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DG250EXD5 Frigidaire Dryer - Instructions

All Instructions for the DG250EXD5
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Drum making noise when running ( rear bearing )
Took a putty knife and released top clips. Tipped top back , and took out 4 screws holding front cover in place. Lifted out drum, replaced bearing plate. Removed 2 screws and replaced back panel bearing. Placed drum back in place, installed front panel, snapped top back in place and job was done. Very easy. Took about one hour.
Parts Used:
Rear Drum Bearing Kit
  • Ralph from Wisconsin Rapids, WI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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The clothes were not getting dry, no matter how long they ran
The first thing I did was logged onto the internet to search the web for my dryer information. Next, after I found the correct model, the site referred me to the parts section and that is where I determined the problem was the M series ignition coil. I then unplugged the dryer and turned off the gas. I took a screwdriver and popped the top off and cut the wire straps that held the door strips and the light to the front panel. I then unplugged the door switch at the connector - HOWEVER - DO NOT TRY TO REMOVE THE WIRES FROM THE ACTUAL DOOR SWITCH BECAUSE THEY ARE VERY FRAGILE AND CAN EASILY BREAK. Next, I removed the two screws that hold the front panel on. By using a slight bit of pressure, I removed the front panel and was able to locate where the ignition coil switch was. (It was right in front) I then removed the two screws that held the clamp down, as well as the bad coils. The coils easily slid off the post and the new pieces slid back on just as easy. I then replaced the screws and clamps to hold the new pieces in place and replaced the front panel. **NOTE ~ while the front panel is off, it would be a good time to clean out all the built up dirt and lint that has accumulated over the years. Lastly, I re-connected all switches and wires and replaced the top panel. Once I turned the gas back on, everything ran beautifully.
Parts Used:
M Series Ignition Coil Kit
  • Bruce from madison, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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no heat
I lifted the top at the front edge, slid the top back, disconnected the ground wire connected to the top at the rear edge, just slides off.
Then removed the phillips screws on the inside front edge, only one on each side,near top of dryer disconnect the wiring harness at the right side, cut the nylon tie strap holding harness also.
Tip front panel out a little and lift up, comes right off.
The coils are in plain site on the gas valve, remove the wires, and the two screws holding the bracket that holdes them in place, slide the old ones off and start putting back together.
I also used a vacume and cleaned all the lint and dust off everything I could, including the air intake at the rear of machine, "Peice of Cake"
Parts Used:
M Series Ignition Coil Kit
  • James from Alpena, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Extremely noisy, grinding, old electric dryer.
Removed small panel at rear of dryer which allowed access to the Idler Pulley asembly. Easily removed, and replaced with new idler assembly. Fed belt onto new pulley and attached tension spring. Actually, this replacement idler pulley assembly is much better than the original. It has a shoulder to allow the belt to "track" better over drum and around motor pulley. Dryer is now extremely quiet, like a new machine. Hope to get another 29 (yes 29) years out of it. Extremely pleased. Doug East Lansing, Michigan
Parts Used:
Idler Pulley Assembly
  • DOUGLAS from EAST LANSING, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers
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New Belt slipped off pulley - drum won't rotate
Removed access door. Disengaged spring, removed old idler. Slipped belt around new idler and motor pulley. Difficulty is putting spring back and inserting idler pulley bracket back in place while there is a lot of tension from the belt. Finally used adjustable wrench as a mini hammer.
Parts Used:
Idler Pulley Assembly
  • Lawrence K from Harrisonburg, VA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
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Dryer drum stopped spinning
First I took the drum out of the dryer. This was an easy tear down. I had to remember 2 wires, and a belt assembly ( 2 pullies ). I removed 3 screws inside the drum to release the bearing assembly from the back. Then I went to the dryer chasis and removed the mounting bracket by removing 2 screws. I simply replaced the mounting bracket with the new one. This required having to use a magnet to hold a small ball bearing in place while I worked the rest of the pieces in position.I greased it up and went back to the drum. I replaced the old bearing assembly with the new one. Easy. I took the time to shop-vac the inside of the dryer. There was a lot of loose lint, candy rappers, coins, etc. Finally, I put it back together. Unfortunately, this is the forth (4th) time I've had to do this. It's cheaper than buying a new dryer. Now, I've got to fix the washer.
Parts Used:
Rear Drum Bearing Kit
  • Ron from Senatobia, MS
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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broken belt and pulley
First of all, I've purchased a belt from local service center that cost me more than $21 (local tax is 8.5%). But, I can not find the idel pulley assembly so I searched on the Internet and ordered from PartSelect.com.

Surprisedly, my order came just one day - they must cross-ship from local distribution that it's even faster than to get those in local stores (driving .. and hope they have what I want ..).

