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SE1000 Maytag - Instructions

All Instructions for the SE1000
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The pump starting leaking around the center portion.
The hardest part was figuring out how to get the front panel off of the washer. Once that was done, the pump came off easy.... 3 screws attached it to the bottom panel and 2 hose had to be disconnected. Putting the new one in was easy.
Parts Used:
Drain Pump
  • Kenny from Covington, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
11 of 14 people found this instruction helpful.
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The drive belt broke.
1st We pulled the washing machine from the wall and unplugged it. 2nd We tilted the maching back against the wall so that we could see all the pullies. 3rd. We removed the two screws that afix the front panel on the lower part of the washing machine and removed the panel. 4th We removed both belts and put new belts on. 5th We put all parts back in place and plugged maching back in, slide it back in place. 6th It worked like a charm and I proceeded to wash 3 loads of laundry that evening. The only tool we needed was the phillips head screw drive to take off the front panel. It took us 5 minutes to fix the machine.
Parts Used:
Belt Kit
  • Debbie from Georgetown, SC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
11 of 14 people found this instruction helpful.
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Washer rocking to left and vibrating
Wish there was a video. I am above average handy but this one- I might just pay someone next time...The tape on the threads was a great tip but took a while to understand what they meant by putting tape on the threads. Scraping off the old pads is easy for the front one but the back pad and a half is so hard to reach to really get it cleaned. Bruised and cut knuckles on that one. Then not having the glue for the pads was a surprise and you have to get a good contact type cement that sets in 10-15 minutes or you will be waiting hours to put it back together. It was easy to put the first spring on, then the second and third got harder and harder.
Parts Used:
Damper Pad Kit
  • John from Chesapeake, VA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
10 of 11 people found this instruction helpful.
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Leaking near one of the seal clamps
Thoroughly cleaned the edges to be sealed with a wire brush and sand paper. shimmed the top piece with 1/4 inch plywood strips. seated the top piece with the seal attached and worked the seal down into place. Positioned the seal clamp, carefully, and tightened the clamp screws. Replacing the seal did the trick, even though the old seal did not look to be in bad shape.
Parts Used:
Outer Tub Clamp Seal
  • JIM from PINE RIVER, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
11 of 15 people found this instruction helpful.
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Leaking from under tub
removed screws on front of washer, removed bolts holding top cover hinged back, nut driver to remove agitator, slipped agitator off, removed tub hoses, did not have special wrench to remove large nut on shaft, used punch and grinder to removed, had new large nut so wasn't concerned about damaging old one, pay attention to thread pattern to know how to turn, if you had special wrench job would be easier, removed spring bolts and took out inside drum and tub. cleaned corrosion and installed new seals, can be hard to slip on new seal, don't use grease, get dishwashing soap to use as lubricant to put on. Put back together and all is good.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Reece from Joplin, MO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
9 of 9 people found this instruction helpful.
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
12 of 18 people found this instruction helpful.
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Smoking Washing Machine.
Well, I figured out a couple of things during this process. #1 The Washer was smoking. It had happened before (a sock got suck between the basket and the tub) so I assumed that happened again. I couldn't see anything in that space this time, so I dissasbemled the washer to see if any clothing was there. Relatively easy once finding the screws to remove the front panel. #2 What I found was a sock in the pump box. I disconnected the hoses and removed it, saw nothing between the basket and tub and ran it to see if problem corrected itself. It still was smoking. That is when I checked the belts, #3 first the pump belt, replaced it, very easy, just pulled the old one off, and wheeled the new one on. It still was smoking, #4 so I replaced the drive belt, very easy and the same as the pump belt. It still was smoking so I lubed the wheels for the belts, and #5 cleaned the residual rubber around the wheel from the old, fried, dry rotted drive belt. No more smoke!!! However #6 remember to leave space between the basket and the top of the tub, as when I put the washer back together the basket didn't spin. I removed the top and ran the spin cycle, it spun fine, reconnected and it didn't spin, the tub top was touching the basket, that's when I relized the top was on too tight. I reattached and left about 1/4 in of space and all is well now.
Parts Used:
Belt Kit
  • Matthew from Wilmington, DE
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
10 of 12 people found this instruction helpful.
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Standing water in washer tub
Thinking the water pump was not doing its job in removing all of the water after the rinse cycle, I replaced the water pump.

1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.

This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.

Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
Parts Used:
Drain Pump
  • James from Baton Rouge, LA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
9 of 10 people found this instruction helpful.
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no water drain
removed old pully, put new one on with hex driver, removed belts, put new belts on and finished.
Parts Used:
Belt Kit Belt Kit Motor Pulley
  • Franz from Lakeland, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
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I broke the elbow when I pulled the washer too far from the wall for another repair.
I removed 2 screws holding the front of the cabinet and set the front panel aside. Next I removed the screw securing the relay and water level switch to the front of the cabinet, and removed 4 screws holding the top of the washer to the cabinet. I removed the hose, then removed the 4 screws securing the siphon break to the rear panel and pulled it inside the cabinet. I removed the elbow and gasket, installed the new elbow and gasket, and reassembled all parts previously removed. I reconnected the hose and fastened it to the drain, and I was back in business. It took about 35 minutes.
Parts Used:
Corrugated Drain Hose Syphon Break Gasket Syphon Break Elbow Kit with Clamp
  • George from Smithfield, KY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Washer did not drain.
Took front panel off. Ran machine. Pump is see-through. Could not see any "aeration" of the water in the pump and no water was coming out of drain hose. Disconnected electric. Disconnected hose from drum to pump(first emptied ALL water from drom)and drained in bucket. Disconnected drain hose from pump to drain and drained any water. Checked for obstructions in hoses. Removed pump. Checked belt (was fine after 14 years). Ordered new pump. Received the next day! Replaced pump and tighten belt. Connected hoses and test it. All OK. Replace panel and did laundry.
Parts Used:
Drain Pump
  • Basil from St. Charles, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Socket set
9 of 10 people found this instruction helpful.
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Dryer would not heat.
First I removed the front panel on the dryer. While the dyer was running, I noticed the igniter did not turn its normal amber color and ignite the gas supply. I then disconnected the wire to the igniter and removed the screw holding the igniter in place. Next I replaced the igniter, tightened the screw and reconnected the wire. Finally, I replaced the front panel. This is a relatively simple repair.
Parts Used:
Flat Style Igniter
  • William from Batavia, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
9 of 10 people found this instruction helpful.
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Noise in dryer
How to disassemble the dryer has been covered in past repair stories. I will add a make shift repair that will get you up and running until you get your replacement blower wheel. We repair gas dryers for a living and this repair works and some machines are still running for two years. Remove the blower wheel. Cut a piece of plumber strap of similar sized metal to about 3/16" x 1/2". Hold it with vise grips and then heat it with a torch. When it is hot melt it into the hole in the blower wheel. This will give you a flat spot in the shaft hole that will keep the blower from spinning on the motor shaft. Some trial and error fitting is involved. If you do it carefully the blower wheel will fit very nicely and will not vibrate or make noise.
Parts Used:
Blower Wheel with Clamp
  • Joseph from Hampton bays, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
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tub leaked
followed instructions elsewhere here. Procedure went flawlessly
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.

STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Fritz from Redway, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable), Wrench set
8 of 8 people found this instruction helpful.
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All Instructions for the SE1000
121 - 135 of 1475