MUG2000AWW Maytag Washer Dryer Combo - Instructions
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Dryer shut off before clothes were dry
The old sensor came out by removing 2 screws. I unplugged the two wires from the back of the sensor and plugged them into the new sensor. I reinstalled the new sensor using the same two screws. Of course, I unplugged the dryer first.
Parts Used:
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Paul from Tamaqua, PA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver
10 of 14 people
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water leaking on the floor.
I opened the door on the washer,and pushed on inner tub upward.it moved about 1 inch and the I knew tub bearings where shot .So I removed all components and repaced the outer tub with new bearing pack.. NOTE... Not an easy repair..but when i finished i had no probems with water leakage.ALL GOOD.
Parts Used:
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john from st helen, MI
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Difficulty Level:Really Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Socket set
8 of 9 people
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mold on door boot, replace door boot
followed the approach on fixya.com. when installing new boot and cable loop, found it easier to remove drum cover from machine (held on with simple clips). Then you can install boot onto the cover and the door frame. Putting everything back in machine and re-attaching the various braces took only a couple of minutes.
Parts Used:
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TJ from WARWICK, NY
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Screw drivers, Socket set
8 of 9 people
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No Heat
I suspected a faulty igniter and disconnected the cable to the igniter and measured the resistance of the igniter and found it to be 70 ohms then I checked the voltage at the same cable towards the power source and found it to be 25 volts ac which should be 120 volts ac. Next I checked the radiant flame sensor and found it to be open (it should be a closed circuit when cold). I removed the flame sensor (with the power off) using a small box wrench and found a broken lead. Replacing the flame sensor solved the problem.
Parts Used:
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NICHOLAS from PARMA, OH
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Wrench set
9 of 12 people
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Over the last year the 'start' button has had to be held to 'start' the dryer, with a humming noise during the process. Eventually it hummed, stank, and wounldn't start.
Yanked the front panel, observed motor operation while my smoking hot wife started the unit. Our washer and dryer get beaten like rented mules with kid laundry. I tried this site, and decided to spend a little $$ on a replacement motor. I was impressed with the operator, she even asked what the symptoms were and helped to avoid wasting time and money.
The part arrived on time, and installed quickly. I am a hero in my wife's eyes, and that certainly carries weight.
Then again, I didn't have to dispose of the old dryer, pay for a new one, or haul the replacement upstairs.
Win-win!
The part arrived on time, and installed quickly. I am a hero in my wife's eyes, and that certainly carries weight.
Then again, I didn't have to dispose of the old dryer, pay for a new one, or haul the replacement upstairs.
Win-win!
Parts Used:
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Ryan from Raleigh, NC
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers, Socket set
9 of 12 people
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Squeaking sound then Barrel stoped turning
Unplugged the unit
Removed door and two clips that hold front panel on (6 Philip crews)
Then removed front panel by hand hold each side of the panel at the top
Of the “U” shape and pulling out ward until it frees it self from the two
Bottom clips.
You can now see a belt that is no longer tight around the drum
When I tried to put the belt back on I noticed the idler pulley was flopping around and I would need to replace it .That where you guys saved me.
Your exploded model and parts list made it easy to see exactly what parts I
Needed to order.
The rest gets a little tricky there is another plate that supports the barrel
A couple of clips that hold the top cover in place all of this must be removed
Note the top cover only need to be lifted up an inch or two at the front where the
Two steel clips where and doses not need to be removed to get this panel off that
Supports the barrel.
There are some wires attached to it also I only had to unplug the three that go to
The door safety switch then I was able to rotate it off to the side out of the way
And now the barrel can be lifted out. You can now remove the idler pulley assembly
I used pliers to remove the spring and a crocket wrench to remove a bolt that holds
The bracket that also should be replaced due to ware at the idler pulley barring pin
The tricky part is putting it all back together again. To explain this I would need to Wright a book. It takes a lot of good common sense. I was proud of how I reached
Around from each side of the motor and by feel alone and get the belt around
The motor pulley and the idler pulley that keeps the belt tight around the barrel
Makes me think I should have been a repairman.
Removed door and two clips that hold front panel on (6 Philip crews)
Then removed front panel by hand hold each side of the panel at the top
Of the “U” shape and pulling out ward until it frees it self from the two
Bottom clips.
You can now see a belt that is no longer tight around the drum
When I tried to put the belt back on I noticed the idler pulley was flopping around and I would need to replace it .That where you guys saved me.
Your exploded model and parts list made it easy to see exactly what parts I
Needed to order.
The rest gets a little tricky there is another plate that supports the barrel
A couple of clips that hold the top cover in place all of this must be removed
Note the top cover only need to be lifted up an inch or two at the front where the
Two steel clips where and doses not need to be removed to get this panel off that
Supports the barrel.
