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Models > MAT10CSAAW > Instructions

MAT10CSAAW Maytag Washer - Instructions

All Instructions for the MAT10CSAAW
76 - 90 of 395
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After the washer machine reached the water level the washer would not begin its wash cycle.
I removed the old lid switch assembly from washer and one by one exchanged the wires to replace correctly on the new part. I placed the new lid switch assembly in the washer using the screw to tighten the part in place. I turned on the washer and after the water level stop the wash cycle began immediately. Friends were impressed I used your web site to determine the part selection by the previous reviews and that I replaced the part with ease. Thank you for an user friendly web site.

Granville County/North Carolina
6/13/2010
Parts Used:
Lid Switch Assembly
  • Vickie from Butner, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
8 of 10 people found this instruction helpful.
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Washer made screeching sound during spin cycle. Also, the clothes were still very wet at end of spin cycle.
I used two vise grip wrenches in place of specialized tool that is no longer available. I put the vice grip wrenches on the brake assembly and hit them alternately with a hammer. I also used penetrating oil.

Note, the parts package stated made in USA but the bearings had China stamped on them.
Parts Used:
Brake Assembly Rear Bearing
  • Edward from EUCLID, OH
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
7 of 8 people found this instruction helpful.
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Washer was shaking and not balanced
The instructions were clear. Did every step. Did 2 loads so far and everything works like new.
Parts Used:
Damper Pad Kit
  • Dean from New Lenox, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
8 of 12 people found this instruction helpful.
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Worn belts
All I had to do is tilt the machine to expose the bottom and replace the belts. It was fast, easy and the machine works fine now.
Parts Used:
Belt Kit Belt Kit
  • Ronald from Birmingham, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
8 of 12 people found this instruction helpful.
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Washer making high pitched squeal at stopping of spin cycles
My washer is apparently 37 years old. I bought it used in the 90’s and have had to do little or nothing to it repair wise. It started to make a loud squeal/squeak when the spin cycle stopped. I watched a couple videos showing the brake assembly, bearings and belt replacement and was able to find parts. However, one bearing appears to no longer be made (just repacked with heavy duty grease) and the special tool is nonexistent. I read others using a chain clamp vise to remove the brake assembly and bought a 20 inch chain clamp vise and a 3 set variety of vise grip pliers for about $20. They make an 18 inch chain vise but glad I got the 20 inch. I used two vise grip pliers to clamp chain around notch two notches that the specialty tool would normally grab. It was a cumbersome getting in there to whack the pliers with a small sledge hammer so I got a approx 18 inch 2x4 and cut a notch at the end to keep chain vise from digging into bottom of washer and whacked the end of the 2x4. Seemed to work ok and did the same to tighten back after replacing break assembly. Got it out back together and no more squeal.
Parts Used:
Brake Assembly Rear Bearing Belt Kit
  • Chad from BOERNE, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
7 of 9 people found this instruction helpful.
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Oil leak from lower lip seal
I didn’t have special tool for brake but punch and hammer worked. Seal was easy to replace. Several videos online to show you how. It wasn’t worth it to tear apart the transmission and buy more parts/seals (if they were even available). But I didn’t know how much oil was in it. I drilled a hole in the side to somewhat check level and added 80-90 gear oil. It was almost empty and added almost a quart. Used a self taping screw/bolt with gasket sealer to plug the hole. I got 34 yrs out of this washer. If it fails, oh well. Just hate to buy a new one that only last 10yrs if im lucky.
Parts Used:
Transmission Lower Lip Seal Repair Kit
  • Anthony from CHESANING, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
6 of 6 people found this instruction helpful.
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Washer was overfilling from water level selected
Tried the water level control first. didn't fix it.
Then replaced the air tube for tub fill volume.

