DE712 Maytag Dryer - Instructions
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old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
Parts Used:
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William from ORANGEBURG, SC
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Difficulty Level:A Bit Difficult
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Total Repair Time:30 - 60 mins
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Tools:Screw drivers, Socket set
4 of 4 people
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Dryer tumbler belt broke.
I followed the videos on your website, but had to clean 30 years of dust and lint out in the process. Cleaning took the longest time.
Parts Used:
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Robert from Fort Worth, TX
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers
6 of 10 people
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very noisy, not working properly
Took it apart according to the videos, replaced about all moving parts (almost). Put it back together and still made noise. It turned out to be the blower wheel. Ordered a new blower wheel and installed it. Works great and has mostly all new parts. The website was great!!
Parts Used:
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Fred from Columbia Falls, MT
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set
4 of 4 people
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Blower fan came loose and broke
No manual on this so had to remove about 12 screws to figger out disassembly,after locating the right ones[front]the job was easy.Remove front plate,remove drum bearing,remove blower front cover,remove snap ring,remove broken fan,clean fan shaft,slide new fan onto shaft[there is a flat in the bore of new fan]instal fan retainer on stub of fan,reinstal snap ring,reinstal the rest of the parts,test drive system[all sat]The part was exactly as ordered,thanks,Jim Thompson
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jim from sierra vista, AZ
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
4 of 4 people
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replaced the lint filter
No big deal about replacing a lint filter , take the old one out and put the new one in.
Parts Used:
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michael from farmington, NH
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Difficulty Level:Really Easy
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Total Repair Time:Less than 15 mins
4 of 4 people
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The timer stopped, but a repair man suggested it was the heating element
I removed the old element and replaced it. There were only two screw to deal with once I had the front panel off of the dryer. The electrical hookups were easy and the part I got fit exactly like the old part. I had to work at it a bit to get the back end to fit into the exhaust hose, but once that was taken care of this was one of the easiest appliance repairs ever. I agree with the repair man that first told me to fix it, these old machines are worth a few dollars to keep running. They work great!
Parts Used:
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John from Cleveland, OH
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Difficulty Level:Really Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers
4 of 4 people
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Dryer worked but did not heat.
Using a "Fix it Yourself book" and following a simple test method (measuring ohms) to determine if heating element or if it could be a heat sensor or something else was bad. Going slow the heating element was ID'd to be the problem in about one hour. Searched on line and found your site, ordered the part and in 1 day had the part. It took about an hour to install. Wife is very happy. Overall an easy task. Thanks much.
Parts Used:
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Joe from Burlington, CT
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
4 of 5 people
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Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
Parts Used:
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Francis from Half Moon Bay, CA
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Difficulty Level:Easy
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Total Repair Time:1- 2 hours
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Tools:Screw drivers, Socket set
5 of 8 people
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No Heat
Insure the double pole breaker in the breaker box is functioning properly.
Parts Used:
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Mark from Napa, CA
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Difficulty Level:Very Difficult
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Screw drivers
5 of 8 people
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Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
Parts Used:
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William from Winter Park, FL
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Pliers, Screw drivers
4 of 5 people
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Dryer will not heat
The 2 screws that hold the front cover to the dryer was hard to see because they are facing down.
After the 2 front screws were removed from the dryer, the heater was easily accessed. All I had to do was to remove the old heater assembly and transfer the limit sensor and wire on the assembly. The hardest part to the repair was fitting the rear end of the heater assembly to the back duct. I just bent the edges to conform to the rear duct where they mate together. Once I got the heater to line up, the rest was easy. Remember to use a shop vac to clean up the inside of the dryer since you have it all opened up. You'll be amazed at what you will find!
My dryer was up and running in no time and my wife was happy and so was I that we didn't have to buy a new dryer!!!
After the 2 front screws were removed from the dryer, the heater was easily accessed. All I had to do was to remove the old heater assembly and transfer the limit sensor and wire on the assembly. The hardest part to the repair was fitting the rear end of the heater assembly to the back duct. I just bent the edges to conform to the rear duct where they mate together. Once I got the heater to line up, the rest was easy. Remember to use a shop vac to clean up the inside of the dryer since you have it all opened up. You'll be amazed at what you will find!
My dryer was up and running in no time and my wife was happy and so was I that we didn't have to buy a new dryer!!!
Parts Used:
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Christopher from Lake Worth, FL
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Difficulty Level:Easy
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Total Repair Time:15 - 30 mins
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Tools:Nutdriver, Screw drivers, Wrench set
4 of 5 people
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Very noisy.
