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Models > DGT400KW2 > Instructions

DGT400KW2 Kelvinator Dryer - Instructions

All Instructions for the DGT400KW2
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No heat.
As others have described in more detail... I lifted the top, removed the 2 screws holding the front panel (one on each side, inside the control panel on either side - not the easiest to get at, but not too bad), popped the clips holding the front panel in place and removed it. With the front panel off, the location of the coils is obvious (lower left side). The only challenging aspect of this repair is that the 2 screws holding the coils in place are really torqued in so it was crucial to use the exactly correct size screwdriver and not let the screwdriver slip while unscrewing those screws. Actually swapping out the coils took seconds, of course they have to go in exactly the same way as the old ones. I did take a few minutes extra to vacuum out years of lint from the inside of the dryer. Overall, much easier and cheaper than I was expecting and now I know where everything is inside the cabinet.
Parts Used:
M Series Ignition Coil Kit
  • Steven from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
3 of 4 people found this instruction helpful.
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heat would initially come on then go off or sometimes not come on at all.
1. unpluged the dryer and turned off the gas.
2. pulled dryer out so i'd have ample room to work on it.
3. used large flat blade screwdriver in the front between the top lid and dryer face to gently pop-up the lid.
4. removed 4 screws from inside, that hold the face to the main box leaving the wires all intact.
Found the coils on the lower left, held in place by two screws and plate.
5. took a good look at thier orientation before unpluging old and installing new, I recommend one at a time.
6. Vacuumm any exceess lint and check foam seal between lint trap and exhuast duc, the glue came undone on mine causing extra lint dust that is potentially flamable.
6. screw dryer front back on to main box, make sure to check wiring harness and that all electrical blade connectors are still pluged in to their componants.
7. At this point plug in, turn on gas and do a test run.
8.if everything checks out good then lower top make sure flexable exhuast hose is still connected on hte back of the dryer.
9. Tell your wife or girlfriend or husband or boy friend they can now finish your laundry :)
Parts Used:
M Series Ignition Coil Kit
  • Vincent from Fairfield, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
3 of 4 people found this instruction helpful.
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Gas flame turns off after a while, dryer keeps turning but no heat is generated.
Before this fix which worked beautifully, I tried replacing the flame sensor which did not work. To read that story, search under part number PS459818 (Flame Sensor). Our model is a Westinghouse, so access to the unit is a bit different than the other stories. It's a stacked front-loader sitting on top of a washing machine.

1. Open the little front door (lower left side) by unscrewing the little screw right below it. The door will pivot and slide out vertically.
2. Disconnect the electrical main lead coming from the back of the unit (just in case).
3. Close the gas switch lever on main gas pipe coming from the back on left side (just in case).
2. Remove 2 phillips screws on top of the metal bracket holding the two coils. The screws have to be removed completely along with the bracket. It's easy, they are right in front and there is room for the screwdriver. Use a thin long one instead of one with multiple bits to better align with the screws, which are very close to the coils.
3. The two coils slide right out and are very different so it's easy to keep them straight. Remove electrical connectors before or after removing the coils (I marked the plastic on top with a sharpie to keep them in the right orientation).
4. Drop in the two new coils and reconnect them to the electrical leads.
5. Reconnect main electrical lead from back (match wire colors)
6. Reopen gas lever on gas pipe.
7. Drop in front cover at an angle, tilt vertically and put screw back underneath. Use magnetized screwdriver or a piece of scotch tape to hold the screw or it might fall off the screwdriver.
8. Voila'. It worked.

This website is great. Our dryer is a Westinghouse bought in 1991 (almost 20 years old!) and with this fix it's just like new. In 1994 we used parts bought here to fix our washing machine (Westinghouse LT350RXW1). That machine is now 15 years old and still going!
Parts Used:
M Series Ignition Coil Kit
  • Giuseppe from San Francisco, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
3 of 5 people found this instruction helpful.
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Gas dryer wouldn't stay hot.
I definitely would not have tried to do this had it not been for the other testimonials written here. But it sounded so easy, I had to just try it (the repair man estimated that with parts and labor, we would be looking at somewhere between $250 and $300!).

The repair itself took less than 15 min, but I spend a good deal of time looking around the garage for a few screwdrivers and my socket set (me and tools don't meet too often). I could simply pry up the top cover on the dryer with my hands, then got it all the way up after removing two screws from the lint trap and undoing this really annoying wire connector thing. From there the front panel lifted off. To remove the drum, just had to release the tensonier on the belt, and it came right out. From this point it was really obvious where the replacement parts would be going. A few screws later, and I could swap the parts, and put humpty dumpty back together again.

