LG5791XSW1 Whirlpool Dryer - Instructions
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dryer would stall and the motor would hum before tripping circuit breaker
When the problem first came up, I took the dryer apart without first looking up any instructions. This wasn't difficult, but didn't realize when removing the fan from the motor, there is a square lug as part of the fan hidden by the rear clamp securing the motor. I was able to remove the fan by holding the motor shaft with a crescent wrench and removing the fan by hand, but was difficult and gloves were necessary in case the fan loosened quickly and my hand came in contact with the sheet metal (very sharp).
I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.
This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.
The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.
This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.
The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
Parts Used:
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Charles from Placentia, CA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Socket set, Wrench (Adjustable)
11 of 12 people
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One of the drum support rollers was worn out
I lifted the top of the dryer and removed the front panel. I removed the drum exposing the drum rollers. I replaced the rollers and reassembled the dryer. The exploded views on the web site made it easy to see what to do.
Parts Used:
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David from Fleetwood, PA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Wrench (Adjustable)
13 of 19 people
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squeaky and very loud noise
first we printed out directions from a couple of online repair sites that had pictures.
We followed the directions to remove the front of the dryer and removed the belt off the drier and then took out the drum. We had a hard time trying to keep the rear seal on so used CLOTHES PINS to put on the seal, then we added the adhesive replacing the clothes pins until the whole seal glued. Since the drum was already out, we put it in the sun to really dry the glue.
Next we attacked the drum support rollers. We removed the back of the dryer and used a 9/16" socket with an extention to remove the back nuts.
We took out the shaft, used sandpaper on it and then replaced the triangle clips and the support rollers.
Then put the back on again, then the front, making
sure the drum fit on the front. You have to then figure out the belt, with the rubber side down, and then work with the tensioner, which took my poor husband a while. Then lowered the top, put the clips back on and the bottom, making sure we turned the drum. It was a success after about 3 hours. You can do it a lot easier with pictures.
We followed the directions to remove the front of the dryer and removed the belt off the drier and then took out the drum. We had a hard time trying to keep the rear seal on so used CLOTHES PINS to put on the seal, then we added the adhesive replacing the clothes pins until the whole seal glued. Since the drum was already out, we put it in the sun to really dry the glue.
Next we attacked the drum support rollers. We removed the back of the dryer and used a 9/16" socket with an extention to remove the back nuts.
We took out the shaft, used sandpaper on it and then replaced the triangle clips and the support rollers.
Then put the back on again, then the front, making
sure the drum fit on the front. You have to then figure out the belt, with the rubber side down, and then work with the tensioner, which took my poor husband a while. Then lowered the top, put the clips back on and the bottom, making sure we turned the drum. It was a success after about 3 hours. You can do it a lot easier with pictures.
Parts Used:
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Jimmie from Lucerne Valley, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers, Socket set
11 of 13 people
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Dryer stopped spinning
The dryer quit working. I did some trouble shooting on your amazing site, ordered what i thought it might need and then got to work. Took no time to get it apart and replace roller kit and belt. What took the longest was getting in there and cleaning out probably 15 years worth of dirt and dust. If you have not opened your dryer up and done this, 10/10 recommend, because in doing so i found that the motor was the real culprit. Once i opened it up more, especially cleaning around the blower fan and motor, i was half a day in. Put it all back together and got it running for two more loads before the motor quit. Replaced that and since the hard work was done, had it back in in half an hour and running great. Probably will need to redo the felt seal one day, but for now, i am calling it a win. This is my go to site for all things and i have been able to work on most of my major appliances and do it myself using the helpful information here.
Parts Used:
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Danielle from FREEDOM, IN
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Difficulty Level:Really Easy
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers
13 of 19 people
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broken clip on top panel hold down
pressed clip into hole on top of front panel. first remove two philip screws that hold filter so you can lift top up.
Parts Used:
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Mark from Huntington Station, NY
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
15 of 26 people
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Badly worn idler pulley and rollers.
Braced dryer drum with a block. Removed the two rollers one at a time by using a screwdriver to pop off the triangular clip. Slid on new rollers. Would have been easier to remove the drum out the front instead of bracing it. Installed new idler pulley and belt. Dryer is 25 years old and sounds like a new one now when running.
Parts Used:
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TODD from GRASS VALLEY, CA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
11 of 14 people
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Drum would not turn and drum seal old
Watch the utube video a few times. Followed instructions. Marked all screws. Cleaned the inside of dryer where motor is. Replaced drum seal and then belt. I replaced front of dryer screwed everything in place and I did it. Holding drum in place while installing front of dryer was hard as it was heavy but I did it m. My friends and husband couldn’t believe it. Utube is great!
Parts Used:
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Geraldine from Stacyville, ME
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Screw drivers
11 of 14 people
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my teenage son was messing around and got into the dryer and broke the door catch and bent the door.
removed the catch and the pin and replaced it. We were sent a couple different sizes so we tested the one that looked like the closest match. I think the pin was made with different thicknesses of metal. Worked great and saved us from having to get a new dryer!