My first attemp was to replace the drum roller and idler roller, drive belt, and the felt seal for the back, since I had experience replacing these on an older machine many years ago. The dryer was very easy to work on....After installing the new parts, I reassembled and discovered it still made the same loud noise. I then, disassembled for the second time to discover the blower wheel was worn out; so i ordered another blower wheel and a drum support roller (i only ordered one the first time.). After reassembling it made an annoying high pitch sound. I attributed that to the new parts...probably the new belt and new felt seal. Gave it some time to run-in and it seems to have quieted down. Overall, i found the dryer very easy to work on. I actually found the felt seal the most onerous to install....needed to have about three hands to get the drum back in place! I just wish that the stamped metal dryer housing didn't have such sharp edges. I had to be very careful to avoid sharp burrs but still got nicked a couple of times.
Parts Used:
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Benjamin from Baton Rouge, LA
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Difficulty Level:Really Easy
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Total Repair Time:More than 2 hours
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Tools:Nutdriver, Pliers, Screw drivers, Socket set
4 of 6 people
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Broken Tumbler & Motor Belt
Disassembled per instructions. Additional time used to clean inside unit.. Its much easier to install belt on motor pulley and tension pulley ( Roller) from rear access panel. Also ensures proper belt alignment on all items.
Parts Used:
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John from ELBRIDGE, NY
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Difficulty Level:Really Easy
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Total Repair Time:1- 2 hours
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Tools:Nutdriver, Screw drivers
3 of 3 people
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Drum would not turn, drive motor humming loudly and unable to turn drum/blower wheel
The repair video is terrific and many others here have thoroughly described the steps involved to replace the drive motor.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
The biggest hurdle for me was that the motor came with a new switch that required a different wiring configuration. No wiring diagram was included. Several others had posted questions about wiring in the Q&A and unfortunately PartSelect kept copy/pasting the same confusing and incomplete answer over and over:
"The Yellow goes to T6, Red to T5 Black to T2, blue to T1 and the white you will remove the blue jumper lead between the switch terminal 4 and 1/4" protector tab, connect the grey harness lead to the 1/4" protector tab."
Reading that doesn't tell me what to do with the white wire, doesn't address that my blue and white wires were crimped into the same connector from the factory, doesn't address that I had 2 black wires crimped into the same connector from the factory, and doesn't address a factory ground wire that connected the frame of the OEM motor to the bracket that the motor sits in.
With all the other excellent info supplied by PartSelect, this was surprising and frustrating. The sales dept ignored an emailed question from me, and the Q&A section didn't allow me to post a question.
Searching the internet, I found a wiring diagram on aceappliancesd dot com that addressed my dryer's OEM wiring configuration. Here's what I ended up with:
TI - Blue and white, crimped together into a single connector
T2 - Black & black, crimped together into a single connector (the wiring diagram I found said this should be black & brown, but they both look black to me)
T5 - Red
T6 - Yellow
1/4" Thermal protector tab - Grey (from the harness)
The new motor switch had a grounding tab with nothing connected to it. I removed the screw holding that tab into the switch and connected the (also grey) OEM short ground wire from the motor frame to the mounting bracket.
I had to cut 2 of the pieces of tape holding the OEM wiring harness together in order to get enough slack for all the connections to reach. If you do this too, make sure all the wires are still clear of the moving parts and the hot bits. You may need to retape the wires together at a different location to keep things tidy.
I also laid the belt over the drum and put 2 pieces of tape over it to hold it in place while I got the drum positioned, then I reached through the back access panel to loop the belt around the motor pulley and idler. Once that's done, just reach over the top of the drum and peel the tape off. I found that much easier than trying to loop the belt by reaching through and past the drum.
Parts Used:
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Peter from REDONDO BEACH, CA
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers, Socket set
3 of 3 people
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Much noise when drying clothes.
Installation of drum support kit was difficult because my snap ring pliers would not fit in the snap ring holes. Had to use pliers and screw driver to get them off and to put them back on. That took much patience and time. Installation of front guides was a bit difficult because the rivets were loose and turned when trying to drill them out. Also they were bigger and I needed a larger drill bit than the 1/8 told about in the video. Used drill, screw driver and pliers to get the rivets out. Also took more time and patience to do this. Belt did not need replacement but felt it a good idea to do it as long as I was in there. Belt installation was easy because my dryer has a rear view opening and I could use it to thread the belt. Tried it from the front as shown in the video just to see if I could and found it impossible. Could not even get my hands to hold the belt. Also vacuumed out 20 years of lint and dust that was inside the dryer. The videos were excellent in showing what to do and how to do it. Not sure how well I would have done without them.
Parts Used:
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Roger from RALEIGH, NC
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Difficulty Level:A Bit Difficult
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Total Repair Time:1- 2 hours
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Tools:Pliers, Screw drivers, Socket set
5 of 9 people
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