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DE400ADW2 Frigidaire Dryer - Instructions

All Instructions for the DE400ADW2
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Had a squelch/squeak coming from the rear of the unit
I looked up a YouTube video on my specific model. Found one that said “basic disassembly”. I watched that and had it apart and back together in no time. Very easy to take apart and put new parts back in it. Re-assembled and since the repair no squeaking.
Parts Used:
Drum Belt Rear Drum Bearing Kit Drum Support Bearing
  • Stephen from HICKSVILLE, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Drum was not revolving
Open the back plate. Broken pulley was already out of place. Put the spring on the pulley and placed it. It took me less than 10 min
Parts Used:
Idler Pulley Assembly
  • khalid from HILLSBOROUGH, NJ
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
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Squeaky drum until drum would not turn.
Watched on-line video, then applied those steps.
1. Pop the front of the deck loose using putty knife to depress clips;
2. Disconnect wires from light and door switch;
(Before I disconnected wires from door switch and light, I made wiring sketches to make sure I reconnected in original manner.)
3. Remove lint filter mount screws and mount from bottom of door opening;
4. Cut drum belt with wire-cutters and removed it;
5. Remove drum support clip from top center of front panel;
6. Remove (1) screw from each side of dryer body that hold front to sidewalls, removed front panel;
7. Remove drum by lifting the rear out of the bearing, then moving it forward through the machine front;
[While I had the dryer disassembled, I thoroughly cleaned it of lint, dirt & metal filings. The metal filings were from the worn ball hitch and drum support bearing cup. I spent as much time cleaning it out as I did working on it.]
8. Stand drum on gallon paint bucket while removing ball hitch (Use a #2 drywall phillips apex to obtain sufficient seating & torque to remove and reinstall ball hitch screws at rear of drum.);
9. Have a second person hold the new ball hitch in position while starting screws, if necessary;
10. Use nut driver w/5/16" socket to remove bearing retainer & ground ball clip;
11. Install new bearing into retainer clip, insert attachment screws through the holes in both, stick grounding ball in depression on back of bearing as screws are fed through back panel;
12. Hold ground ball clip in place to start one screw, then the other & tighten with nut driver;
13. Start drum belt on motor shaft and position against tensioner pulley;
14. Feed drum through front of machine and loop belt over rear of drum;
15. Slide belt forward on drum as drum moves to rear to keep it aligned with position of tension pulley;
16. Lift rear of drum to place ball hitch on top of bearing, then press down to seat it into bearing;
17. Turn drum to ensure belt alignment, then re-accomplish steps 6 thru 1.
Parts Used:
Rear Drum Bearing Kit Rear Drum Bearing Kit Drum Support Bearing Rear Drum Bearing Kit
  • Doug from ODESSA, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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The dryer gets too hot on top.
Unplugged the dryer, removed the top of, disconnected the electrical connectors, removed the front panel, disconnected the belt, removed the drum, removed the old Safety Thermostat, installed the new Safety Thermostat and assembled the dryer again.
Parts Used:
Safety Thermostat - L285-40F
  • Keith from FOND DU LAC, WI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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lack of heat
Followed the video
Parts Used:
Thermal Limiter - Limit 220
  • ann from WALLA WALLA, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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quit heating
The repair went smoothly considering I am a rookie. The repair videos on your site are great. Followed the techs instructions and got thru it fine.

