LW9203-W2 Amana Washer - Instructions
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Frayed V-belt
VERY EASY!!!
SAFETY FIRST-Always unplug the appliance.
Use 8mm socket to remove front panel screws. Loosened up two hose clamps connected to the pump and removed both lines (Hoses contain water, use a towel) which is located underneath the motor. Disconnect motor electrical connector on the left side of the motor. With socket, remove 4 mounting bracket screws that secure the motor and pump assembly. Pull back the tension/idler pulley to loosen belt off the main pulley to the washer drum. Tilt and pull out motor/pump assembly. Underneath the pump, use star-bit to remove the pump from motor assembly to remove the belt. Install new belt on motor pulley (Good time to check for debris or anything restricing free movement of pump) and re-install pump. Install the motor/pump assembly and loosely secure the motor/pump assembly. Place the belt onto the motor pulley and pull back the tensioner/idler pulley to allow slack of belt to be placed on washer drum pulley. Put the belt on the lip of the drum pulley and rotate while pulling back the tensioner/idler pulley until the belt is seated on the groove of the drum pulley. Tighten the motor/pump assembley. Re-attach the 2 hoses and tighten down the clamps. Re-connect the electrical connector to the motor...Don't forget to plug in the washer and secure the front panel...Piece 'O cake, you're done! About 15 minutes to do the job. Much like changing a belt on most vehicles.
SAFETY FIRST-Always unplug the appliance.
Use 8mm socket to remove front panel screws. Loosened up two hose clamps connected to the pump and removed both lines (Hoses contain water, use a towel) which is located underneath the motor. Disconnect motor electrical connector on the left side of the motor. With socket, remove 4 mounting bracket screws that secure the motor and pump assembly. Pull back the tension/idler pulley to loosen belt off the main pulley to the washer drum. Tilt and pull out motor/pump assembly. Underneath the pump, use star-bit to remove the pump from motor assembly to remove the belt. Install new belt on motor pulley (Good time to check for debris or anything restricing free movement of pump) and re-install pump. Install the motor/pump assembly and loosely secure the motor/pump assembly. Place the belt onto the motor pulley and pull back the tensioner/idler pulley to allow slack of belt to be placed on washer drum pulley. Put the belt on the lip of the drum pulley and rotate while pulling back the tensioner/idler pulley until the belt is seated on the groove of the drum pulley. Tighten the motor/pump assembley. Re-attach the 2 hoses and tighten down the clamps. Re-connect the electrical connector to the motor...Don't forget to plug in the washer and secure the front panel...Piece 'O cake, you're done! About 15 minutes to do the job. Much like changing a belt on most vehicles.
Parts Used:
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John from Milton, PA
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
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Water leaking on floor from "mysterious place underneath washer"
Water was leaking on the floor during the wash cycle and especially during draining of the washer. I removed the front panel at ground level and watched while draining after a rinse.
I t was obvious that water was spraying from a hole in the rubber end of the hose (the hose is a fused assembly of a plastic section and a rubber section).
So, I finished draining, removed the hose (required pliers to squeeze off a hose clamp).
Upon inspecting the hose, it was also apparent that the hole was caused by rubbing against a support bracket for the motor. This should not happen, but it did because the plastic standoff supposed to keep the hose away from the bracket was installed 180 degrees backwards.
So, I simply replaced the hose and turned the bracket around to the correct orientation.
Everything worked as planned and my repair cost was much less than if I had called someone out.
I t was obvious that water was spraying from a hole in the rubber end of the hose (the hose is a fused assembly of a plastic section and a rubber section).
So, I finished draining, removed the hose (required pliers to squeeze off a hose clamp).
Upon inspecting the hose, it was also apparent that the hole was caused by rubbing against a support bracket for the motor. This should not happen, but it did because the plastic standoff supposed to keep the hose away from the bracket was installed 180 degrees backwards.
So, I simply replaced the hose and turned the bracket around to the correct orientation.
Everything worked as planned and my repair cost was much less than if I had called someone out.
