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Models > LG400AXW1 > Instructions

LG400AXW1 Frigidaire Washer Dryer Combo - Instructions

All Instructions for the LG400AXW1
91 - 105 of 548
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The drum was squeaking and running slow
Removed drum replaced bearing with kit, replaced both front drum seals and drive belt. The only problem was when replacing the rear drum ball the three screw holes were poorly tapped and took several tries to get them in. The manufacturers could easily fix this problem. They could provide self tapping hex head screws instead of the Phillips head screws. Everything else went very smoothly.
Parts Used:
Multi-Rib Drum Belt Upper Drum Glide Front Lower Drum Seal Rear Drum Bearing Kit
  • Terry from TENINO, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
Parts Used:
Rear Drum Bearing Kit Rear Drum Bearing Kit Drum Support Bearing Rear Drum Bearing Kit
  • Doug from ODESSA, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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No heat
Raise the top and remove the front panel assembly. One philips screw, 24mm gas line coupler and 3 electrical connectors frees the burner assembly. Slid the old igniter out and the new one in.2 philips screws to remove the coil retainer and replace the coils.
Parts Used:
Igniter M Series Ignition Coil Kit
  • Matthew from JOLIET, IL
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Wrench set
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Noisy operation - "Chugged" during operation.
With prep work mentioned below and a good flashlight it takes about 15 to 30 minutes if you're a good handy-man. If you're not, get a neighbor or friend who is. This repair isn't rocket science, but does take a some mechanical aptitude. This unit is a washer/dryer combo unit. Unplug power cord and remove water supply hoses, the drain hose and dryer vent if required to obtain easy access to front panel. There is water in all the lines, so have some towels and a small gallon bucket to help drain the lines if disconnected. Remove two screws on bottom of front panel. Be sure there is about 2 inches from washer/dryer to floor in front to allow front panel to drop directly down, then pull panel out lightly. Wood spacers or similar are recommended under front feet to prop-up front of washer. (There are two tabs on each side of the front panel. The panel must be pulled straight down to clear tabs). Another option is tilt back the washer/dryer about 60 to 75 degrees unit to make the front panel more accessible if all is disconnected in back and you have the room to do so. Once the front panel srews are removed, you may have to place an object (thin pry bar or screw driver) between the top of the washer unit and the front panel for release (be careful not to dent or scratch the top metal or front panel. Remove front panel and set aside. Locate belt near bottom and tensioner pulley (it moves back and forth laterally), push in tensioner pulley to relieve pressure on belt and remove belt from small pully wheel at motor, then the large drum pulley wheel. Place new belt on large pulley first, then small pulley. Push in tensioner pulley and move middle of belt to the inside of the tension pulley to take up the slack. This process is somewhat hard. It takes good hand strength. Be sure the belt is aligned in pulley grooves. Place washer/dryer back in level position, re-attach water supply hoses, drain hose, dryer vent line and power cord, if removed for repair. Check for leaks in water supply lines and be certain the drain hose is well attached to the drain pipe. (This is a good time to clean or replace the dryer vent line to prevent possible lint fires.) Plug in washer/dryer unit and test as if washing a small load. Re-install front panel after successful test in run operation. The part came quickly and fit perfectly.
Parts Used:
Drive V-Belt
  • Peter from Lynnwood, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Worn front drum slides
The disassembly was very easy and it appeared that this would be a very quick repair. But the removal of the old felt was difficult and once it was removed it took a lot of effort to remove the bits still stuck on. The tool of choice to remove the stuck on felt was a small torch. After that use a coarse sand paper to remove the remnants. Glue on the new felt and reinstall the front panel.
Parts Used:
Upper Drum Glide Front Lower Drum Seal
  • David from Plymouth, ME
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Brown stains on clothes.
Followed your website repair guides and the great belt replacement video.

Other parts used were; front lower basket seal, dryer seal, and dryer drum belt.

Had no problems except for keeping the drum belt idler pulley tension spring in place. Used the rear access panel to solve this issue.

