FDG546NBS2 Frigidaire Dryer - Instructions
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Not enough heat
Checked PartSelect online for people with a. similar problem. Found most common problem was the coils.
I opened the top, removed the two screws holding the front panel, unclipped the wiring harness from the machine to the door and removed/cut the plastic wire tie and front came off easily. I put the front piece to the side after changing the light bulb. I cleaned out a large amount of lint and found the coils on the left hand side without trouble. Carefully disconnected the wiring clips, unscrewed the holding screw and removed the old coils. Installed the new colis, 1 has three prongs and the other has 2 so you ca'nt mix them up. Replaced the hold screw, re-connected the witing harness, installed a new wire tie, and re-stalled the two holding screws. Closed the cover and turned it on.
At first it did not heat up which was dissappointing; but then I left it alone and 15 minutes later it worked like new! And heated up just fine ever since.
Total cost about $35.00 with shipping. I took a chance that I would not need the sensor or the ignitor based on the comments of others and I just bought the coils. If I had to do it over I would have bought all three and saved on the shipping.
I opened the top, removed the two screws holding the front panel, unclipped the wiring harness from the machine to the door and removed/cut the plastic wire tie and front came off easily. I put the front piece to the side after changing the light bulb. I cleaned out a large amount of lint and found the coils on the left hand side without trouble. Carefully disconnected the wiring clips, unscrewed the holding screw and removed the old coils. Installed the new colis, 1 has three prongs and the other has 2 so you ca'nt mix them up. Replaced the hold screw, re-connected the witing harness, installed a new wire tie, and re-stalled the two holding screws. Closed the cover and turned it on.
At first it did not heat up which was dissappointing; but then I left it alone and 15 minutes later it worked like new! And heated up just fine ever since.
Total cost about $35.00 with shipping. I took a chance that I would not need the sensor or the ignitor based on the comments of others and I just bought the coils. If I had to do it over I would have bought all three and saved on the shipping.
Parts Used:
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John from Bergenfield, NJ
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
4 of 6 people
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No heat
Raise the top and remove the front panel assembly. One philips screw, 24mm gas line coupler and 3 electrical connectors frees the burner assembly. Slid the old igniter out and the new one in.2 philips screws to remove the coil retainer and replace the coils.
Parts Used:
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Matthew from JOLIET, IL
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Difficulty Level:Very Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers, Wrench set
3 of 3 people
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The lint screen had tears on it which could cause a serious problem, possibly a fire.
I unscrewed the old the lint screen FRAME and easily removed it, replacing it with the new one. The new lint -- SCREEN -- just needed to be squeezed here and there, and molded into a better shape. The screen itself, arrived flattened on the bottom, causing it to be too wide and difficult to remove from the frame. I easily molded it with my hands into the shape of the previous one and it slipped right into place. ( Shaped like an oval, flexible sack.) VERY easy!
Parts Used:
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Joyce from North Dighton, MA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
3 of 3 people
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Lint screen had torn
For me it wasn't even a repair, but rather, open the package, take out and discard the old lint tray and pop the new one in! Done. I didn't have to replace the frame. I would like to comment on how easy ordering was from partselect.com and how quickly the part arrived. Very satisfied customer! Thank you!
Parts Used:
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Luann from Huntersville, NC
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
3 of 3 people
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The drier was "screeching"
First of all, the folks at Part Select have been terrific. I balled up my address and they were great in correcting my error and getting the parts promptly to me. They provide directions with the parts. And You Tube, is a wealth of information too. The process is to remove the drum and replace the nylon busihing that supports the drum at the back of the machine. Getting it out was no sweat. Getting the drum back in was a bit more challenging single handed. If I was going to make any suggestion it would be this is a good project for two sets of hands with the second set needed for about ten minutes. The You Tube video I watched said putting the front cover with the drum attached to the back of the unit would be the challenge and they were right. Otherwise, super easy and the results are it's back to "new" condition. Thanks again to Part Select!
Parts Used:
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Michel from CHICAGO, IL
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers
9 of 9 people
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Small burn marks on light clothing
First I unpluged the machine, then opened the top with a flat head screw driver. Then I removed the two screws inside, unpluged the door sensor. (makes it stop when opened) Removed old gasket, cleaned with emery cloth, cleaned the residue and applied the glue provided. Waited about 1 min. and applied the new gasket leaving about 1/8'' of it hanging over the door facing the drum.
Parts Used:
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Gordon from Canton, PA
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
3 of 3 people
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Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
Parts Used:
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Doug from ODESSA, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
3 of 3 people
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Needed new lint screen for dryer
Removed 2 screws and dropped new screen holder in with lint screen in it and replaced screws. Really easy
Parts Used:
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Harriett from Leesburg, FL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
3 of 4 people
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No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
Parts Used:
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Steven from San Francisco, CA
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
3 of 4 people
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heat would initially come on then go off or sometimes not come on at all.
1. unpluged the dryer and turned off the gas.
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
Parts Used:
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Vincent from Fairfield, CA
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
3 of 4 people
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screen fell out of lint screan frame
remove 2 screws,pull frame out. put new in. tighten 2 screws. put lint screen in
Parts Used:
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steve from scottsville, KY
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
2 of 2 people
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Wire Meshing Had Broken Away From The Rubber Framing Tha Was To Hold It Together And Lint Was Bypassing The Screen And Getting Into The Vent Tube.
Opened the dryer door unsrewed the two phillips holding the filter framework in place did a two second swap-out dropped the new unit into place the new unit and refastened it with the 2 screws that held the old one in place . And was drying a load of clothes within two minutes . . Thank you jg
Parts Used:
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JOHN from NAUGATUCK, CT
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
2 of 2 people
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Both knobs were broken
Ordered knobs on Monday early. Received midday Tuesday! Very fast delivery. Knobs fit perfectly, no tools required.
Parts Used:
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LAURA from MORGAN, TX
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
2 of 2 people
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replace old screen
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charles from nantucket, MA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
2 of 2 people
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Water temperature knob broke
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Michael from Weston, FL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
3 of 5 people
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