Parts Used:
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Bryan from Chicago, IL
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Difficulty Level:Easy
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Total Repair Time:Less than 15 mins
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Tools:Pliers, Socket set
51 of 57 people
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The Seal On The Bottom Of The Tub Was Leaking
Removed the front of the washer, then lifted the top up and held it up with a prop. Pulled the agitator straight up and started the disasembly. Using the photos in the hub and seal kit was a big help. The large nut on the output shaft had to be cut off with my dremel tool and the hub removed with a wheeler puller. Assembly was pretty much straight forward. Primed the pump and started the machine for the stated time and was a sucess.
Parts Used:
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HOWARD from CORTLAND, OH
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
34 of 43 people
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Bearing went out causing lots of noise.
This is not a bad repair, but give yourself some time. I did not have to take the tranny and motor out, but the inner and outer tub and all related parts had to come out, along with the outer tub base. If you are replacing the tub bearing, you HAVE to order the seal kit. Don't try to skimp like I did, since you will need the seal kit as this is what causes that bearing to fail in the first place. We forgot how quiet the washer was after I fixed it, and it saved us from buying a new washer since we were ready to say the heck with it and buy a new pair. You might need an 1.5 inch socket to get the big nut off the spindle, but I was able to get with a visegrip and hammer. The nice thing about this repair is even if you screw it up, you won't have water all over the place because of the seal design. I just checked under the washer a few times for the first few weeks and all seems fine.
Parts Used:
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mike from hull, IA
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
24 of 26 people
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tub leaking water
Took off the agitator, removed inner tub, exposing the hub drive. Found fusion between hub drive and agitator shaft. Rather than using a wheel puller as instructions recommended I got my masonry hammer and removed the drive hub in pieces. Removed debris from the tub. Installed sealant around lower seal as instructed. Re-assembled inner tub, agitator with new upper seal. Plugged in the washer, turned on the water. No leak. Happy happy.
Parts Used:
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Raymond from East Sandwich, MA
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Socket set, Wrench set
18 of 22 people
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Did not know the hub nut hex wrench was needed till I got everything torn apart
I did as the directions said that came with the kit. Except everything came off by hand until I got to the hub nut. Instead of waiting for another shipment and buying a tool I would have used once and never touched again I called SEARS and a technician came to my house because I did not have the hub nut hex wrench. He called it a spanner wrench. Once he used the tool to get off the nut I was in business. Until I had to put the nut back on. I ended up wrapping a towel around the end of a 12" adjustable crescent wrenc and litle by little smacked it with a hammer until the nut looked like it was all the way down. Just to put the nut back on my way took almost an hour alone. The directions said that a puller was needed to get off the adjutator shaft (unsure of correct name), but it came off with a little wiggleing. Once I put the new one on it would not budge off so a small puller would have been needed to remove it if I needed to again. And puting it back on was a chore in it self. I ended up using a hammer and 6" 1/2" drive extension with a 20 something MM socket on the end to force it down all the way. And the shat that the large seal goes over also requires a tool which is also not mentioned until you read the directions. I was able to twist and force on the new one with a little bit of included grease around the meeting surface. For the most part the directions were correct, but left out a bunch of nice to know things that the average person who is not mechnically inclined may not have figured out. Overall the whole procedd was pretty easy once all the tools were available. Suggestions I would make are to say in the advertisement of the seal kit that the Hub nut hex wrech (spanner wrench) and seal tool will be needed inorder to complete the removal and/ or installation. Which are sold seprately.
Parts Used:
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Robert from Yucaipa, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Screw drivers, Socket set, Wrench (Adjustable), Wrench set
15 of 17 people
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Leaked Water through lower tub seal
1st, I removed the top, back and side panels. Then removed the plastic parts off the top of the tubs. Next removed the agitator from it's hub. In the center of the agitator hub was a retaining bolt to be removed next using a 7/16" socket. Had to use a gear puller to get the agitator hub up off it's spline. Then there were four 1/2" socket size hex bolts to remove facilitating the removal of the inner stainless steel tub. Next was the toughest part of my task, the removal of the large hex nut holding the inner tub hub down. Since I did not have a socket large enough to fit the nut, I used a ball peen hammer to loosen it by striking it on it's hex flats in an angle that would tend to drive it in a CCW rotation. It took several blows but finally it began to loosen. Then removed it with my Channel Lock water pump pliers. Once the Inner tub hub was removed, the lower seal was accessible. Removed the old seal from the outer tub flange, and scraped off all the old sealant with a razor blade scraper. Then installed the new seal according to the instructions supplied with the new hub and seal kit. Re-assembled the washer, ran it through a cycle while it was still out in the garage to ensure the leak was fixed and was happy to find that indeed it was. Everything went fairly well if you overlook the slight cut on my right thumb I suffered while re-assembling the covers. It wasn't too bad, a band aid fixed it up.