There are some wires attached to it also I only had to unplug the three that go to
The door safety switch then I was able to rotate it off to the side out of the way
And now the barrel can be lifted out. You can now remove the idler pulley assembly
I used pliers to remove the spring and a crocket wrench to remove a bolt that holds
The bracket that also should be replaced due to ware at the idler pulley barring pin
The tricky part is putting it all back together again. To explain this I would need to Wright a book. It takes a lot of good common sense. I was proud of how I reached
Around from each side of the motor and by feel alone and get the belt around
The motor pulley and the idler pulley that keeps the belt tight around the barrel
Makes me think I should have been a repairman.
Parts Used:
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John from Palmdale, CA
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Screw drivers, Socket set
8 of 9 people
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dryer wouldn't heat
First I unplugged the dryer. I shut off the gas line to the dryer. I opened the access door on the lower front of the dryer. I illuminated the interior of the dryer with a small flashlight that was mounted on two legs with magnets on the end to allow the light to be specifically directed. I took few digital pictures of the electrical connections to the dryer gas valve and the various sensors attached to the unit. I shut off the gas line valve to which the dryer gas valve was attached. I removed the two screws holding the dryer gas valve an lifted the unit out of the dryer. I vacuumed the inside of the dryer with an electric vacuum and also vacuumed the lint and dust off the gas valve I took out of the dryer. The flat style igniter was mounted on the front of the gas value. I removed two screws and took off the old flat style igniter. I reattached the new flat style igniter (carefully holding it by the ceramic mounting area to avoid breaking the igniter itself). I reinserted the gas valve into the dryer and reattached the two screws holding the gas valve into the dryer. I reattached the gas valve to the gas line in the dryer. I reattached the electrical connectors to the gas line and the sensors in the dryer. I turned the gas line in the house to the dryer back on. I plugged in the dryer and started it. No ignition.! I unplugged the dryer and reached in through the access door. I angled the flashlight to each of the sensors attached to the gas valve and the dryer electrical harness and pushed each one to make sure the electrical contacts were solid. When I checked the flame sensor ( a little box with a window mounted over a rectangle cut in the wall of the cylinder in which the flame burns when the gas is shooting out of the valve) the lower wire was unattached to the sensor. (Because the sensor sits on the side of the cylinder pointing towards the interior of the dryer its connections at the sensor was not visible. I bought a new flame sensor. I detached the old flame sensor from its connector, removed the screw mounting it to the cylinder and lifted it out of the tab holding it to the cylinder. I installed the new flame sensor by putting its tab in the slot for the tab in the cylinder and reattached the screw holding the flame sensor to the cylinder. I reconnected the electrical connection from the flame sensor to the dryer electrical harness. I plugged in the dryer. I turned the dryer on and got ignition of the dryer heater flame. Repair complete!
Parts Used:
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Barry from Highland Park, IL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
9 of 12 people
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replace rubber door seal on front load washer
On the Maytag front load washer, we found the easiest way was to unscrew and lift the top of the washer up, then take off the door, and front panel. Removing the old seal (moldy) was easy, but to replace the new one you need to see what you are doing. (Reaching up blindly to slip the new seal around AND connect the spring, is near impossible.) It was not hard to do...IF you can see what you are doing. You need access to attach the drain tube, make sure the gasket is slid in place (with notches in line with openings) slip the cable around and attach the spring. Everything is easy IF you can see what you are doing (and a little muscle to pull the spring and connect it).
Parts Used:
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cynthia from naperville, IL
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers
10 of 15 people
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Was not cycling
Figured out it had to be the timer after checking unit out and with a little research. Ordered a timer, it was so simple to replace just unscrewed cover and removed timer, it just plugs in, hooked it back up works like a charm.
Parts Used:
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Ken from Lyndhurst, OH
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
8 of 9 people
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motor not working
followed the diagnostics instruction in the Maytag Owners booklet which pointed to the Motor Control Assembly.
PartSelect was a very good choice for securing the part.
PartSelect was a very good choice for securing the part.
Parts Used:
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CECILE from BROOKLYN, NY
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver, Screw drivers
21 of 48 people
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Metal burr ate away felt and tumbler edge
My boyfriend took the dryer apart but was not available for the reassembly. I simply pulled up the detailed diagram that Part Select had in their database and was able to put it back together, although a little slower than anticipated.
Thank you for everything.
Thank you for everything.
Parts Used:
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Jill from Cape Corral, FL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
12 of 21 people
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After initial ignition & first heat cycle, gas valve would fail to re-ignite
The good: No need to pull out dryer beyond point where (wall) gas valve could be shut off.