Thanks,

Jim
Parts Used:
Thermal Limiter - Limit 220
  • James from ALBUQUERQUE, NM
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Rear drum bearing and belt needed to be replaced.
Remove top cover and front and remove drum and install a new bearing kit and new belt.
Parts Used:
Rear Drum Bearing Kit
  • Antonio from LOS GATOS, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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May not have to take out the whole drum to replace the limiter!
After lifting the dryer top and finding the location of the thermal limiter on the back of the dryer, where it is difficult to get at, I carefully cut through the dryer cabinet with the multimaster on three sides to form a 'flap' upon which the limiter was mounted. By prying this flap open from the back, the two wires and two screws are easily accessible to replace the limiter, without having to remove the whole drum. Afterwards, I just bent the flap back into place and taped the seams. If it ever blows again, the fix will take all of about two minutes.
Parts Used:
Thermal Limiter - Limit 220
  • Timothy from CRANBURY, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
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Screeching noise under load
I basically followed the video instructions on your website. Pretty simple but ran into an issue pre-threading the 3 self taping screws into the spindle bearing. The screws provided were blunt on the end and did not tap easily at all. I used the existing screws that were much more "sharp" and worked much better. Also, the new screws were Philips drive and due to the amount of torque trying to self tap nearly stripped them out. The old sharper screws were square drive which had a better bite. So basically, I used the old screws to self tap and then used the new screws for the final installation.
It took a long time to clean all the lint out from the inside of the dryer. The motor was completely embedded with lint and animal hair. You may want to suggest that a good cleaning may be needed so bring a shop vac...and also something to carefully pick the lint balls out from around the motor armature and bearing area. Overall the video instructions were really a big help!
Parts Used:
Drum Belt Rear Drum Bearing Kit
  • John from WESTLAKE, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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clothes get stuck and burn in upper drum glide
Found the promblem as described at this site while looking for diagrams for the dyer. Repair went as described. Once I removed the old upper drum glide I used acetone to remove old glue. Cleaned up fast and easy. Once installed I let cure for about an hour and then reassembled. Let it cure for about an hour more and then I used the dyer. I could feel that the gap around the front of the drum was again narrow so that my finger tip would not slide into a grove. So far so good.
Parts Used:
Upper Drum Glide
  • DOUGLAS from CHILLICOTHE, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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loud squeeling noise
After changing the drum support bearing, and the front felt ring, the noise continued. It turned out to be the tensioner pully. The harmonic vibration travels throughout the dryer box like an instrument so you can't tell where the sound is comming from. Before you do anything, spray a little wd40 between the bushing and the shaft on the belt tenioner pully. If the squeel goes away, you have found your smoking gun.
Parts Used:
Drum Support Bearing
  • Lewis from Thornton, CO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Support was worn out, tub shaft also.
Removed two screws in the inside of the front after opening the top by releasing the two clips. Front comes off of bottom clips easily. Drum can be removed and repairs made. Takes less than 30 minutes Be sure to remove door switch wire & unplug unit first. Drum belt can be re-installed easily thru the back access panel.
Parts Used:
Shaft Drum Support Bearing
  • George W. from Limon,, CO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Zippers and other items on clothing getting stuck in drum.
Followed the instructions in the video. It was very helpful.
Parts Used:
Upper Drum Glide
  • Dan from Parker, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
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loud noise, gringing sound like dry bearings
Took front door off, top off, frunt off, removes screws holding rear bearing pivot, and then removed drum. repainted bearing surface on drum, installed parts, let paint dry for a day and reassembled.
Parts Used:
Upper Drum Glide Drum Support Bearing
  • George from Reno, NV
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Dryer making groaning, squeking and thumping sound
Moved dryer out where I could get to all sides, then pulled top off, then unscrewed the front panel. The drum lifted out of it's ball bearing assembly in the back with a little force. Then it slid out fairly easy.

I replaced the rear bearing assembly, the bottom drum glide strip, the top drum glide and the vent seal all at the same time. The glue for the glide strips took about an hour to set up and I used clothes pins every 4-6 inches as suggested by someone else here on this site. Then I vaccuumed out the entire dryer body, vent pipes and every nook and cranny.

I put everything back as it had come out and then put the dryer back in it's place. Plugged it back in and it's as quiet as when it was new. Total time of project was about 1:45.
Parts Used:
Upper Drum Glide
  • Bryon from Springerville, AZ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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All Instructions for the DE400ADW2
106 - 120 of 323