It works!!!
Parts Used:
M Series Ignition Coil Kit
  • David from Petaluma, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
2 of 2 people found this instruction helpful.
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The lint screen was old, rusty, and torn.
This was the easiest and most inexpensive repair I ever had on a dryer. I did a search on the internet, found "PartSelect.com" searched their web site, found the part I needed (at a very reasonably low price) ordered it, received it within 2 days, opened the box, removed 2 screws from the old part, put the new part in, replaced the 2 screws, inserted the filter screen... and my wife was happy. Thank You PartSelect.com for perfect selection, ordering and service.
Parts Used:
Lint Screen and Frame
  • Paul from Dennis, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Door catch broken
Popped in the new door catch! Tightened the hinge screws( which work loose and allow the door to droop. The reason the catch broke!) Also put red Loctite on the screws in an attempt to keep them from backing out again! Working great so far!!!
Parts Used:
Door Catch
  • TJ from SCOTT DEPOT, WV
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
2 of 2 people found this instruction helpful.
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Riped lint screen
This was easer than, well brushing my teeth. And it took less time than that too. Really, really easy, just like I read.
Parts Used:
Lint Screen and Frame
  • Bill from Shelby, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
3 of 5 people found this instruction helpful.
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dryer lint screen rplacement
removed two screws - replaced lint screen replacement, TIME TO REPLACE UNIT - ONE MINUTE. What made this project a snap was the pictures and graphs( parts replace) uses to ensure you are ordering the exact screen .
Parts Used:
Lint Screen and Frame
  • Frank from Las Vegas, NV
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
2 of 2 people found this instruction helpful.
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replace old screen
take out of box remove old screen drop in new screen
Parts Used:
Lint Screen and Frame
  • charles from nantucket, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
2 of 2 people found this instruction helpful.
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Wire Meshing Had Broken Away From The Rubber Framing Tha Was To Hold It Together And Lint Was Bypassing The Screen And Getting Into The Vent Tube.
Opened the dryer door unsrewed the two phillips holding the filter framework in place did a two second swap-out dropped the new unit into place the new unit and refastened it with the 2 screws that held the old one in place . And was drying a load of clothes within two minutes . . Thank you jg
Parts Used:
Lint Screen and Frame
  • JOHN from NAUGATUCK, CT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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screen fell out of lint screan frame
remove 2 screws,pull frame out. put new in. tighten 2 screws. put lint screen in
Parts Used:
Lint Screen and Frame
  • steve from scottsville, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Very noisy
Replaced rear drum bearing, drum support bearing & drum belt. Still very noisy. Will order new motor & see if that does the trick.
Parts Used:
Drum Belt Rear Drum Bearing Kit Drum Support Bearing
  • Cherry from WATERVLIET, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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No heat to dry clothes.
There was a lot of screws. And I cleaned everything well. The one part was bad so I replaced them all to make sure it'll last.
Parts Used:
Igniter M Series Ignition Coil Kit Flame Sensor
  • James from SAGINAW, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Gas dryer would generate heat at the beginning of the cycle but would stop after 5 min and would start making a buzzing noise.
Unplug from electric outlet. Use putty knife to press on two brackets holding the top cover. Raise top cover. Unscrew two screws holding the front panel. Raise front panel up and move to the right (careful with the wires). Disconnect wires from coils. Unscrew two screws holding a small bracket holding the coils. Replace coils and reassemble everything. (HINT: make sure you drum is empty. Mine contained dump clothes, and it turned out front panel actually provides support to the drum, so mine was hanging there with some weight in it - probably not good).
Parts Used:
M Series Ignition Coil Kit
  • Denis from LONGMEADOW, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Drum would not spin
After unplugging the dryer, disconnecting it from the vent, and moving into an open work area, I popped the top open with the blade of a screwdriver, disconnected the two wires that connect to the door switch, then lifted the front panel (with the door) up and away from the drum. Next, I lifted the drum out of the worn rear bearing assembly and lowered it into the dryer in order to release tension on the belt. I then removed the entire drum by carrying it forward and out of the way. I then removed the old bearing assembly, which was loose and covered with metal dust. After cleaning the area with a dry cloth to remove the old grease and metal dust, and vacuuming all the lint off *everything*, I installed the new bearing assembly with a 5/16" nut driver, being careful to position the provided ball-bearing between the plastic bearing assembly and the outer clip. The little ball-bearing is very important, as it is the drum's only path to ground, and prevents the build up of static electricity as the drums spins. I then filled the new bearing assembly with the provided grease. Everything is easy up to this point, but the difficult part for me was removing the old hub from the drum and re-attaching the new one. It is held on by three screws and they become seated very tightly. After loosening them and removing the old hub from the drum, attaching the new one prvoed difficult as well, as the screw-holes in the new hub are not threaded to fit the screws. The screws muct be forced to cut a thread as you install them, which requires a great deal of force. After installing the new hub and putting the new belt (pruchased separately) around the drum, the next step is to reinstall the drum by lifting it in through the front of the dryer and positioning the new hub over the new bearing assembly and pressing it down into place. It will gently "snap" into place as it seats. Then, on the back side of the dryer, I removed the vent panel by removing the two screws that hold it in place and positioned the new drive belt (loosely dangling around the drum) over the motor's drive wheel and behind the sring-tensioned idle arm. Then it is a simply matter to reinstall the front panel by genly lifting the drum and sliding the door opening inside it, then reseating all the little clips that hold the front panel in place. I then pressed the top back into place, reconnected the vent hose, plugged it back in and checked for operation. My fifteen year-old dryer now works like new!
Parts Used:
Drum Belt Rear Drum Bearing Kit
  • garland from Morganton, NC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
3 of 5 people found this instruction helpful.
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All Instructions for the DGT400KW2
61 - 75 of 456