I've replaced the belt 2 days ago - it's easy with 4 screws removed to pull out the front door. The back panel is opened with 2 screws remove, and very easy to replace the pulley.

It's a heavy duty gas dryer made in 1989 and this is the third time I changed the belt and the first time to change a new pulley. I would recommend to change the idle pulley because I may not need to change the belt if I have had replaced it last time. A broken or not functional idle pulley may damage the belt in a short time.

Appliance such as gas dryer like mine will last forever with replaceable belt and pulley. I'm really happy to see a working dryer (almost 20 years old) and my wife is asking a small component for her washer .. that I think I can easily fix that too .. with the help of PartSelect search.

Hope this will help.

John
Parts Used:
Flat Style Belt Idler Pulley Assembly
  • John from Temple City, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Pliers, Socket set, Wrench (Adjustable)
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Drum stoppped spinning, motor didn't.
Opened the top, removed the 4 screws that held the front top the cabinet, took the front off, went after the dust with the vacuum cleaner, lifted the drum, installed the belt, put the front back on, and put the belt over the idler. Most of the time was in the cleaning.
Parts Used:
Flat Style Belt
  • Allen from Cardington, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver
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squeaking dryer driving insane
First removed the top of the dryer, then the front of the dryer. Took the plate off the back left of the dryer to disengage the belt off the pulley.
Took the three screws out that hold the drum in place, of course the third screw stripped and had to use a screw remover, which didn't work, but the adjustable pliers did so then lifted the drum out of the plastic reservoir in which the bearing laid. Next unscrewed the two bolts holding the plastic reservoir which also loosened the small metal piece on the back of the dryer where a small bearing is located. Put the new parts in, but instead of putting the larger bearing that fits in the plastic reservoir, I decided to put it on the drum first and guide it into the reservoir all at once, this worked well . Prior to that I put the new plastic piece on the inside and taped it there while holding that piece put the small metal piece with the small bearing on the back of the dryer. I'm sure it is alot easier with two people doing this part, but it worked and I didn't lose the small bearing. Next put the front of the dryer back on and then put the belt back on the pulley, then the top.
It definitely helped immensely to read how someone did this, just follow the instructions given and there you go, no more annoying squeak and also a feeling of accomplishment and thanks to the person who wrote the story on how to do this job, appreciate it.
Parts Used:
Rear Drum Bearing Kit
  • greg from great cacapon, WV
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers
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Loud squealing
As all others have said, without being redundant, I'd view post #1 or #2 for a good detailed set of instructions.

The primary issue I had was with the stainless steel ball bearing that was shipped with the kit. I couldn't figure out what it was used for, because when I removed the bearing carrier the ball fell out before I could see where the original one was located. The stainless ball bearing is a grounding ball, not a bearing. It goes on the exterior of the plastic bearing carrier/receiver.

Once I figured that part out, it was a piece of cake.

Took a little longer than other people's repairs, but I also put a new belt on and re-worked the exhaust duct for solid ducting versus flexible duct. fine-tuning the rigid duct work was a piece of cake with the tumbler out, since i could crawl right inside the chassis and make sure everything would line up (level legs, adjust elbows, etc)
Parts Used:
Rear Drum Bearing Kit
  • John from Avis, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Rear Bearing wearing out
I first looked at your directions then felt I could do the repair. So I ordered the part. The video was extremely helpful and allowed me to follow each step in the process. Last time I paid $270 for the exact repair. This time I costs me under $30. Plus I was able to clean out the entire inside of the dryer. The sitr instructions were very helpful and on target for any level of experience. I fixed my own dryer and saved a ton on it! Thank You, Randy In Colorado
Parts Used:
Rear Drum Bearing Kit
  • Randy from CENTENNIAL, CO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Door latch receiver broke
Super simple pushed in the new receiver and boom all good and working
Parts Used:
Door Latch Kit
  • sandra from PLYMOUTH, MN
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers
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Drum was not revolving
Open the back plate. Broken pulley was already out of place. Put the spring on the pulley and placed it. It took me less than 10 min
Parts Used:
Idler Pulley Assembly
  • khalid from HILLSBOROUGH, NJ
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
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Dryer does not start
Followed video instructions, easy installation. Unfortunately it didn't fix the problem. Plan to take back off and check belt, etc before ordering another part.
Parts Used:
Door Latch Kit
  • Anna from FLORENCE, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
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Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
Parts Used:
Rear Drum Bearing Kit Rear Drum Bearing Kit Drum Support Bearing Rear Drum Bearing Kit
  • Doug from ODESSA, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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All Instructions for the DG250EXD5
61 - 75 of 225