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MDE21PNAGW Maytag Dryer - Instructions

All Instructions for the MDE21PNAGW
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Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Dryer was leaving black marks on the clothes, and was very noisy.
The video was excellent and made for an easy repair. Would highly recommend.
Parts Used:
Front Glide Kit Drum Support Roller Kit
  • Fred from GREENCASTLE, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Screw Idler Arm Screw Sleeve
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Noisy
This is the dryer of a 28 year old Maytag laundry pair. I had replaced the glide kit 8-10 years before. Did them again because they were worn in half again but this time I added the 2 roller kits and the belt, really just guessing. I was surprised how full of dust and lint the inside was, especially the blower fan blades. I ordered the screw because the belt idler pulley assembly was very wobbly and I hoped that was the screw anchoring it to the motor housing was the problem but it wasn't. Turns out the threaded hole in the housing was stripped, due I guess to years of vibration. It was too tight to get a tap and dye in there so I drilled the hole out and replaced the screw with a bolt and nut and lock washer. Before drilling it out I tried a few strands of wire and JB Weld, like the trick with stripped wood holes where you break off toothpicks in the hole and fill with wood glue. But that stripped out too so I drilled and used the bolt. Turned out I didn't need that $7 screw. Probably should have known comparing it to the old one which looked the same after I cleaned it. Anyway, it sounds fine again.
Parts Used:
Screw Multi Rib Belt - 91-5/8 Inches Front Glide Kit Drum Support Roller Kit
  • Dave from CRANBERRY TWP, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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squeaky sound when drying
Removed front panel and tumbler, replaced roller axle,
wheel, and front glides. Anybody can do this.
Parts Used:
Roller Shaft Front Glide Kit
  • Chris from Sherman, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Wrench set
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replace door closer
Removed power and front panel, removed broken latch, pushed in new latch and replaced the front panel and power. Done
Parts Used:
Door Catch Kit
  • Erwin from Somersworth, NH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set, Wrench set
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dryer door would not close
discovered it was a broken latch. Ordered the latch, only took 2 days to arrive and all I had to do was remove the broken latch and snap in the new one. I saved myself a service call. I'm very happy!!!!!!
Parts Used:
Door Catch Kit
  • Priscilla from Portland, ME
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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broken door clip
After watching the great install video, I followed his lead and within 20 min had my dryer door fixed. This dryer was bought in 1986 and I really thought I was looking at buying a new dryer. How wonderful that I could fix it for less than $11. Easy to find web site, easy to find part, great instructions and fast delivery!
Parts Used:
Door Catch Kit
  • Lynette from Rock Island, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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The dryer was make a loud screeching sound
Remove the door and the plastic brackets on the other side of the door opening. Remove the front cover by gentally pulling from the top first. Support the dryer basket (I used an old towel and a block of wood. With a 1/2 inch wrench remove the Roller Shaft with the Drum Support still attached. Replace new shaft and drum support. (always replace both at the same time or you will find that the problem will come back much sooner.) Careful when installing. Make sure that the new non metalic washers (suppied) are propery seated when you are tightening down the nut.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Jonathan from Spokane, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Wrench set
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squeak when drum rotated
I removed the dryer door and attaching hardware to other covers. Raise the top cover and prop it up. Remove the drum retaining cover and disconnect the door switch wires, making note of their locations. Release tension on idler and take belt off of motor. Pull the drum out with belt still around it. Vacuum lint and dust from inside cabinet. Use snapring pliers and remove the snaprings on the drum rollers. Remove the old rollers and washers, clean the shafts and apply a light film of oil on the shafts. Install new rollers and plastic washers on shafts and secure with snaprings. Remove the "E" clip from the idler shaft and remove the old roller. Clean and lube the shaft and install the new idler and clip. Place the new belt on the drum with the ribs against the drum. Put the drum in place and install the front drum retainer. Position the belt around the motor pully and tensioner. Rotate the drum to get the belt to track. Attach the remaining covers.
Parts Used:
Idler Pulley Wheel and Bearing Multi Rib Belt - 91-5/8 Inches Drum Support Roller Kit
  • Bruce from Pitman, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Baffle partially flopping around
Save the money and buy the part with partselect. My dryer problem was obvious. Before I purchased the part I jumped on YOUtube to see if there was a repair video that matched my problem. FRIELINK5 had a very thorough video. This guy did it with one hand and overall it looked easy. Then I ordered the part. When it arrived I gathered all of the tools first. Rewatched the youtube video, then installed the part. I recommend going through parts select problem determination if you do not know what is wrong. Follow the instructions and purchase the part. I saved probably over $125. House call 50$ + Labor and part $100 from a service call. TRY IT save money.
Parts Used:
Short Baffle
  • mary from Temecula, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
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The female catch in door was bro9ken
I took out the old worn out part and replaced with the one I order.
Parts Used:
Door Catch Kit
  • JOSEPH from ANSONIA, CT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Loss of two baffles
Others have described how to remove 4 screws and remove the front panel of the dryer. The problem I saw is that some screws broke off and fell inside while others remained on the separated baffle. The old screws that I found were 1 1/4 inch. The parts manual indicates a replacement screw that is 1 inch long and a number 10 width. One set of holes for the baffles has slotted holes. It appears that wear in the paint indicates movement before breaking off. My solution to the slotted holes was to use washers on the screws and to tighten the screws in the position where any force was not going to move the screws to the center position of the slots. The force of the separation caused the slotted holes to expand.
Parts Used:
Short Baffle
  • James from Revere, MA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
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Squeeking
First removed front door 2 screws holding it to frame, then removed 2 screws holding front cover panel on tilt out front panel, used vac to clean inside, removed idler arm with pully attached, replaced with new parts when I did a test run still had a llitle squeek, the drum support wheel on right looking from front making some squeeking,I went back in removed part shaft had small rust spot cleaned with jewelers cloth lubed and wiped off, no more squeek I wish I had ordered new drum wheel when I ordered idler parts, then I could have done a complete overhaul now I know more I have never worked on a dryer before the drawings on the web site heleped a lot
Parts Used:
Idler Arm and Shaft Idler Pulley Wheel and Bearing
  • David from Colbert, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Broken belt, drum did not spin.
We could not find directions for the brand that we have. First we took the back off, which we did not need to do.
lift the top of the dryer, remove the front remove drum. Place belt on front of motor, wrap double belt around support on bottom of dryer, open the remaining belt and stretch around drum. Hold drum in place, replace front and top.
Need at least 2 people, not at all intuitive.
Parts Used:
Multi Rib Belt - 91-5/8 Inches
  • Beth from Feura Bush, NY
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers
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Dryer was making rubbing noise
With the parts in hand, and after disconneting power and shutting off gas line, I again removed the door, front panel and front tumbler frame to expose the blower wheel. I discovered that the blower wheel was not damaged, but that compressed pieces of lint and other items where stuck to the wheel. I removed the pieces and vacuumed the the whole thing clean, tested it, and the sound stopped. Since I had the unit open, I replaced the front glides by drilling out the old rivets, removing the old glides and then riveting the new glides in place. A very simple procedure overall.

Make sure you keep track of where the different screws go and keep them inside something so you don't lose them. I also used my cell phone to photograph various areas and screws for later reference.
Parts Used:
Front Glide Kit
  • chris from port washington, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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All Instructions for the MDE21PNAGW
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