John H.
Palm Desert, CA
Parts Used:
Upper Drum Glide
  • John from Palm Desert, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Not enough heat
Checked PartSelect online for people with a. similar problem. Found most common problem was the coils.
I opened the top, removed the two screws holding the front panel, unclipped the wiring harness from the machine to the door and removed/cut the plastic wire tie and front came off easily. I put the front piece to the side after changing the light bulb. I cleaned out a large amount of lint and found the coils on the left hand side without trouble. Carefully disconnected the wiring clips, unscrewed the holding screw and removed the old coils. Installed the new colis, 1 has three prongs and the other has 2 so you ca'nt mix them up. Replaced the hold screw, re-connected the witing harness, installed a new wire tie, and re-stalled the two holding screws. Closed the cover and turned it on.
At first it did not heat up which was dissappointing; but then I left it alone and 15 minutes later it worked like new! And heated up just fine ever since.

Total cost about $35.00 with shipping. I took a chance that I would not need the sensor or the ignitor based on the comments of others and I just bought the coils. If I had to do it over I would have bought all three and saved on the shipping.
Parts Used:
M Series Ignition Coil Kit
  • John from Bergenfield, NJ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
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Loud Squeek while the dryer is running.
1. After checking the Parts Select website for some useful information I unplugged the dryer.
2. I popped the two clips holding the top down and lifted the top up and out of the way.
3. I used the 8mm socket and screwdiver combo to remove the two screws holding the front of the dryer on. These screws are so close to the sides of the dryer that you need something very thin to seat the socket, it is so thin a small rachet would not fit.
4. Once the to screws are free to forget to unhook the two wires that lead to the automatic cutoff switch on the right. Label them and move them out of the way.
5. The front of the dryer should pivot forward and come right off. Don't forget about the two clips at the bottom, they are not really attached to anything and can be easy to lose.
6. Get your screwdriver and dive into the drum, on the back should be three screws, take those out.
7. Spin the dryer around and take off the vent cover in the lower left corner of the back of the dryer, watch out the socket is a smaller size.
8. Once inside there is an idler pulley like on the back of a ten speed bike, pull the tension out of it and take the drive belt off the pulleys.
9. The drum should be able to be pulled out the front of the dryer, set aside with the door. The screws on my dryer were so tight I had to use a hammer drill to remove them.
10. This is were I got stuck, no one mentioned how to get the bearing plate off, as if everyone would just know. You must lift up on the bearing plate and once it moves up then you can pull it out.
11. Use the 8mm socket to unscrew the old plastic bearing guide. The small metal clip on the back of the dryer will fall off with the grounding ball bearing.
12. With brum bearing kit in hand start off by putting as much high temp lubricant as you can into the bottom of the new bearing guide. I also use a little lubricant like glue to hold the new grounding ball bearing in the little hole on the back of the bearing guide.
13. Here is the tricky part you have to screw the bearing guide into the the dryer while simulaneously holding the little metal clip in place on the back of the dryer. I used duct tape to hold the metal clip and once the screws got started I just took the tape off.
14. Now you have to do the impossible, the bearing must be screwed to the drum. So unless you have 7 foot long arms you can't hold the bearing and drive the screws. Another problem is the bearing itself, the holes are not the same size as the original and they are not threaded. I stripped every screw that came with the kit trying to get them through the metal of the bearing.
15. With an unwilling victim holding the bearing steady I finally got a replacement screw to seat through the bearing. Once you get one the rest are easier.
16. You are ready to reassemble, after vacuuming everything ou, pick up the drum making sure the belt is around the drum about where it was when you took it off. Push the drum through the front of the dryer all the way to the back, aim a little high so the bearing can move down and seat in the bearing guide.
17. Tuck the clips on the front panel of the dryer into the bottom front edge of the dryer and the whole front should pivot up, when you get it almost closed you will have to lift the drum and set it on the front bearing in the door.
18. While holding the front of the dryer on you have to reach inside and get the 8mm screw started on the left or right, if you let go the front of the dryer will pop off and you have to start over with the pivot. Now is a good time to have a magnet on a stick so when you drop the screw or screw driver you don't have to take the front off to retrieve your tools.
19. Once the front is on reconnect the two wires to the switch in the front of the dryer. Remember the ones you were supposed to have labeled earlier.
20. Close the top of the dryer and spin the dryer around so you can reach inside the vent door and pull the tension pulley over and reseat the drive belt. Rem
Parts Used:
Rear Drum Bearing Kit
  • Miles from LaPorte, IN
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
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Loud Squeaking c/c unlevel. Led to shaft breaking
Took off all controls and panel. Removed the top. Pulled out the drum. Unscrewed shaft and bearing holder. Replaced all parts and started it back up.
--The parts were shipped timely,
Parts Used:
Multi-Rib Drum Belt Rear Drum Bearing Kit Rear Drum Bearing Kit Drum Support Bearing Rear Drum Bearing Kit Dryer Drum Bearing Bracket
  • Chad from Reisterstown, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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over filling
no problemO top loader. open top, disco two electrical plugs and a small hose, then remove two screws that hold valve in place and remove. Re install in reverse order. Thanks for your support Eliot in Alaska!
Parts Used:
Water Inlet Valve
  • eliot from fairbanks, AK
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
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heat would initially come on then go off or sometimes not come on at all.
1. unpluged the dryer and turned off the gas.
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
Parts Used:
M Series Ignition Coil Kit
  • Vincent from Fairfield, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
Parts Used:
M Series Ignition Coil Kit
  • Steven from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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no filter
filter inalled
Parts Used:
Dryer Lint Screen
  • Luis from La Jolla, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Gas flame turns off after a while, dryer keeps turning but no heat is generated.
Before this fix which worked beautifully, I tried replacing the flame sensor which did not work. To read that story, search under part number PS459818 (Flame Sensor). Our model is a Westinghouse, so access to the unit is a bit different than the other stories. It's a stacked front-loader sitting on top of a washing machine.