The gotcha: Be sure to wear thick leather gloves to protect your hands. I discovered sharp edges the hard way!
The tip: To loosen gas valve inlet nut and to remove gas pipe from valve, use a bottom-to-top wrench motion. Despite threads being right-handed, this counter-intuitive operation (the thinking is that you are tightening the nut instead of loosening it) is necessary due to nut being located on the valve rather than the gas pipe which reverses the context.
The ending: Wife is happy to be back in the drying business and I'm happy just to have her happy not to mention saving a little $ in the process! Thanks PartSelect.com!!!
The gotcha: Be sure to wear thick leather gloves to protect your hands. I discovered sharp edges the hard way!
The tip: To loosen gas valve inlet nut and to remove gas pipe from valve, use a bottom-to-top wrench motion. Despite threads being right-handed, this counter-intuitive operation (the thinking is that you are tightening the nut instead of loosening it) is necessary due to nut being located on the valve rather than the gas pipe which reverses the context.
The ending: Wife is happy to be back in the drying business and I'm happy just to have her happy not to mention saving a little $ in the process! Thanks PartSelect.com!!!
Parts Used:
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Lawrence S from Rancho Santa Margarita, CA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Wrench (Adjustable)
10 of 15 people
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Motor won't run.
Followed the troubleshooting procedure that came with the
washer.Found problem,(with a little help from my experience
in electronics). Order motor and control board kit.
Followed the easy instructions that came with parts and
had it working in no time!!!!
Good job PartSelect !!!!
washer.Found problem,(with a little help from my experience
in electronics). Order motor and control board kit.
Followed the easy instructions that came with parts and
had it working in no time!!!!
Good job PartSelect !!!!
Parts Used:
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Vicente from Newnan, GA
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Socket set
10 of 16 people
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The dryer drum would not rotate when the start button was pushed.
First this I did was to disconnect the power cord. Then I removed the screws that held on the door and the two on the other opposite side. This allowed the front panel to be removed. Next I removed the top two screws which allowed the top to hinge up and out of the way. Then I removed the rest of the screws that held the front drum support and moved it to the side. I did have to unclip the wires that ran to the interior light. I did not how ever have to disconnect any wires at the front of the dryer. Next I reached in from the bottom of the drum and released the drive belt from the spring loaded pulley. at this point the drum was able to be removed out the front of the unit. This gave access to the motor. It was necessary to remove the several screws that held on the front half of the fan housing. Again I did not remove any wires as this too could be moved to the side out of the way. I then removed the snap ring and clamp from the fan end of the motor shaft and pulled the fan off of the shaft. Next I unclipped the wiring connector from the top of the motor and used a screw driver to pry the connector off. Next I used a socket on a long extension to push down on the motor clamps while tilting the socket out to allow the clips to release. I then removed and replaced the motor and assembled in the reverse order. While I had the drum out I inspected the rear support wheels and noted that one would hardly turn. I removed both wheels via a nut on the back side of the shafts. I found that one had shifted on the bushing and was making contact with the frame. I used a vise to press the wheel back into the correct location. I also applied anti seize with a small amount of dry graphite to both wheels and insured that the both rotated freely. I then installed the front two glide slide pads using the pop rivets provided in the kits. I used a shop vac and cleaned any lint from inside the dryer. I then reassembled the front covers in reverse of the disassembly process. I rotated the drum by hand prior to applying power. I also ran the unit with the heat off for the first five minutes. Total cost was under $160.00 or half of the replacement cost.
Parts Used:
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Bruce from Gladstone, MI
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set
7 of 7 people
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Noisy and thumping drum
I set the dryer on its back to make alignment of the front drum guide cover easy to reinstall in the seal after completion. I removed the 2 screws at the bottom front then removed the white and yellow wires to the interlock switch and set the front cover aside. I then removed the 4 nut screws holding the front drum cover and removed. On the back side there are two teflon and cork "bearings". I had ordered two even though only one was worn down to metal. On each one I then removed the two rivets by drilling them out. Then I placed the corks into the bearing slots with a little glue then inserted the teflon into the slots and riveted them into place with the rivets that came with the kit. I replaced the drum cover, connected the switch and screwed the dryer front cover back on. I set the dryer back up. Connected the vent hose and turned the dryer on. Beautiful sweet smooth and quiet operation. I had replaced the front and back drum seals a few months ago and saw the teflon was missing but did not have the kits at that time. With a complete job I would recommend replacing the front and rear drum seals and the two teflon/cork bearing kits at the same time.
Parts Used:
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Barry from League City, TX
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Difficulty Level:Really Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
7 of 7 people
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