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Models > MAT12CSDAQ > Instructions

MAT12CSDAQ Maytag Washer - Instructions

All Instructions for the MAT12CSDAQ
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Washing machine lid hinge balls fell off machine lid
First I had to hold the balls into the little holes on the side of the lid - one at a time- and tap the plastic ball into the side with a small hammer. I did the same with the other side. Silde the lid to match the holes located on the washing machine - give a little push to make sure that the balls are in place. You have your lid fixed to your machine where you can lift the lid and it will stay up without falling.

Note: If the balls fall out - make sure to tap a little harder so that the balls stay in place.
Parts Used:
Washing Machine Lid Hinge Ball
  • Sandra L from Warren, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
6 of 7 people found this instruction helpful.
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The washer would only go on the delicate cycle no matter what cycle it was set on.
This is a coin-op washer so the timer had to be removed through the coin box. The top lid was first removed from the coin box. There is one 5/16 hex head screw holding the timer in. After removing the screw the timer was lifted from the box. It is a tight fit that requires some wiggling around of the timer. There are two plug in wire harnesses attached to the timer. Because of the position of the timer the wires are a little short, but are able to be unplugged. The new timer was installed and the procedure reversed.
Parts Used:
Washer Timer
  • Don from Crescent City, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver
6 of 7 people found this instruction helpful.
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Very old washer was leaking oil and grease drops into the wash water.
Followed the procedures recommended for replacement of all the parts included in the Tub Bearing Kit and the Mounting Stem/Tub Seal kit as illustrated in a detailed, 32 minute repair video for the Maytag A606 washer which is available on YouTube. Many difficulties were experienced in the disassembly procedures due to extensive corrosion of tub bearing and tub stem parts (the washer is 47 years old).
I was not successful in using a special tub wrench that was purchased to break loose the old tub mounting stem and its threaded lock nut. The old tub mounting stem, lock nut, and the tub bearing race had to be cut off the threaded support shaft using a saws-all electric tool. Finally, corrosion on the edge of the tub caused problems with water leaks once the tub top and its rubber tub seal ring were reinstalled and the washer was put back into operation. The bottom line is that it may be questionable to attempt major repairs on washers that are 40+ years old and have any extensive corrosion in internal, mechanical parts.
Parts Used:
Mounting Stem/Tub Seal Kit Tub Bearing Kit
  • William A from PITTSBURGH, PA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
5 of 5 people found this instruction helpful.
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The washer would not spin
One of the easiest repairs I have done to this machine. I took off the back plate of the control panel (the machine was already unplugged) disconnected the connection, removed the old switch and replaced it with the new one. Once all that was done I connected the wires, screwed the back plate back on, plugged it in and started doing laundry.