1. Open the little front door (lower left side) by unscrewing the little screw right below it. The door will pivot and slide out vertically.
2. Disconnect the electrical main lead coming from the back of the unit (just in case).
3. Close the gas switch lever on main gas pipe coming from the back on left side (just in case).
2. Remove 2 phillips screws on top of the metal bracket holding the two coils. The screws have to be removed completely along with the bracket. It's easy, they are right in front and there is room for the screwdriver. Use a thin long one instead of one with multiple bits to better align with the screws, which are very close to the coils.
3. The two coils slide right out and are very different so it's easy to keep them straight. Remove electrical connectors before or after removing the coils (I marked the plastic on top with a sharpie to keep them in the right orientation).
4. Drop in the two new coils and reconnect them to the electrical leads.
5. Reconnect main electrical lead from back (match wire colors)
6. Reopen gas lever on gas pipe.
7. Drop in front cover at an angle, tilt vertically and put screw back underneath. Use magnetized screwdriver or a piece of scotch tape to hold the screw or it might fall off the screwdriver.
8. Voila'. It worked.

This website is great. Our dryer is a Westinghouse bought in 1991 (almost 20 years old!) and with this fix it's just like new. In 1994 we used parts bought here to fix our washing machine (Westinghouse LT350RXW1). That machine is now 15 years old and still going!
Parts Used:
M Series Ignition Coil Kit
  • Giuseppe from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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drive belt old and stretched
unplugged machine. pried up with large regular screwdiver on top washer lid. removed two phillips screws bottom of front panel, had to use rubber mallet to drive front panel down to remove as was rusty and old. removed old belt using screwdriver. put new belt under tub pulley and put belt on small pulleys. kept moving tub and springs by pushing on tub. Took several tries to get new belt to go on the large tub pulley but finally did it. I used the instructions you gave for replacing broken drive belt and it worked. replaced front panel and two phillips screws, put top back on and away it went.
Parts Used:
Drive V-Belt
  • George from Sault Ste. Marie, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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All Instructions for the LG400AXW1
91 - 105 of 548