CFRE5714KW0 Frigidaire Dryer - Instructions
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Screeching noise under load
I basically followed the video instructions on your website. Pretty simple but ran into an issue pre-threading the 3 self taping screws into the spindle bearing. The screws provided were blunt on the end and did not tap easily at all. I used the existing screws that were much more "sharp" and worked much better. Also, the new screws were Philips drive and due to the amount of torque trying to self tap nearly stripped them out. The old sharper screws were square drive which had a better bite. So basically, I used the old screws to self tap and then used the new screws for the final installation.
It took a long time to clean all the lint out from the inside of the dryer. The motor was completely embedded with lint and animal hair. You may want to suggest that a good cleaning may be needed so bring a shop vac...and also something to carefully pick the lint balls out from around the motor armature and bearing area. Overall the video instructions were really a big help!
It took a long time to clean all the lint out from the inside of the dryer. The motor was completely embedded with lint and animal hair. You may want to suggest that a good cleaning may be needed so bring a shop vac...and also something to carefully pick the lint balls out from around the motor armature and bearing area. Overall the video instructions were really a big help!
Parts Used:
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John from WESTLAKE, OH
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
4 of 4 people
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Dryer was getting very hot
I watched videos so I would know what I was doing. Well No, My thermostat was in the front of the dryer. But after a little blood and sweat, and I am not kidding, I got the front off. I ordered my new part. Finally got it in Spent $40.00 and it still doesn't work. I know it was the right part. I checked all the trouble shooting web site. That was the only thing they said it would be. Friends advice tell me it is the brains of the thing and I need a new one. Well not 2 weeks before Christmas. Thanks for asking. Single hard working mom.
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marjorie from Cary, NC
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Difficulty Level:Difficult
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Total Repair Time:More than 2 hours
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Tools:Screw drivers, Wrench set
9 of 19 people
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heater element was broken
I removed dryer exhaust hose.unsnapped top cover the clips are in front and exposed inside of dryer,remove 2 screws on inside of front cover and set aside. remove lower cover in back and push belt extender until belt is loose remove 3 screws on inside of tumbler. remove tumbler out the front of dryer be careful not to damage belt set aside remove ball plate by pulling up and out it will unsnap. Now remove 2 sets of wires that are connected to heater element plate remove 4 screws holding element plate in place. Since dryer was all exposed I cleaned everything out with a wet vac put back together following instructions in reverse. Good luck
Parts Used:
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eufemio from deltona, FL
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Difficulty Level:Easy
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
5 of 8 people
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dryer had no heat and stopped turning
i first looked up the diagram for this model and checked for the best way to take the front cover off the dryer. after removing the front cover i start looking for the wires that connect the door switch and remove the wires. the front cover also supports the weight of the drum, so carefully pull the cover until the drum comes loose. at this point you can visually see the parts of the parts that make up the workings of the dryer. i first noticed the drum was coming out with the front cover at this time i knew the rear drum assembly was broke. i then took the belt loose from tension pulley and slid it off the drum and removed both from the cabinet. after the drum was removed i also noticed the heating was broken in several places. i removed four screws from the heating element assembly and also removed two wire that were connected to the element. with all pieces removed i checked the thermal switches, there are three switches, one on the heating element, one on the vent side and one on the back panel of the cabinet. i then installed the rear drum assembly and the heating element assembly and connected the wires. i then slid the drum almost all the in place and put the new belt around the drum and dropped the rear drum into the bracket that supports the rear drum then run the belt around the tension pulley and around the motor pulley. i then placed the front panel back in place and connected the wires for the door switch and lifted the drum assembly up just enough to insert the front panel door support into the drum and placed the clips in place, checked all connections twice and connected power back to the unit and turned on and run it through all its settings.
Parts Used:
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Eric from Spicewood, TX
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Nutdriver, Screw drivers
5 of 8 people
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My lent screen broke on my dryer
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Mary from Garland, NC
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Pliers
4 of 5 people
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Knob needed replaced.
I ordered a new knob on 12/22 and received it 12/27. Put in place of the broken knob, all fixed! ! ! All the appliances in my home are Frigidaire. I bought medium priced machines. W/D are about 7 years old. Dishwasher is about 5 years old. Fridge and stove are about 3 years old. They have all served me well and when they need replaced, I will shop for Frigidaires.
Parts Used:
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Sharon from Moses Lake, WA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
4 of 5 people
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door catch wasn't working and screws in door were loose.
