KEYE800THT0 KitchenAid Dryer - Instructions
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the drum was not turning because a broken belt
I lifted the top of the dryer cabinet, like the hood of a car using a screwdriver to pry it open. I removed the two screws in the upper right corner of the cabinet front. I disconnected the safty switch on the front door. The front of the cabinet can then be removed by lifting up the front off the pins in the base. With the drum exposed you can place the belt on and thread it through the two pulleys on the motor. Consult the diagrams provided on the PartsSelect website for the proper positioning of the belt on the pulleys. After the belt is installed spin the drum by hand one turn to make sure that it is seated properly on the drum and pulleys. Reassemble the dryer in the reverve order.
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thomas from bloomfield, NJ
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
14 of 19 people
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Dryer was getting hotter than blue-blazes, melted synthetics, damaged belt
Removed back of dryer, there were 3 screws on each side. There were two thermostats on the output vent and one thermostat on the heating element housing. Adjusted the temp settings on the thermostats per the instructions received with each thermostat (cross-refernece of original number required). Each thermostat had two screws and two wires. Terminals were coded "1" and "3," must get correct wires back in same place. The heating element thermostat required to splice new connector on one wire (per instructions enclosed with thermostat).. Easy as pie. BELT: Remove screws from lint screen housing, then pry up front of top of dryer and swing back (make sure you are next to the wall so it doesn't fall.) Remove the bottom front panel, remove the door tension springs, remove the two screws on the front of the front panel and remove the two top screws on the inside of the door panel (leave the door attached, but use tape to hold it shut so it doesn't hit you on the head) Careful of the door switch wire, carefully lean door up so it doesn't fall. The Drum will fall when front panel is removed, so have someone to help you hold it up. You do not have to remove the drum. With your frend holding the drum, go under and pull the tension spring roller back to slack up the belt and remove the belt from the tensioner and motor pulley. Remove belt from drum. Wrap new belt around drum (ribs down facing drum) and re-route belt around pulleys according to diagram in instructions (same way you pulled it off). I did it by myself, but I got konked in the head by the door, so be careful. Easy, but awkward. Watch for sharp sheetmetal edges.
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William from BURNET, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers, Socket set
17 of 29 people
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Door latch (female part) was broken.
I used a screwdriver to remove the old part and pushed the new part in with my fingers, it was very easy. If I could do it, anyone can. I was a lot cheaper then having a repair man come to house. I am very glad I found your site online, I will definitely be using your company again.
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JEANMARIE from BELLEROSE, NY
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
11 of 11 people
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Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
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Michelle from Richardson, TX
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
83 of 227 people
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dryer would stall and the motor would hum before tripping circuit breaker
When the problem first came up, I took the dryer apart without first looking up any instructions. This wasn't difficult, but didn't realize when removing the fan from the motor, there is a square lug as part of the fan hidden by the rear clamp securing the motor. I was able to remove the fan by holding the motor shaft with a crescent wrench and removing the fan by hand, but was difficult and gloves were necessary in case the fan loosened quickly and my hand came in contact with the sheet metal (very sharp).
I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.
This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.
The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.
This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.
The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
Parts Used:
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Charles from Placentia, CA
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Socket set, Wrench (Adjustable)
11 of 12 people
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Dryer would not generate heat
My dad was ready to spend $2000 on a new washer/dryer (he has to have a matching set!). Anyway, his dryer would not generate heat. A google search turned up partselect.com, which walked me through the procedure to see what we needed.
It turned out to be a simple to replace $25.00 part! The dryer is drying as if it was brand new. Saved $1,975. Hehe.
Thanks, partselect!
It turned out to be a simple to replace $25.00 part! The dryer is drying as if it was brand new. Saved $1,975. Hehe.
Thanks, partselect!
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Douglas from Greensburg, PA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Nutdriver
11 of 13 people
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broken clip on top panel hold down
pressed clip into hole on top of front panel. first remove two philip screws that hold filter so you can lift top up.
Parts Used:
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Mark from Huntington Station, NY
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
15 of 26 people
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Dryer runs heats up, will run for a short period and then shuts down, after a minute or two it will come back on and will resume drying.
Replaced the thermastat first, then the cutoff switch, still the same, I then replaced the thermister, and still have the problem.
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John from Brookings,, OR
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers, Socket set, Wrench set
18 of 36 people
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Replaced a broken pulley.
Half of my pulley was broken off so there were no wrench flats to take it off. I was able to remove it using Channel Locks and the 7/16 wrench shown in the video.
Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Parts Used:
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Brian from IMLAY CITY, MI
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Difficulty Level:Very Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers, Wrench set
10 of 12 people
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my teenage son was messing around and got into the dryer and broke the door catch and bent the door.
removed the catch and the pin and replaced it. We were sent a couple different sizes so we tested the one that looked like the closest match. I think the pin was made with different thicknesses of metal. Worked great and saved us from having to get a new dryer!
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Dawn from Chesapeake City, MD
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
13 of 21 people
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Lint Filter screen torn and rusted
Pulled to old out inserted the new. I would like to say your turn around from date part was ordered until I recieved it was three days, I find that amazing. I'm still waiting for a part I ordered from another company 1 month ago. The price was right shipping cost was very reasonable and your web site extremly easy to use. Thanks very much, Al
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Albert from Burlington, MA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
9 of 9 people
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Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
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Ronald from Oakdale, CT
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
10 of 13 people
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Old motor was making noise and tripping after a few minutes
I disassembled the dryer once to clean the motor and compartment. After reasembly, the problem persistes. I ordered the motor and the second diasasssembly was accomplished in 10 minutes and the entire job took 45 minutes and the dryer was running like new. Tip- Leave the motor secured while removing the blower fan.
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John from Midland, TX
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Pliers, Screw drivers
10 of 13 people
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Busted Dryer Belt
I order a new belt and I watched the video instructions on how to replace it, follow the instructions, removed the top and took out the dryer tumbler or can, found a broken idler pulley, order a new one, got it in about two days, replaced all the parts and now its working like a new dryer, I called several repair shops and I got estimates from $65 to $150, I spend less than $35 and it took me about 35 minutes to install and I got it fixed..
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Oscar from Dallas, TX
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
8 of 8 people
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Dryer had quit turning
I first disconnected the power cord and the vent hose. I removed the screws on the top of the back side to raise the top of the unit. There are also 2 screws holding the lint filter shoot which were also removed to allow the top to be lifted up. Its not necessary to remove the top since this would require disconnecting the wiring harness etc.
Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.
With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.
I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.
I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.
I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.
After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.
Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.
To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.
I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.
Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.
With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.
I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.
I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.
I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.
After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.
Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.
To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.
I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.
Parts Used:
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Martin from Lynchburg, VA
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
8 of 8 people
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