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MLE15MNAYW Maytag Dryer - Instructions

All Instructions for the MLE15MNAYW
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Loudly squealing dryer
Piece of cake. Use the available manual to ascertain dismantling procedure. Only thing that might be tough for average DIY'er is the internal snap rings. Snap ring pliers are mandatory for quick easy repair.
Total time was probably about 15 minutes and this was the first time I had taken it apart. Quiet as a mouse now!
Very helpful site.
Parts Used:
Idler Arm and Shaft Idler Pulley Shaft Washer Retaining Ring Idler Pulley Wheel and Bearing Drum Support Roller Kit
  • Donald from Bridgewater, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
5 of 10 people found this instruction helpful.
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baffle broke
i removed the 2 screws holding the door hindges on. then i removed the 2 adjasent screws to remove the front door panel. i rotated the drum to aceses the screws holding the baffle and installed the baffle .
Parts Used:
Short Baffle
  • Tom from Crystal City, MO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
3 of 4 people found this instruction helpful.
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Dryer baffle broke when drying sneakers
I was able to quickly make this repair with the help of some instructions that I found on this site on how to remove the front panel of my dryer. 4 screws on the front around the door (and removal of the door) and then it was simply a matter of rolling the top portion out to pop it out of some clips and then the front panel opened toward me and I was able to lift it off of the metal fingers that secure it on the bottom. Removing the old baffle was a matter of removing two screws with a nutdriver and installation of the new baffle was a breeze. All in all I was done start to finish in under 10 minutes.
Parts Used:
Short Baffle
  • Chad from West Fargo, ND
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
3 of 4 people found this instruction helpful.
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Noisy & Drum stop working
Replaced damaged parts and recommended parts normally causing the problem. Dryer is working again like new. I expended $112 rather than $600 for a new equipment. Good deal!
Parts Used:
Retaining Ring Idler Pulley Wheel and Bearing Roller Shaft Idler Shaft Retaining Ring Multi Rib Belt - 91-5/8 Inches Dryer Drum Felt Seal Drum Support Roller Kit
  • Tulio from ASHLAND, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
5 of 10 people found this instruction helpful.
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electric dryer stopped heating - the thermostat got very hot
The numbers on the metal plates were the JC Penney numbers - that no one recognizes. I eventually found the model number inside the timer case on a printed schematic. I started by disassembling whatever metal covers were removable by finding sheet metal screws and unscrewing them. If you pull on the sheet metal covers, you can find where they are connected to the frame. Eventually, I found that both the heating element was broken and the thermostat was fried. It took a while looking at various websites to find the proper parts. It's all OK now.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Ignas from Midpines, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
4 of 8 people found this instruction helpful.
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Dryer Was Making A Very Loud Screching Sound
I looked on line and found a scematic from your web site to determine how to dismantel the dryer. Once I was inside I was able to determine that the drum roller was making the noise. I decided to replace the other moving part while I was inside just in case. . . Pretty easy job
Parts Used:
Multi Rib Belt - 91-5/8 Inches Idler Pulley Wheel and Bearing Drum Support Roller Kit
  • Mitch from Ripin, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
3 of 5 people found this instruction helpful.
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Broken Baffle in Dryer
Removed Dryer Door and front face of dryer, total of 4 screws, turn dryer drum to position broken baffle screws, remove screws, install new baffle, attach front face of dryer and reattach dryer door. Time 15-30 min. total. Real easy. Thank You PartSelect. Maytag told me my part was no longer available, but I fold it at PartSelect.com.
Parts Used:
Tall Baffle
  • Brian from Warsaw, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
2 of 2 people found this instruction helpful.
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motor hummed but wouldn't turn drum
Unplugged dryer and removed screws that hold door in place. removed screws that hold front panel. removed front panel. took drum belt off idler pulley. pulled drum out of dryer cabinet. unhooked wiring harness and removed motor. replaced motor and reversed steps to put back together. Thanks to partselect for getting me the parts so quickly. I ordered the motor on line on Friday and it was at my house on Saturday.
Parts Used:
Drive Motor - 115V
  • Yvonna from Mulberry Grove, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench set
3 of 5 people found this instruction helpful.
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squeaky sound when drying
Removed front panel and tumbler, replaced roller axle,
wheel, and front glides. Anybody can do this.
Parts Used:
Roller Shaft Front Glide Kit
  • Chris from Sherman, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Wrench set
3 of 5 people found this instruction helpful.
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front glides wore out
Followed instruction video
Parts Used:
Front Glide Kit
  • james from WOODBURN, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
2 of 2 people found this instruction helpful.
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Dryer would not run; blown thermal fuse
unplug dryer; remove dryer door; remove front cover; thermal fuse located on heater underneath and beside drum; remove two electrical leads on fuse; remove two screws holding fuse in place; install new fuse and do the above in reverse; clean lint from duct; plug dryer into
Parts Used:
Thermal Fuse (Limit: 183)
  • Michael from OAKWOOD, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
2 of 2 people found this instruction helpful.
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Noisy tub rollers
By watching a video I disassembled the front and took the dryer tub out and replace the two rollers and it took about 60 minute.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Johnny from MUNCIE, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Loud squeaking noise
I removed the front of the dryer and the drum support plate. I drilled out the old rivets and installed the Glides with the enclose rivets. The Glides came loose in a few days! The holes in the glides are larger than in the old Glides. I disassembled the dryer again and reassembled with my rivets. This time I held the rivet gun inside the perimeter of the dryer so that the head of the rivet is opposite the initial installation. So far, so good, except the dryer still squeaks. The idler pulley is now the culprit. White grease burned up. I reassembled with high temperature grease. If that does not work, I will need another idler pulley. The journal looks very worn. the dryer is 30+ years old.
Parts Used:
Front Glide Kit
  • William from ORANGE, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
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Dryer was leaving black marks on the clothes, and was very noisy.
The video was excellent and made for an easy repair. Would highly recommend.
Parts Used:
Front Glide Kit Drum Support Roller Kit
  • Fred from GREENCASTLE, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Screw Idler Arm Screw Sleeve
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
2 of 2 people found this instruction helpful.
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All Instructions for the MLE15MNAYW
91 - 105 of 532