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Models > RGD4400VQ0 > Instructions

RGD4400VQ0 Roper Dryer - Instructions

All Instructions for the RGD4400VQ0
106 - 120 of 2006
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Aft seal deterioated and causing brown spot on clothing due to netal to metal contact.
Removed top and front of dryer then drum and followed the instructions in the package. It was a real simple procedure. I did additional cleaning while the dryer was disassembled.
Parts Used:
Rear Drum Felt Seal
  • Cleo from Laurinburg, NC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
11 of 12 people found this instruction helpful.
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Motor wore out
I took the dryer apart ( using a repair book ) It was Super Simple to do I only needed a extra set of hand's to hold the drum in place while reassembling it. removed the hold down snap on collar's on the Motor ( after removing the Blower from the back of the dryer ( super simple. Extra set of hand's needed ) Reassembled in the same order. And now The Dryer work's like NEW..Shure Beat Buying a new Dryer..
Parts Used:
Maintenance Kit Drive Motor with Pulley
  • Charles from Clarissa, MN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
12 of 15 people found this instruction helpful.
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Bearings wore out of drum rollers
I raised the top of the dryer, removed the front, the belt and the drum. Slipped off old rollers, installed new ones and new tensioner. Reinstalled drum and belt, bolted front back on and closed the top.
Parts Used:
Maintenance Kit
  • Judy from Kalamazoo, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
11 of 12 people found this instruction helpful.
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One of the drum support rollers was worn out
I lifted the top of the dryer and removed the front panel. I removed the drum exposing the drum rollers. I replaced the rollers and reassembled the dryer. The exploded views on the web site made it easy to see what to do.
Parts Used:
Roller Support Tri-Ring Rear Drum Support Roller Kit
  • David from Fleetwood, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
13 of 19 people found this instruction helpful.
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A piece of cloting snagged and broke the door switch.
Repair job took less than 10 minutes: 1) Unplug Dryer 2) Remove Lint screen and 2 Phillip screws 3) use flat putty knife to depress lid latches while lifting (latches located approx 2 - 3 inches from each side. 4) unplug defective door switch 5) remove 2 Phillip screws that secure the door switch. Reinstall switch repeating the above steps in reverse order and your done.
Parts Used:
Door Switch
  • Ronald from LANCASTER, CA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
11 of 13 people found this instruction helpful.
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Dryer stopped spinning
The dryer quit working. I did some trouble shooting on your amazing site, ordered what i thought it might need and then got to work. Took no time to get it apart and replace roller kit and belt. What took the longest was getting in there and cleaning out probably 15 years worth of dirt and dust. If you have not opened your dryer up and done this, 10/10 recommend, because in doing so i found that the motor was the real culprit. Once i opened it up more, especially cleaning around the blower fan and motor, i was half a day in. Put it all back together and got it running for two more loads before the motor quit. Replaced that and since the hard work was done, had it back in in half an hour and running great. Probably will need to redo the felt seal one day, but for now, i am calling it a win. This is my go to site for all things and i have been able to work on most of my major appliances and do it myself using the helpful information here.
Parts Used:
Rear Drum Support Roller Kit Multi Rib Belt - 92-1/4"
  • Danielle from FREEDOM, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
13 of 19 people found this instruction helpful.
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Badly worn idler pulley and rollers.
Braced dryer drum with a block. Removed the two rollers one at a time by using a screwdriver to pop off the triangular clip. Slid on new rollers. Would have been easier to remove the drum out the front instead of bracing it. Installed new idler pulley and belt. Dryer is 25 years old and sounds like a new one now when running.
Parts Used:
Dryer Idler Pulley Assembly Rear Drum Support Roller Kit Multi Rib Belt - 92-1/4"
  • TODD from GRASS VALLEY, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
11 of 14 people found this instruction helpful.
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broken clip on top panel hold down
pressed clip into hole on top of front panel. first remove two philip screws that hold filter so you can lift top up.
Parts Used:
Front Top Lock
  • Mark from Huntington Station, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
15 of 26 people found this instruction helpful.
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replace lint filter
with both hands
Parts Used:
LINT SCREEN ASSY, WOD
  • Ed from Greensboro, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
10 of 11 people found this instruction helpful.
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Replaced a broken pulley.
Half of my pulley was broken off so there were no wrench flats to take it off. I was able to remove it using Channel Locks and the 7/16 wrench shown in the video.

Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Parts Used:
Motor Pulley - 60 Hz.
  • Brian from IMLAY CITY, MI
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
10 of 12 people found this instruction helpful.
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LP gas conversion
Followed instructions, except to advoid sharp edges, and completed the job in under an hour.
Parts Used:
Liquid Propane Conversion Kit
  • Robert from Palmdale, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
11 of 15 people found this instruction helpful.
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Had to convert from natural gas to propane
Well, here's the rub...in order to find out what part I needed to order, I needed to take the dryer apart to where the gas controls are, and there on a sticker was a part number for an LP conversion kit. But, in order to get to that gas valve unit, I fumbled about figuring out how to take this brand new dryer apart, since there were absolutely no instructions whatsoever in the owners manual. And once apart, and pretty much all apart, I wondered how it would be that the Maytag repair man would be so lonely, as he'd have plenty to do.
However, the kit had great instructions as to how to take it apart and change out the orifices.
Parts Used:
Liquid Propane Conversion Kit
  • Peter from The Rock, GA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
12 of 18 people found this instruction helpful.
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
10 of 12 people found this instruction helpful.
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
12 of 18 people found this instruction helpful.
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the directions didn't say I needed clips to hold the felt in place while I did the glue
Once I started using a bunch of clothespins to hold the felt in place and then started gluing small sections at a time I was able to complete the task. The glue comes out of the tube very quickly so don't squeeze it a lot.
Parts Used:
Rear Drum Felt Seal Rear Drum Support Roller Kit
  • Todd from SAN JOSE, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
9 of 9 people found this instruction helpful.
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All Instructions for the RGD4400VQ0
106 - 120 of 2006