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SE1000 Maytag - Instructions

All Instructions for the SE1000
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Dryer would not heat up.
I unplugged the dryer,removed the two small screws on the front of the dryer and pulled the bottom forward. The two wires connected to the door do not have to be removed. With an electrical tester using the Ohm setting I tested the Radiant sensor and the Gas Valve coils. The two terminal coil was DOA. The dryer can be operated with the front open as long as the door wires are connected. Symptons: The igniter would heat up and not release gas. My repair was successfull due to this awesome website and the super fast shipping service. AAAA++++
Parts Used:
Dryer Radiant Flame Sensor
  • Roger from Bonners Ferry, ID
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
26 of 29 people found this instruction helpful.
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The Control Pad started loosing fuctions, one at a time until finally my stack unit would not even come on.
First I removed the control panel and board (which requires moving a total of 6 screws. I cleaned the board and touch padthem of the dust that had accumulated over the years and put them back to make sure that they needed to be replaced and when that didn't seem to help, I knew my options. The parts were $350.00 and although that might seem like alot.
I had watched a repairman do this 10 years earlier and saw how simple it was. To have the repairman do it, cost me over $600.00 last time.
He recommended that I replace the unit back then. This is one of the easiest repairs I've ever done. I 'd do it again, if I had to. At this rate maybe I'll get another 10 years out of my washer / dryer stack unit.
Parts Used:
Electronic Control Board Touchpad with Bracket
  • Maurice from Dallas, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
25 of 27 people found this instruction helpful.
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Heard squealing sound when washer went into the "spin" mode. Tub did not spin
Replaced the 2 belts according to instructions received with the belts. Very easy repair
Parts Used:
Belt Kit Belt Kit
  • Edward from Stroudsburg, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
28 of 36 people found this instruction helpful.
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Strange noises - drum not always emptying
Found a very stretched, loose pump belt. Was able to pull it off pump pulley and motor pulley easily. Pushed motor assembly toward transmission pulley and removed wider drive belt. Wiped all pulleys clean. There's a double on the motor- one for drive belt, one for pump belt. Removed two hoses from pump using nutdriver. Removed pump. New pump installed. Installed two hoses on new pump. Installed drive new drive belt. Installed pump belt last. Slid pump to near farthest spot in slots. Tested for correct tension by pinching pump belt. Should be able to pinch center so two pump belt sides come within 1/4" of each other just as the spring tensioned motor mount starts to move. Pused washer back into place after external hoses connected. All new hose washers and filters on both hot and cold. Ran, checked for leaks - none! Absolutely perfect. Put front panel back on. No weird noises and drum empties perfectly every time. My wife is so pleased she's doing more loads.
Parts Used:
Drain Pump Belt Kit Belt Kit
  • Kenneth from Sunnyvale, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
26 of 31 people found this instruction helpful.
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Dyer would not heat, flame would shut off within 10 seconds
I opened the panel, undid the plugs, detached the radiant sensor by undoing one screw and removed and replaced the part. Fairly simply.
Parts Used:
Dryer Radiant Flame Sensor
  • Christy from Riley, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set
24 of 29 people found this instruction helpful.
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washer wouldn't let the water spin out!
I was told that it might be a clog in the tube.. we check the tubes that wasn't it Then I Google it and was told it might be the drain pump. I was just glad that Part Select had what I need because my machine is over 20 years old. We change the pump and now I hope I get at least another 20 years out of my machine. I will always use part select to get my parts. Thanks
Parts Used:
Drain Pump
  • SHARON from DETROIT, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set
22 of 23 people found this instruction helpful.
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Leaking siphon break valve
1. Unplug power to the washer.
2. Remove 2 screws from bottom front panel on either side. Panel then rotates out and unhooks at the top. Remove front panel
3. Remove bolts from underneath the top front on both sides using a socket.
4. Rotate the top upward to provide space to see and work.
5. From the back of the washer, remove 4 bolts using a socket around the drain tube at the upper left.
6. From the front, the siphon valve can be removed from the inside upper right.
7. From the front, unscrew the clamp holding the drain hose on the water pump housing at the bottom right front and remove the hose. Be prepared for water to drain from the hose. Remove hose and siphon valve together and discard.
8. Install new hose on new siphon valve and screw new clamp tight. Make sure the rubber ring is inserted properly on the new valve (See old valve for reference)
9. Holding the siphon valve in place, use a socket and re-attach the 4 bolts around the drain tube at the back of the washer.
10. From the front, insert the opposite end of the new hose to the water pump at the lower right front and screw the circle clamp tight. Note: Re-use existing clamp.
11. Rotate the top back down into normal position.
12. Plug the power back in and run a short cycle and watch for leaks.
13. If no leaks, re-attach bolts for the top with a socket.
14. Re-attach front panel with 2 screws. Done.
Parts Used:
Pump-to-Siphon Break Drain Hose Siphon Break Connector Kit
  • Steven from Indianapolis, IN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
24 of 29 people found this instruction helpful.
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the dryer was just getting warm at best
The dryer was not getting hot the clothes we're damp and had to put on hangers to finish drying. I pulled the cover plate saw the element was glowing the gas cable would kick on had a flame for about a four to six second count. I did some checking on the web. I read about others who were having same type of problem. Order the limit part and now.the flame stays on for about twenty second or less the dryer gets hot and it drys fast. Thanks for the web site. It took about thirty minutes . Now it works great.
Parts Used:
High Limit Thermostat
  • catherine from victorville, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
23 of 27 people found this instruction helpful.
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Rattling sound.
