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LE6685XPW0 Whirlpool Dryer - Instructions

All Instructions for the LE6685XPW0
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dryer would stall and the motor would hum before tripping circuit breaker
When the problem first came up, I took the dryer apart without first looking up any instructions. This wasn't difficult, but didn't realize when removing the fan from the motor, there is a square lug as part of the fan hidden by the rear clamp securing the motor. I was able to remove the fan by holding the motor shaft with a crescent wrench and removing the fan by hand, but was difficult and gloves were necessary in case the fan loosened quickly and my hand came in contact with the sheet metal (very sharp).

I took the motor out and attempted to clean it as it was loaded with dust as was the dryer internals. I tried to lube the motor bearings and appeared to free up, but the sight of metal shavings on the rear bearing seal had me concerned. This ultimely did not work and was trying to buy some time until the new motor arrived.

This is when I looked up the motor part number and found that Parts Select had the part number in stock. I ordered the motor on a Saturday afternoon and got a quick response acknowledging my order. The motor shipped that following Monday from Fresno and arrived on my Southern California doorstep Tuesday. These guys have their act together and are helpful in making the repairs. In my case I did not have to make any adjustments to the wiring or the pulley for my model and replaced the motor the following weekend in about 45 minutes. Since I had the unit apart several times before replacing the motor, the installation went quickly.

The dryer is again working fine for a unit 12 years old and my wife is once again happy that we didn't have to purchase a new dryer.
Parts Used:
Drive Motor with Pulley
  • Charles from Placentia, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
11 of 12 people found this instruction helpful.
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Motor failure
Used this resource and others' advice -thank you . Make sure to disconnect power first. I had replaced the rollers and tensioner a week earlier due to squeaking, but mine was the rare one where squeaking meant motor failure, so I had to place another parts order. The dryer was 19 years old, and my blower wheel did not simply 'unscrew with reverse threads'. During removal the blower wheel's plastic deformed, so had to do like someone else did and cut the rear shaft with a reciprocating saw. Just be careful not to damage the bulkhead's built-in bracket that anchors the rear of the motor. I think it was a 13/16" wrench that fit the blower wheel and I forget the size for the pulley nut on the front of the motor, but I suggest a deep socket since it held well. My best advice when dealing with a motor replacement is to ensure the blower wheel wheel will separate successfully from the motor before placing your parts order should it be a stubborn removal. Good luck.
Parts Used:
Dryer Blower wheel SEAL Lint Trap Housing Seal Blower Motor Shaft Seal Front Top Lock Drive Motor with Pulley
  • James from COTTONWOOD, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Socket set, Wrench set
11 of 12 people found this instruction helpful.
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One of the drum support rollers was worn out
I lifted the top of the dryer and removed the front panel. I removed the drum exposing the drum rollers. I replaced the rollers and reassembled the dryer. The exploded views on the web site made it easy to see what to do.
Parts Used:
Roller Support Tri-Ring Rear Drum Support Roller Kit
  • David from Fleetwood, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
13 of 19 people found this instruction helpful.
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Badly worn idler pulley and rollers.
Braced dryer drum with a block. Removed the two rollers one at a time by using a screwdriver to pop off the triangular clip. Slid on new rollers. Would have been easier to remove the drum out the front instead of bracing it. Installed new idler pulley and belt. Dryer is 25 years old and sounds like a new one now when running.
Parts Used:
Idler Pulley Assembly Rear Drum Support Roller Kit Multi Rib Belt - 92-1/4"
  • TODD from GRASS VALLEY, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
11 of 14 people found this instruction helpful.
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broken clip on top panel hold down
pressed clip into hole on top of front panel. first remove two philip screws that hold filter so you can lift top up.
Parts Used:
Front Top Lock
  • Mark from Huntington Station, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
15 of 26 people found this instruction helpful.
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Dryer only worked on one of three cycles
I started out by looking up information on the Internet to test the various dryer components (thermal switches, heating coil and timer) with a multi-tester. Everything checked out OK except for the timer. I knew it was bad anyway since only one of three cycles worked. It's good to check everything out while you have the back panel removed just in case other parts need to be replaced. Replacing the timer was very easy. Just remove one wire at a time and connect it to the new timer before moving on to the next wire. The new resistor, which came with the timer, was a different type, but was still easy to figure out how to connect with the provided instructions.

The hardest and most time-consuming part of the job was cleaning out all of the lint inside the dryer airways and all through the exhuast line - which vents through the roof of my house. I removed the lint filter airway from the dryer and found a lot of lint (one pound, maybe) caked up at the bottom, right next to the fan blade which pulls air through the dryer. After doing all of this, the dryer now dries like a new one on all cycles - even the automatic ones. Cleaning out the lint is crucial to helping the dryer not work harder than it has to, which saves you money on electricity (or gas)!