Parts Used:
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John from Greenup, IL
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
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Washer began to leak about a pint of water per load. Water was stained black by residual belt abd brake dust the water was picking up as it dripped throught the machine.
I followed the instructions that came with the hub and seal kit, which were pretty well written but not terribly detailed. Once I got into the job though, I felt confident that the instructions told me all of the important information--the rest was common sense. If you're reasonably handy you can pull this off.
The instructions call for some specialty tools, which I was able to do without by using the following:
• Drive Bell:
The old drive bell slid right off without a puller--I think I got lucky on this one.
To install the new drive bell I used a long 1/4-20 bolt, nut and fender washers. I spun a nut way up the bolt then slid the fender washers on. I threaded all of this down into the transmission output shaft until it bottomed out. Then I turned the nut down to push the washers and drive bell down until it hit bottom. Then I backed out out the bolt and washers and installed the shoulder screw.
• Hub:
I used a generic wheel-puller I already had to get this off and it came off with little effort. I put the old shoulder screw back into the top of the shaft for the point of the puller to sit on so it wouldn't mess up the transmission output shaft or threads (obvious, I know but a bad thing to overlook).
Drive Bell Seal:
• This calls for seal tool #293P4. I'm sure the seal can be installed by hand but it happened that the two extension tubes from my Shop-Vac were exactly the right diameters to seat the bottom and top parts of the seal.
• Lint filter:
The instructions just say "remove lint filter" but it was pretty stuck on and seems pretty fragile so I took it easy. I used a small scrap of 1/8-inch plywood to slide under the edge until it popped off.
The instructions say not to use the four rubber washers on the bolts that attach the inner tub to the hub if the machine has a stainless tub. Mine has a stainless tub and the original bolts had rubber washers on them so I used the new washers when i reinstalled the inner tub.
I found the 3M-800 Scotch Seal industrial sealant at a local appliance pats distributor. I researched it and it seemed like a specific enough product that it wasn't worth risking the whole job to use something I already had like Lexel. I learned that the reason it doesn't come with the kit is that it requires Haz-Mat handling, which would probably double the cost of the parts kit. One set of instructions I read from Maytag said that "the customer can use the machine after 15 minutes". But the sealant tube says it fully cures in 1 - 3 days. So I squirted out a ribbon on a piece of paper when I did the job so I could monitor the drying time and split the difference, allowing it to dry overnight. Seems as though that's long enough.
I did the job step-by-step and it seems to have worked. The first load is running right now and so far it's dry as a bone.
One thing I noticed is that some of the parts seem to have been updated over the original ones to improve performance. The drive bell and associated seal have a more sophisticated mating relationship that seems as though it will provide a better seal than the original.
Good luck
The instructions call for some specialty tools, which I was able to do without by using the following:
• Drive Bell:
The old drive bell slid right off without a puller--I think I got lucky on this one.
To install the new drive bell I used a long 1/4-20 bolt, nut and fender washers. I spun a nut way up the bolt then slid the fender washers on. I threaded all of this down into the transmission output shaft until it bottomed out. Then I turned the nut down to push the washers and drive bell down until it hit bottom. Then I backed out out the bolt and washers and installed the shoulder screw.
• Hub:
I used a generic wheel-puller I already had to get this off and it came off with little effort. I put the old shoulder screw back into the top of the shaft for the point of the puller to sit on so it wouldn't mess up the transmission output shaft or threads (obvious, I know but a bad thing to overlook).
Drive Bell Seal:
• This calls for seal tool #293P4. I'm sure the seal can be installed by hand but it happened that the two extension tubes from my Shop-Vac were exactly the right diameters to seat the bottom and top parts of the seal.
• Lint filter:
The instructions just say "remove lint filter" but it was pretty stuck on and seems pretty fragile so I took it easy. I used a small scrap of 1/8-inch plywood to slide under the edge until it popped off.