The End.
Parts Used:
Lid Switch
  • Brian from West Hartford, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
6 of 8 people found this instruction helpful.
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The old pump was beginning to drag due to the age of the washer.
Removed the front panel. Then blocked up the front of the machine. Removed the pump belt. Removed the 3 5/16" screws from the bottom of the old one and tilted it slightly to remove. Put the new one in and reinstalled the 3 screws. Put the belt back on and slid new pump all the way to the right and tightened 1 screw. Loosened the screw until there was about 1/4" of gap when squeezed the belt together. Tightened the one screw, then the other 2. Put the front panel back on and lowered the machine. New pump works great.
Parts Used:
Drain Pump
  • Howard from ALBRIGHT, WV
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
5 of 5 people found this instruction helpful.
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Broken belt
It was as simple as leaning the machine back far enough so I could get to the belts - which were on the bottom. The diagrams that came with the ordered parts were right on. This is the first time I have attempted this myself - my repairman has retired - I'm sure I will do it again.
Parts Used:
Belt Kit Belt Kit
  • Edith from Cornwall, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
6 of 8 people found this instruction helpful.
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Water was leaking from under the front of the washer when it was used.
After turning the water off and unplugging the machine, I took the front panel off the washing machine. I then slipped the belt off the pump sprocket. The pump was right in the front and easy to remove. All I needed was a screwdriver, for the hose clamps, and a 5/16" socket to remove the old pump. I then installed the new pump, with the existing screws, re-attached the 2 hoses, slipped the belt back on, and popped the front panel back into place. The new pump works great and the leak is gone. The whole job onlt took about 30 minutes.
Parts Used:
Drain Pump
  • Greg from Manhattan, KS
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
5 of 7 people found this instruction helpful.
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Noise from dryer in spin cycle,
Found noise to be belt slapping the base sheet metal, from being too loose. Belt was loose because the drive pulley was worn and one side of pulley was loose! Used allen wrench to loosen the pulley set screw, and pryed off the old pulley. Replace d with new pulley and new belts. Works and sounds like new!
Parts Used:
Motor Pulley
  • curtis from ROCKDALE, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
4 of 4 people found this instruction helpful.
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Threads on old legs had been damaged in moving to new location.
Removed the damaged legs, replaced with parts from this site and leveled the washer .
Parts Used:
Adjustable Leveling Leg
  • Wayne from SEDONA, AZ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Wrench (Adjustable)
4 of 4 people found this instruction helpful.
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Broken Belts
Lets just say thank god for part select!!!! # 1 By far. This was a one two three job.
Parts Used:
Belt Kit Belt Kit
  • tommy from cortlandt manor, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
8 of 16 people found this instruction helpful.
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Repairs Were Easy.
Removed top. Removed agitator and tubs . Replaced seals and reassembled.
Parts Used:
Mounting Stem/Tub Seal Kit Tub Bearing Kit Belt Kit Belt Kit
  • James from Ventura, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
11 of 26 people found this instruction helpful.
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Resin balls on which the top loader lid hinges had broken.
Cleaned the cavities. Lubed them with olive oil. Inserted one ball on left side, while holding tension against that side to hold the ball in the lid and top indentations. Applied olive oil to right hand side indentation, and placed the new ball into lid indentation. Put lid down into closure cavity with ball, and with lid vertical, began pushing it rearward so as toslightly spring metal lid rolled edge and top metal away from one another UNTIL the new ball snapped into the hinge indentation in the machine cover. Done.
Parts Used:
Washing Machine Lid Hinge Ball
  • EL from O'Fallon, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
5 of 8 people found this instruction helpful.
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Washer would not start or fill up.
First of all unplug the washer and turned the water off to the washer. I second removed to back plate from the top control panel. Third using a 10mm nutdriver removed the two screws holding the control panel to the top of the washer, slid the control panel toward the front and flipped it out of it's grooves. Fourth unplug the lid switch. Fifth slide the old switch forward, up, and out. Finally replaced the new switch and lined the push button on the switch up with the lid detent switch. Plugged the cable switch back in, turned on the water, and plugged in the power cable. Tested the washer to ensure the switched was lined up correctly. Once the water started coming out. I turned off the machine unplugged the washer and finished reassembling the control panel. All in less than 10 minutes and SAVED myself over $130 for a service call.
Parts Used:
Lid Switch
  • DAVID from ATASCADERO, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
4 of 5 people found this instruction helpful.
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smelled like something smoking
took front panel off had 2 screws, propped up washer in front, took belts off with hands and put new ones on in reverse order One belt was badly cracked. I am 77 year old female, if I can do it, anybody can. great service on getting belts too. Thank you
Parts Used:
Belt Kit
  • Sharon from ANKENY, IA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
3 of 3 people found this instruction helpful.
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old belts slipping squealing, rubber shavings on floor.
Pull washer out from wall. Remove front panel (2 Philips head screws), swing bottom of panel out, remove panel. Tilt washer backwards, lean against wall to expose area under washer. Roll off old belts, roll on new belts. Move washer back upright, replace front panel, replace the philips screws, move washer back to original position.
Parts Used:
Belt Kit
  • Elzo from KALAMAZOO, MI
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
3 of 3 people found this instruction helpful.
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All Instructions for the MAT12CSDAQ
61 - 75 of 282