Turned off circuit breaker. Removed two screws at base of front panel with stubby Phillips-head screwdriver. Swung panel up about 30-degrees, and removed panel, disconnecting red and yellow wire to door switch. Removed four sheet metal screws and took off large drum support bracket. Checked drum support rollers and shafts. They were fine. Reset circuit breaker and turned on dryer. Rattling noise still present.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Laurence from Leesburg, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
21 of 24 people found this instruction helpful.
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Would not heat sometimes
Pulled the big front panel by removing two screws near bottom of front and pulling out at bottom until the top pops loose. Vacuumed out all of the dust and checked for loose connections. Ran dryer - igniter would light, but no gas. Checked the two solenoids with a VOM. the one with the two leads would intermittently read Infinity (open). Super simple repair. Remove two screws on solenoid bracket on top of the gas valve, Replace solenoid and plug it back in with the easy push-on connector. NO PROBLEM - all fixed.
Parts Used:
M Series New Style Coil Kit
  • Chris from Laguna Niguel, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
21 of 25 people found this instruction helpful.
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Dryer was making awful noise during use
Removed the screws and took the door off then took the front panel off and popped up the top. Then pulled the drum out. Took snap ring pliers and removed rollers and replaced with new rollers then vacuumed all lint from machine and reversed operation to put everything back together. Operation was a total success!
Parts Used:
Drum Support Roller Kit
  • Pam from Aberdeen, WA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
20 of 22 people found this instruction helpful.
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Gas dryer runs, but no heat.
Unplug the dryer and remove the front panel (two screws at bottom of the panel), being careful of the door switch wires attached to the front panel. Using an ohm meter, I checked the ignitor for continuity and found it was open (should be 50-100 ohms). Make sure to check the solenoids on the gas valve. When the igniter goes bad, it will usually burn out the valve 1 solenoid boost coil (the one with 3 terminals), which was the case with my dryer. The solenoid coils are held in by a bracket with two screws (series 01 dryer) and are easy to remove and replace. Be careful replacing the igniter as the heating element is VERY fragile. Take the time to vacuum out all of the accumulated lint and dust inside the dryer while the front panel is removed, including the lint trap and duct. New igniter and boost/hold solenoid fixed the problem.
Parts Used:
Flat Style Igniter
  • Anthony from Merritt Island, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
21 of 25 people found this instruction helpful.
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Agitator Not Woking
Unplugged power cord then disconnected the water supply and drain hose. Removed 2 screws and took the front panel off. Laid washer on it's side and posistioned the transmission with the cover facing upward. Removed the hex head screws then used a razor knife and a putty knife to remove the silicone sealant. Found that the agitator shaft spring had broken and fallen into the housing jamming the gears that's used in agitation. Removed the oil and all broken pieces of the spring. Installed new shaft spring, replaced the oil then applied sealant to the cover and screwed the cover back down. Let the washer stay in the same posistion for about 18 hours to let sealant dry completely. Then I sat the washer back on it's feet and removed 2 screws that holds the top lid in place. This allowed me access to the tub cover where the injector t is located. Installed the injector t along with the injector tube seal. Connected the hose and hose clamp. Then I put the lid back down and secured with the screws. Connected the water supply and drain hose then the power and selected a wash time and observed the operation. Everything worked ok so I put the front cover back on. Note: I had used the injector t from this washer to fix another washer that an appliance dealer had given me to use for parts to repair the one just described above. That was the only thing that was wrong with it. It was used for about a year and a half and it developed a problem in the spin cycle. Appears to be a brake problem. I intend to repair it as well.
Parts Used:
Injector Tube Hose Clamp Agitator Shaft Spring Injector Tube Seal
  • Richard from Alexander City, AL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
20 of 24 people found this instruction helpful.
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Washer leaking badly and making loud noise on spin
Determined the tub seal was bad and ordered the seal and tub bearing. Removed the front cover with two phillips screws and unbolted the top to lift back. Removed the agitator with 1/4" setscrew on side and lifted out. Using punch and hammer, broke the inner tub nut loose (clockwise is off). Lifted out the inner tub, unscrewed springs from the bottom and removed; then removed the bearing with a little prying (had to raise the tub slightly and tap the center splined shaft to push out) and lifted out the outer tub. Outer tub had few rust spots about to penetrate, so sanded off rust, primed with etching auto primer and sprayed enamel topcoat to prevent further corrosion. Reassembled in the same order.

When done, there was still a loud noise on the spin cycle, so obtained a spin bearing and brake assembly (need to replace both most always). Tilted the machine on its back and removed the pulley, then put a special wrench on the brake assembly and broke loose (counterclockwise) with a 3 foot extension after placing a 2x4 section in the tub between wall and one of the bases for the spring arms (to keep the tub from turning). When the brake came off it was full of water and corroded from the leaking tub bearing previously replaced. Reassembled in reverse order and replaced two belts on the bottom for good measure. Works perfectly now and is very quiet.

In my estimation, the repair should have included both the tub bearing/seal and the spin bearing/brake assy from the outset. Could have used a chain visegrip wrench instead of special tool to remove the brake assy - whatever is available. The tool costs a lot and will never be used again.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Barry from Brooklyn, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
19 of 22 people found this instruction helpful.
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Stripped leveler screw making impossible to level my washer
Put blocks under the washer where the leveling leg was needed and screwed the part into the washer. Then it was just a matter of moving the washer into place and leveling. Pretty easy.
Parts Used:
Adjustable Leveling Leg Rubber Foot Pad
  • Rebecca from Wylie, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Wrench set
21 of 28 people found this instruction helpful.
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All Instructions for the SE1000
61 - 75 of 1475