I bought my multi-tester at Radio Shack years ago. It has saved me hundreds of dollars by pinpointing the exact component which is causing the problem. Otherwise, you may buy parts you don't need that don't fix the problem. So, for about $104, my wife has a 22 year old dryer which performs like new and she is very happy about that. That's a lot cheaper than paying upwards of $400 for a new dryer - which we don't need yet.
Parts Used:
Dryer Timer
  • Jim from Plano, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
10 of 12 people found this instruction helpful.
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my teenage son was messing around and got into the dryer and broke the door catch and bent the door.
removed the catch and the pin and replaced it. We were sent a couple different sizes so we tested the one that looked like the closest match. I think the pin was made with different thicknesses of metal. Worked great and saved us from having to get a new dryer!
Parts Used:
Door Catch Kit
  • Dawn from Chesapeake City, MD
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
13 of 21 people found this instruction helpful.
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Lint Filter screen torn and rusted
Pulled to old out inserted the new. I would like to say your turn around from date part was ordered until I recieved it was three days, I find that amazing. I'm still waiting for a part I ordered from another company 1 month ago. The price was right shipping cost was very reasonable and your web site extremly easy to use. Thanks very much, Al
Parts Used:
Lint Filter
  • Albert from Burlington, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
9 of 9 people found this instruction helpful.
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Old motor was making noise and tripping after a few minutes
I disassembled the dryer once to clean the motor and compartment. After reasembly, the problem persistes. I ordered the motor and the second diasasssembly was accomplished in 10 minutes and the entire job took 45 minutes and the dryer was running like new. Tip- Leave the motor secured while removing the blower fan.
Parts Used:
Drive Motor with Pulley
  • John from Midland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
10 of 13 people found this instruction helpful.
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Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
Parts Used:
Multi Rib Belt - 92-1/4"
  • Ronald from Oakdale, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
10 of 13 people found this instruction helpful.
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Washer stopped working mid cycle restarts after resetting lid
Repair went well, but my switch only had one contact on the non common end. The new switch had two contacts. One is for operation with lid open and one for lid closed. Make sure to connect to the lid closed contact and the common on the other end and leave the lid open contact unused.
Parts Used:
Lid Switch
  • Eric from West Chester, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
11 of 16 people found this instruction helpful.
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Heating Element went bad
Took the back cover off and WA-LA, a bad element. Went online to PartSelect.Com and ordered the part and my Mom was drying clothes again in lees than a week. Now, I am her favorite son again.
Parts Used:
Heating Element
  • Michael from Brownstown, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
10 of 14 people found this instruction helpful.
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Broken dryer belt
Prop up the hood of the dryer with flat bar. Take out 2 screws holding dryer front end and 2 switch screws for dryer light inside dryer door. Secure dryer drum with bungee cord. Lift front end and remove. Remove broken belt. Route new belt over drum and pass underneatch idler pulley at botttom of dryer. Apply pressure to idler pulley w/one hand while securing belt around motor with the other. Make sure drum seals are snug between front and back of dryer while putting everything back together.
Have confidence. This is a very easy fix.
Parts Used:
Idler Pulley Assembly Multi Rib Belt - 92-1/4"
  • Steven from Bridgewater, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Dryer had quit turning
I first disconnected the power cord and the vent hose. I removed the screws on the top of the back side to raise the top of the unit. There are also 2 screws holding the lint filter shoot which were also removed to allow the top to be lifted up. Its not necessary to remove the top since this would require disconnecting the wiring harness etc.

Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.

With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.

I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.

I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.

I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.

After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.

Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.

To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.

I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.
Parts Used:
Multi Rib Belt - 92-1/4" Rear Drum Seal Kit
  • Martin from Lynchburg, VA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
8 of 8 people found this instruction helpful.
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Loud rumble noise while drum was turning
First I pulled out lint catcher, you will see two screws ,removed two the screws on top ,( philips head screw driver) I than took a putty knife and pushed in the front of the dryer under the lid and lifted the top up, I than removed a self tapping screw on each side with a 5/16 wrench and lifted the front panel out. I than pulled out the drum and this exposed the two rollers, I than pulled of the nut locks with athe pliers , took off the plastic triangle snaps and pullled off the old rollers , replaceing them with the new ones,put the triangle locks on and that the lock nuts on , I than put the drum back in, than the front panel, replaceing the two self tapping screws , snapped down the top,replaced the other two screws again on top and replaced the lint catcher, I was done.
Parts Used:
Rear Drum Support Roller Kit
  • Marcia from CAmden, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Wrench set
9 of 11 people found this instruction helpful.
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All Instructions for the LE6685XPW0
61 - 75 of 1281