The instructions say not to use the four rubber washers on the bolts that attach the inner tub to the hub if the machine has a stainless tub. Mine has a stainless tub and the original bolts had rubber washers on them so I used the new washers when i reinstalled the inner tub.
I found the 3M-800 Scotch Seal industrial sealant at a local appliance pats distributor. I researched it and it seemed like a specific enough product that it wasn't worth risking the whole job to use something I already had like Lexel. I learned that the reason it doesn't come with the kit is that it requires Haz-Mat handling, which would probably double the cost of the parts kit. One set of instructions I read from Maytag said that "the customer can use the machine after 15 minutes". But the sealant tube says it fully cures in 1 - 3 days. So I squirted out a ribbon on a piece of paper when I did the job so I could monitor the drying time and split the difference, allowing it to dry overnight. Seems as though that's long enough.
I did the job step-by-step and it seems to have worked. The first load is running right now and so far it's dry as a bone.
One thing I noticed is that some of the parts seem to have been updated over the original ones to improve performance. The drive bell and associated seal have a more sophisticated mating relationship that seems as though it will provide a better seal than the original.
Good luck
Parts Used:
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Sheldon from North Yarmouth, ME
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
13 of 14 people
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Wouldn't agitate or spin.
This was my fist time attempting to fix a washer. I had to guess on the length of the belt since the model number on the machine had worn off and the belt had snapped in a way that made determining the length difficult. At first, I ordered a belt that was too small. I realized this after I was unable to remount the motor stand onto the bottom of the machine. This model had the motor assembly right in front of the unit. It was easily accessed after removing the panel on the front of the machine. It was easy to remove the 4 screws (they were all visible) on the motor stand. After that I was able to disconnect the pump belt. This machine has seperate belts for agitation and the pump. The pump belt must be removed in order to install the agitator belt because they both are driven by the same shaft and the pump belt is positioned on the bottom. There is also a tension wheel for the agitator belt which might be easily overlooked. Make sure to install the agitator belt so that the tension wheel is on the outside of the belt's path. The whole job is fairly easy if you have the right part to begin with. If you have to force the belt onto the wheels, then you probably have a belt that is too small.
Parts Used:
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Eric from Akron, OH
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Difficulty Level:A Bit Difficult
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver
9 of 9 people
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The thin walled plastic drain line got a pin hole leak
The washer is four years old.
This is the second time I needed to replace this same drain hose on this same washer since I had the machine
There is only my wife ant myself maybe, 2 -3 medium size loads per week - why I would have two drain lines develop the same problem in almost the same location in two years is disconcerting
There must be a design problem with the clear plastic hose - Suggest Maytag go to a thick walled rubber hose
The hole is alway inside the washer on the bottom just after the hose bracket - I suspect that something rubbing causing a small pin hole to develop - when the condition first starts it is very difficult to located -There will be water under the washer
Run the washer and discharge the water - to locate
The replacement must be made through the lower front removable panel - and is easier to do if the pump return hose is also disconnected from the pump
Be very carful with the thin wall replacement hose - very light weight plastic - do not pull across the floor of washer - it could easily get damaged
Your company did a get job getting the part to me - The Fed Ex track system was great
I could tell exactly where the delivery was al all times -
This is the second time I needed to replace this same drain hose on this same washer since I had the machine
There is only my wife ant myself maybe, 2 -3 medium size loads per week - why I would have two drain lines develop the same problem in almost the same location in two years is disconcerting
There must be a design problem with the clear plastic hose - Suggest Maytag go to a thick walled rubber hose
The hole is alway inside the washer on the bottom just after the hose bracket - I suspect that something rubbing causing a small pin hole to develop - when the condition first starts it is very difficult to located -There will be water under the washer
Run the washer and discharge the water - to locate
The replacement must be made through the lower front removable panel - and is easier to do if the pump return hose is also disconnected from the pump
Be very carful with the thin wall replacement hose - very light weight plastic - do not pull across the floor of washer - it could easily get damaged
Your company did a get job getting the part to me - The Fed Ex track system was great
I could tell exactly where the delivery was al all times -
Parts Used:
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WALTER from Holualoa, Hawaii, AL
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Pliers, Wrench set
9 of 10 people
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Due to the age of the washer, everything on the bottom end was rusted or corroded together tightly.