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NICOLE from WEST JORDAN, UT
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Screw drivers
12 of 29 people
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Cloths not drying
Removed the back panel and the exhaust hose.removed the heater element and changed the thermostat wire was melted cut damaged part of wire soldered and rapped with black electrical tap
Parts Used:
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keith from ELLENVILLE, NY
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
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Tools:Pliers, Screw drivers, Socket set
5 of 8 people
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Squeaking noises (very high pitch)
Replace rear bearing, found Exhust tube seal broken. Went ahead and replaced Drum belt & Idler arm assembly. Works like New !
Parts Used:
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Bruce from Liberty, TX
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers
5 of 8 people
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The timer would not shut off.
Removed back of the control panel. Removed 2 screws unplugged the wires. Plugged wires into the new timer, put the back cover on. Worked great.
The repair man was going to charge us twice the cost of the part ($150) plus labor. He even recommended buying a new dryer rather then putting the money into fixing this one!
The repair man was going to charge us twice the cost of the part ($150) plus labor. He even recommended buying a new dryer rather then putting the money into fixing this one!
Parts Used:
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David from Worthington, MN
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Screw drivers
4 of 5 people
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dryer wouldn't tumble with normally large load - very noisy when it did tumble
I disassembled the dryer using instructions from the following website for White Westinghouse (pictures really helped)
After removing the drum, I first noticed that the grouding ball was sitting on the bottom of the dryer (along with much lint). I then saw that the bracket for bearing support cup and the bearing support cup were both worn well past use. The bracket had been worn down about 1/4" to the SE with matching wear on the bearing support cup. There was a hole in the bottom of the bearing support cup (hence the grouding ball on the floor of dryer).
I installed the new idler pulley assembly and completely vacuumed out the dryer (I didn't know lint could get so stiff!). I installed the new parts from the kit once received (and the new belt bought previously) and the dryer works great. I'm so used to the obnoxious squealing that it seems odd to be so quiet.
The internet is a magnificent thing!
After removing the drum, I first noticed that the grouding ball was sitting on the bottom of the dryer (along with much lint). I then saw that the bracket for bearing support cup and the bearing support cup were both worn well past use. The bracket had been worn down about 1/4" to the SE with matching wear on the bearing support cup. There was a hole in the bottom of the bearing support cup (hence the grouding ball on the floor of dryer).
I installed the new idler pulley assembly and completely vacuumed out the dryer (I didn't know lint could get so stiff!). I installed the new parts from the kit once received (and the new belt bought previously) and the dryer works great. I'm so used to the obnoxious squealing that it seems odd to be so quiet.
The internet is a magnificent thing!
Parts Used:
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Rebecca from Kansas City, MO
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Difficulty Level:A Bit Difficult
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers, Socket set
5 of 9 people
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knob slipping on shaft
ordered new knob from part select. pull off old knob and replaced it with new knob. Now i can set the timer correctly for my clothes to dry. less than 30 sec to repair.
Parts Used:
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Robert from SALVISA, KY
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Difficulty Level:Very Easy
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Total Repair Time:Less than 15 mins
3 of 3 people
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Broken selector knob
Just pushed it on. The gray on the knob is a little lighter shade than the original, but not a problem.
Parts Used:
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Blanche from Mansfield, PA
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
3 of 3 people
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Black lines and small tears
Previous comments on line were so helpful.
My husband and son took the dryer apart by removing the top in order to get to the drum. Part of silver rim that the Drum Glide is attached to was broken,it had been cut somehow. They had to soder it back in place so they could attach the Drum Glide and so far it's working.
Felt- I just ordered one with the adhesive and removed the damaged section used a wire brush, applied the adhesive ( which was more than enough) waited a few minutes for the adhesive to set, applied the felt, attached binder clips to hold it in place while working on the Drum Glide. Really easy.
My husband and son took the dryer apart by removing the top in order to get to the drum. Part of silver rim that the Drum Glide is attached to was broken,it had been cut somehow. They had to soder it back in place so they could attach the Drum Glide and so far it's working.
Felt- I just ordered one with the adhesive and removed the damaged section used a wire brush, applied the adhesive ( which was more than enough) waited a few minutes for the adhesive to set, applied the felt, attached binder clips to hold it in place while working on the Drum Glide. Really easy.
Parts Used:
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Robin from Sewaren, NJ
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Screw drivers
3 of 3 people
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Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
Parts Used:
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Doug from ODESSA, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
3 of 3 people
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