Parts Used:
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Dawn from Chesapeake City, MD
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
13 of 21 people
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Had to convert from natural gas to propane
Well, here's the rub...in order to find out what part I needed to order, I needed to take the dryer apart to where the gas controls are, and there on a sticker was a part number for an LP conversion kit. But, in order to get to that gas valve unit, I fumbled about figuring out how to take this brand new dryer apart, since there were absolutely no instructions whatsoever in the owners manual. And once apart, and pretty much all apart, I wondered how it would be that the Maytag repair man would be so lonely, as he'd have plenty to do.
However, the kit had great instructions as to how to take it apart and change out the orifices.
However, the kit had great instructions as to how to take it apart and change out the orifices.
Parts Used:
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Peter from The Rock, GA
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set
12 of 18 people
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LP gas conversion
Followed instructions, except to advoid sharp edges, and completed the job in under an hour.
Parts Used:
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Robert from Palmdale, CA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Socket set
11 of 15 people
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
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Jim from Foothill Ranch, CA
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
10 of 12 people
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Replaced a broken pulley.
Half of my pulley was broken off so there were no wrench flats to take it off. I was able to remove it using Channel Locks and the 7/16 wrench shown in the video.
Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Parts Used:
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Brian from IMLAY CITY, MI
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Difficulty Level:Very Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers, Wrench set
10 of 12 people
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Dryer only worked on one of three cycles
I started out by looking up information on the Internet to test the various dryer components (thermal switches, heating coil and timer) with a multi-tester. Everything checked out OK except for the timer. I knew it was bad anyway since only one of three cycles worked. It's good to check everything out while you have the back panel removed just in case other parts need to be replaced. Replacing the timer was very easy. Just remove one wire at a time and connect it to the new timer before moving on to the next wire. The new resistor, which came with the timer, was a different type, but was still easy to figure out how to connect with the provided instructions.
The hardest and most time-consuming part of the job was cleaning out all of the lint inside the dryer airways and all through the exhuast line - which vents through the roof of my house. I removed the lint filter airway from the dryer and found a lot of lint (one pound, maybe) caked up at the bottom, right next to the fan blade which pulls air through the dryer. After doing all of this, the dryer now dries like a new one on all cycles - even the automatic ones. Cleaning out the lint is crucial to helping the dryer not work harder than it has to, which saves you money on electricity (or gas)!
I bought my multi-tester at Radio Shack years ago. It has saved me hundreds of dollars by pinpointing the exact component which is causing the problem. Otherwise, you may buy parts you don't need that don't fix the problem. So, for about $104, my wife has a 22 year old dryer which performs like new and she is very happy about that. That's a lot cheaper than paying upwards of $400 for a new dryer - which we don't need yet.
The hardest and most time-consuming part of the job was cleaning out all of the lint inside the dryer airways and all through the exhuast line - which vents through the roof of my house. I removed the lint filter airway from the dryer and found a lot of lint (one pound, maybe) caked up at the bottom, right next to the fan blade which pulls air through the dryer. After doing all of this, the dryer now dries like a new one on all cycles - even the automatic ones. Cleaning out the lint is crucial to helping the dryer not work harder than it has to, which saves you money on electricity (or gas)!
I bought my multi-tester at Radio Shack years ago. It has saved me hundreds of dollars by pinpointing the exact component which is causing the problem. Otherwise, you may buy parts you don't need that don't fix the problem. So, for about $104, my wife has a 22 year old dryer which performs like new and she is very happy about that. That's a lot cheaper than paying upwards of $400 for a new dryer - which we don't need yet.
Parts Used:
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Jim from Plano, TX
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers
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Rust marks on clothing
Our dryer was leaving rust marks on our clothes that looked like a brown pencil mark. It turns out that the rear drum seal in our dryer was absorbing gunk over the years and we had to change it. It was a fairly easy fix but did require pulling the dryer almost completely apart. While we had it apart we changed this as well.
Anyone with a socket stet and screw driver can get it all apart.
On our machine, start by removing the 2 screws that hold the lint filter neck to the top of the machine (under the flap).
Then pry the top of the machine up in the front. It will pop up and you can fold it back.
Then you will need to remove 2 bolts and undo the plug.
From there you can pull the front off and get to the drum.Make sure you note how the belt tensioner comes out (under the drum) and how the belt is routed. It's quite basic.
After you get the drum off, peel the old seal(s) off and put the new seal(s) on as directed.
Pretty easy and our clean clothes stay clean now.
Anyone with a socket stet and screw driver can get it all apart.
On our machine, start by removing the 2 screws that hold the lint filter neck to the top of the machine (under the flap).
Then pry the top of the machine up in the front. It will pop up and you can fold it back.
Then you will need to remove 2 bolts and undo the plug.
From there you can pull the front off and get to the drum.Make sure you note how the belt tensioner comes out (under the drum) and how the belt is routed. It's quite basic.
After you get the drum off, peel the old seal(s) off and put the new seal(s) on as directed.
Pretty easy and our clean clothes stay clean now.
Parts Used:
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Patrick from Manor, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Screw drivers, Socket set
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.
The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.
I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.
I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
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Roger from Westminster, SC
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Difficulty Level:Very Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers
12 of 18 people
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