To remove the drive bell, I drilled numerous holes through the top and split it apart with a screwdriver. The hub was really stuck and due to the unavailability of a 6" puller, I was forced to drill holes in the center section, tap the holes and use a harmonic balancer puller, PB Blaster, and propane torch to remove the hub. After removing the hub, I found small holes rusted through the outer tub. These I repaired with JB WaterWeld quite successfully. The new parts were well made and went on easily in about 45 minutes.
Parts Used:
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Jeff from Garland, TX
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Difficulty Level:A Bit Difficult
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Total Repair Time:More than 2 hours
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Tools:Pliers, Screw drivers, Socket set, Wrench (Adjustable)
6 of 9 people
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Leaky drain hose
First I tried to lift the lid on the top of the washing machine. I eventually realized this model doesn't open up from the top. I removed two screws on the very bottom of the front panel of the washing machine. Then pulled gently downward to release the front panel from the two clips holding it in at the top. Once the front panle was removed, I found I could easily access the drain hose and disconnect it from the pump by loosening the clamp screw. (Be aware, there is still water in the hose and pump that will run out onto the floor; I had a bucket close by and tried to catch most of this water, but its somewhat futile.) There are two additional hose clips one underneath the tub, and one on the back panel of the washer that hold the hose away from other mechanical parts. Once the hose is freed from those clips it could be removed from the washer by feeding the hose out the back panel. The new hose was then inserted and fed down inside the washer, attached to the pump, tighten the hose clamp screw, clip the hose to the other two clamps so it is out of the way of other parts, reattached the front panel and you're done!
One other note about PartSelect.com...A few days after ordering my part, I had an "International Transaction Fee" show up on my debit card statement. I panicked thinking my card number had been stolen only to call my bank and find out PartSelect is based in Canada.
One other note about PartSelect.com...A few days after ordering my part, I had an "International Transaction Fee" show up on my debit card statement. I panicked thinking my card number had been stolen only to call my bank and find out PartSelect is based in Canada.
Parts Used:
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Keith from Little Elm, TX
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers
4 of 5 people
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Drain Hose had a crack and leaked
Removed front panel; loosened hose clamp at pump; removed existing drain hose. Easy part.
Installed new hose at pump and tightened hose clamp. Somewhat difficult.
1. Your hose design should be solid flexible rubber hose instead of corrugated type. Had rough time snaking hose to the pump.
2. Your future designs should have rubber hose or hard piping to the exit hole on the back panel and terminated in a male fitting, then connect flexible hose from fitting to drain line. Similar to "hot & cold " water connections.
3. For future customers- care should be taken installing the "black" portion ; it kinked on me 2 or 3 times because you have to keep rotating the entire hose to keep the "black" portion straight.
Installed new hose at pump and tightened hose clamp. Somewhat difficult.
1. Your hose design should be solid flexible rubber hose instead of corrugated type. Had rough time snaking hose to the pump.
2. Your future designs should have rubber hose or hard piping to the exit hole on the back panel and terminated in a male fitting, then connect flexible hose from fitting to drain line. Similar to "hot & cold " water connections.
3. For future customers- care should be taken installing the "black" portion ; it kinked on me 2 or 3 times because you have to keep rotating the entire hose to keep the "black" portion straight.
Parts Used:
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Bernard from Pinellas Park, FL
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Difficulty Level:A Bit Difficult
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Total Repair Time:15 - 30 mins
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Tools:Screw drivers, Wrench set
4 of 6 people
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none
took the drive belt to the pump off then put the belt for the drum on .then put the belt for pump back on. basickly this unit is one of the easist to work on
Parts Used:
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C from Palatine, IL
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
3 of 4 people
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Drain hose sprung a leak
simple as removing front panel from washer held on by two screws and the hose was right their. Took a few minutes to disconnect it from the pump and pull it out through the rear, then feed the replacement in and reverse the process. Piece of cake. Thank you.
Parts Used:
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Burton from Sutton, MA
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Difficulty Level:Really Easy
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Total Repair Time:30 - 60 mins
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Tools:Pliers, Screw drivers
3 of 4 people
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