holder below the pulled away ends of the exisitng felt
9. Applied glue to the existing felt, including the trrimmed ends so that the ends do not pull away from the ends of the new felt
10. Re-attached the existing felt
11. Let the glue set-up overnight
12. Reinstalled the face of the dryer, turning the drum so that the felt will not get pushed away
13. Reconnected the door switch wires
14. Turned dryer on, with lid still raised, to check for any drifting of the felt
15. Once assured that the felt would stay in place, put the dryer in service
NOTE: I replaced the felt becasue of the gap that opened due to compression of the felt. The gap, as well as a torn piece of the felt that entered the interior of the drum, was catching clothes and tearing them as they were rotated between the drum and the drum holder. The new felt eliminated this problem.
2. Disconnected door switch wires
3. Tore off existing felt
NOTE: The length of the felt that I recieved from PartSelect was incorrect (too short). Since the existing felt was worn and torn at the top, I replaced only a length that matched the length of the new felt.
4. Used a razor blade-type gasket remover/scraper to remove the exisitng glue
5. Applied new glue (which comes with the felt) onto the felt and let it set up
NOTE: In hindsite, I would apply the glue to the drum holder instead, as the glue otherwise soaks into the felt. If applied to the drum holder instead, the glue will spread out and provide more surface area for adherence.
6. Installed the new felt, starting at one end and working my way around to the other end, being careful not to stretch it
7. Trimmed the remainder of the existing felt (see first NOTE)
8. Scraped the drum holder below the pulled away ends of the exisitng felt
9. Applied glue to the existing felt, including the trrimmed ends so that the ends do not pull away from the ends of the new felt
10. Re-attached the existing felt
11. Let the glue set-up overnight
12. Reinstalled the face of the dryer, turning the drum so that the felt will not get pushed away
13. Reconnected the door switch wires
14. Turned dryer on, with lid still raised, to check for any drifting of the felt
15. Once assured that the felt would stay in place, put the dryer in service
NOTE: I replaced the felt becasue of the gap that opened due to compression of the felt. The gap, as well as a torn piece of the felt that entered the interior of the drum, was catching clothes and tearing them as they were rotated between the drum and the drum holder. The new felt eliminated this problem.
Parts Used:
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Robert from York, PA
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
10 of 12 people
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The drier was "screeching"
First of all, the folks at Part Select have been terrific. I balled up my address and they were great in correcting my error and getting the parts promptly to me. They provide directions with the parts. And You Tube, is a wealth of information too. The process is to remove the drum and replace the nylon busihing that supports the drum at the back of the machine. Getting it out was no sweat. Getting the drum back in was a bit more challenging single handed. If I was going to make any suggestion it would be this is a good project for two sets of hands with the second set needed for about ten minutes. The You Tube video I watched said putting the front cover with the drum attached to the back of the unit would be the challenge and they were right. Otherwise, super easy and the results are it's back to "new" condition. Thanks again to Part Select!
Parts Used:
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Michel from CHICAGO, IL
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers
9 of 9 people
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The Dryer Drum Would Not Move. Motor Worked But Drum Didnt.
First I read the manual on how to replaced the dryer drum belt. Second I took off the front panel. This would involving taken all screws from the top of the dryer face and the front panel. Thirdly I removed the exhaust attachment. Then I saw that the belt broke. Really it looked torned apart. I believe too heavy of a load in dryer. I then installed the new belt and reversed everyhing I did to start. The dryer runs great. This is not that bad of a job. If you can do it yourself, why pay hunreds on a service man to do the job.
Parts Used:
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steven from parrish, FL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
10 of 14 people
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Bearing Bracket Worn Out
Took off front panel, removed drum and replaced parts listed. A bit tricky to keep small parts in place. However, masking tape helped. Best of all was the online diagram of how the parts were assembled. In addition, taking step by step phone pixs aided in replacing parts since there was some down time between diagnosis and installation.
Parts Used:
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David from Fairdale, KY
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
21 of 24 people
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drum glides worn out making thumping noise.
watched video on replacing rear bearing.although rear bearing was not the part(s) i needed to replace, video instructed disassembly procedures to get to the drum glides. this was a very simple and easy to follow video. repair was a breezeand took roughly 25 minutes. the most time consuming segement of repair was vaccuuming out lint,that was 15 minutes. In future, as a preventative, i plan to remove front of machine to clean annually.
Thank you.
Thank you.
Parts Used:
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david from edinboro, PA
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
7 of 8 people
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Thumping Noise, Clothes Getting Stuck
Unplug, lift top, unplug 5 wires, remove 2 screws, pull dryer front away while supporting drum. Remove old glides, snap in new. Reverse disassembly procedure
Parts Used:
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LT Frank from Wacissa, FL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
6 of 6 people
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Terminal block, and wires were dammaged/melted
Used nut driver to remove screw and cover from dryer cord terminal block, used screw driver to remove two screws securing old terminal block, cut dammaged wire and stripped wire back and crimped on new terminal connecter, replaced old terminal block with new one, replaced two screws, installed new cord, and replaced cover plate and screw.
Parts Used:
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Edwin from Eagar, AZ
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Pliers, Screw drivers
7 of 9 people
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dryer door part broke
Dryer door would not close, part had broke and fallen in. Once part was received it took less than an minute to put the new one in and I was back in business.
thanks for making it easy to find the part needed. and the delivery was fast!
bonnie J.
thanks for making it easy to find the part needed. and the delivery was fast!
bonnie J.
Parts Used:
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Bonnie from Saint Augustine, FL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
7 of 9 people
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Screeching noise when drying
Rear plastic drum support bearing got worn making the shaft come in contact with the metal bearing bracket. That contact created a groove overtime and eventually snapped the shaft tip off.
Cut power off. Remove all the screws from the front panel. (where the controls are) working from the bottom to the top. Insert putty knife between the dryer and the control panel and push down to release. Carefully disconnect the wire harness.
You will find 2 screws at the bottom and 4 on top holding the dryer door. Remove and expose the drum.
Remove the drive belt
Remove the drum.
You need a 5/16 nut drive to remove the bearing bracket and an extra set of hands to hold the support from the back.
Re-install the parts. I used bearing grease to make it run smoother
Attach the new shaft to the drum and reinstall the drum (its best done with help)
Re install everything back again. And you are done
Cut power off. Remove all the screws from the front panel. (where the controls are) working from the bottom to the top. Insert putty knife between the dryer and the control panel and push down to release. Carefully disconnect the wire harness.
You will find 2 screws at the bottom and 4 on top holding the dryer door. Remove and expose the drum.
Remove the drive belt
Remove the drum.
You need a 5/16 nut drive to remove the bearing bracket and an extra set of hands to hold the support from the back.
Re-install the parts. I used bearing grease to make it run smoother
Attach the new shaft to the drum and reinstall the drum (its best done with help)
Re install everything back again. And you are done
Parts Used:
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David from Rockville, MD
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
6 of 7 people
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drum wouldn't turn
I removed the front access panel above the washer and removed the top dryer front panel. Then pulled out the drum and noticed the drum support ball stud had broken off, rather than order a new one, I welded it back on with a mig welder. I then replaced the drum support bearing and reinstalled the drum. I then installed the new belt before placing the front top panel in place. I removed the small vented panel on the back side to access the belt tensioner and fit the belt around the pulley and motor shaft. The whole job took less than an hour.
Parts Used:
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Keith from Midwest City, OK
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
6 of 7 people
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