The thing here is that it didn't have a hole in it nor was it blocked where you couldn't blow through it.
The prolbem was that at the tub end it has a larger diameter and that was nearly filled with softener residue so it changed the air volume.
That reduced air volume caused the air pressure to be wrong to the water level sensor.
My most useful tool was a magnet mount flashligt inside the cabinet so I could see to get the hose back on.
Parts Used:
Air Tube for Tub Fill Volume
  • Jacob from SMITHFIELD, KY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
6 of 7 people found this instruction helpful.
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Upper and lower filler injectors broken
Power cord out, of course.Popped off the front panel, swinging bottom outward. Wedge shaped protrusions on top of front panel work as a hinge until the bottom is swung out and the entire front lowered. Unscrewed the top--one screw in each front corner accessed from the front opening (removed panel). Panel behind control panel must be removed (5 hex head screws). Tilted front of top up revealing broken injector. Retaining screw for injector accessible from behind control panel loosened and broken injector assembly removed. New (easily assembled--snap together) injector slid into holding slot on one side and screwed down with previously removed hex screw. Reassemble in reverse.
Parts Used:
Upper Fill Injector Lower Fill Injector
  • Henry from Southside, AL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
6 of 7 people found this instruction helpful.
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Washer Leaked Water From Bottom Seal
Removed washer tubs inner and outer nut (part # 10 ) on inner was hard to remove and is a reverse thread used hammer to loosen once off removed 1st tub - then removed set screw #17 and then unscrewed mounting s item #29 this again required some hammer tapping to loosen - once off used flat head screwdriver to pry & remove the rubber piece on bottom of outer or 2nd tub -but keep going as the leak will probably be from part #20 tub bearing ( this will save you the time to test and find out it still leaks and have to take apart again after only replacing #29 removed 3 bolts holding tub - disconnected hoses and removed 2nd tub - used rubber hammer to knock out and install #20 tub bearing - reasembled and wow no leaks to cost about $120 - time worked on 3 hrs - only because took apart 2 times - down time on washer 10 days as we didn't order all parts to start with no beer needed but did enjoy a nice red wine - good luck
Parts Used:
Mounting Stem/Tub Seal Kit
  • JACLYN from RICE LAKE, WI
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
6 of 7 people found this instruction helpful.
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Washing machine lid hinge balls fell off machine lid
First I had to hold the balls into the little holes on the side of the lid - one at a time- and tap the plastic ball into the side with a small hammer. I did the same with the other side. Silde the lid to match the holes located on the washing machine - give a little push to make sure that the balls are in place. You have your lid fixed to your machine where you can lift the lid and it will stay up without falling.

Note: If the balls fall out - make sure to tap a little harder so that the balls stay in place.
Parts Used:
Washing Machine Lid Hinge Ball
  • Sandra L from Warren, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
6 of 7 people found this instruction helpful.
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lid closing to far bumpers missing and fuse block cracked
unhooked power plug removed 2 top screws tilted topfront panel back removed cracked fuse holder replaced with new fuse holder put top cover back on installed 2 top screws plugged in power cord done!
Parts Used:
Washer Lid Bumper Fuse Block
  • eunice from prestonsburg, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
18 of 43 people found this instruction helpful.
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The washer would only go on the delicate cycle no matter what cycle it was set on.
This is a coin-op washer so the timer had to be removed through the coin box. The top lid was first removed from the coin box. There is one 5/16 hex head screw holding the timer in. After removing the screw the timer was lifted from the box. It is a tight fit that requires some wiggling around of the timer. There are two plug in wire harnesses attached to the timer. Because of the position of the timer the wires are a little short, but are able to be unplugged. The new timer was installed and the procedure reversed.
Parts Used:
Washer Timer
  • Don from Crescent City, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver
6 of 7 people found this instruction helpful.
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Burned out part
Good.
Parts Used:
Lid Check Switch
  • RAFAEL from CENTERVILLE, GA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
7 of 10 people found this instruction helpful.
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Very old washer was leaking oil and grease drops into the wash water.
Followed the procedures recommended for replacement of all the parts included in the Tub Bearing Kit and the Mounting Stem/Tub Seal kit as illustrated in a detailed, 32 minute repair video for the Maytag A606 washer which is available on YouTube. Many difficulties were experienced in the disassembly procedures due to extensive corrosion of tub bearing and tub stem parts (the washer is 47 years old).
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
Parts Used:
Mounting Stem/Tub Seal Kit Tub Bearing Kit
  • William A from PITTSBURGH, PA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
5 of 5 people found this instruction helpful.
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The old pump was beginning to drag due to the age of the washer.
Removed the front panel. Then blocked up the front of the machine. Removed the pump belt. Removed the 3 5/16" screws from the bottom of the old one and tilted it slightly to remove. Put the new one in and reinstalled the 3 screws. Put the belt back on and slid new pump all the way to the right and tightened 1 screw. Loosened the screw until there was about 1/4" of gap when squeezed the belt together. Tightened the one screw, then the other 2. Put the front panel back on and lowered the machine. New pump works great.
Parts Used:
Drain Pump
  • Howard from ALBRIGHT, WV
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
5 of 5 people found this instruction helpful.
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All Instructions for the MAT10CSAAW
76 - 90 of 395