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LSE7806ACE Maytag Washer Dryer Combo - Instructions

All Instructions for the LSE7806ACE
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Rattling sound.
Turned off circuit breaker. Removed two screws at base of front panel with stubby Phillips-head screwdriver. Swung panel up about 30-degrees, and removed panel, disconnecting red and yellow wire to door switch. Removed four sheet metal screws and took off large drum support bracket. Checked drum support rollers and shafts. They were fine. Reset circuit breaker and turned on dryer. Rattling noise still present.
Removed six small screws holding blower fan assembly. Shaft receiver on squirrel cage fan was worn completely round (it should fit onto a half-round shaft). Ordered new blower fan from PartSelect.com. Replaced tonight, and it works beautifully. This dryer is 29-years old. All it's ever needed in the 10-years I've owned it is a belt replacement and this repair. Long live the 1970s Maytags, and good parts suppliers like this one.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Laurence from Leesburg, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
21 of 24 people found this instruction helpful.
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Dryer was making awful noise during use
Removed the screws and took the door off then took the front panel off and popped up the top. Then pulled the drum out. Took snap ring pliers and removed rollers and replaced with new rollers then vacuumed all lint from machine and reversed operation to put everything back together. Operation was a total success!
Parts Used:
Drum Support Roller Kit
  • Pam from Aberdeen, WA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
20 of 22 people found this instruction helpful.
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Plastic thing (Fill Injector) that puts water in the washer broke
Unfortunately, I couldn't find instructions for removing the top for exactly this model. First step was to remove the front panel by removing the two lower screws, grabbing the bottom of the panel, and lifting up until the clips on top of the panel let go. Next was removing from underneath the two screws towards the front that held the top of the washer on. This gives you easy access to the Fill Injector, but if working alone you'll need something to prop up the front of the top lid while you work on it. There is one screw that hold on the Fill Injector assembly (top and bottom). This screw is removed from the top, via the control panel. To get inside the control panel you need to remove the back of the control panel (very easy), just unscrew the 5 screws on the back of it. Then remove the one screw that holds the Fill Injector assembly in place. From under the front panel, use your pliers to remove the hose clamp and then remove the Fill Injector from the hose. ONE IMPORTANT ITEM, YOU'LL DEFINITELY NEED A REPLACEMENT HOSE CLAMP. The one you remove to take off the old, broken fill injector cannot be put back on. Put the new clamp loosely on the hose, then connect the hose to the new Fill Injector Assembly. Put the Fill Injector Assembly in place and use a piece of duct tape to hold it there. Then reinstall the screw that holds it in place from the top, inside the control panel. Reinstall everything in reverse, give it a test and then have a beer. You've just "given it to the man" and saved yourself $100+ on a repair bill.
Parts Used:
Upper Fill Injector Lower Fill Injector
  • AMY from Mount Kisco, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Socket set
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Washer drum not spinning correctly
Drum on the Maytag washer was not spinning is a true rotational pattern. Adjust or replace the centering springs.

How-to-description
I had to hack saw off the centering springs eye bolts since they were rusty and not adjustable. If you have to cut the old eye bolts as I had to, be careful... the spring will jump up an inch or two very quickly and you want to keep your hands clear. It makes a load noise and my wife asked "what happened". Not a big deal, just be aware of the spring returning to a normal state.
Place the new eye bolts in position and tighten the nut with 4 turns. With duck tape I held the eye bolts in place from under the machine. Had my son push the drum towards the replaced spring to shorten the length of the end of the spring to the eye bolt. Stretch the new springs with a long screw driver, one end against the washer body, and the other end near the handle. Pulled down on the scrw driver until the spring can hook onto the eye bolt. Before cutting the old eye bolts I measured the length of the eye bolt from the spring to the frame. Adjust the new eye bolts to the same length after the spring is stretch onto the eye bolt. Overall a simple project, cost $40 for me and the best advice is using the long screw driver to pull down on the springs.
Parts Used:
Centering Spring BOLT Eyebolt Nut
  • Paul from Huntley, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
21 of 27 people found this instruction helpful.
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Washer leaking badly and making loud noise on spin
Determined the tub seal was bad and ordered the seal and tub bearing. Removed the front cover with two phillips screws and unbolted the top to lift back. Removed the agitator with 1/4" setscrew on side and lifted out. Using punch and hammer, broke the inner tub nut loose (clockwise is off). Lifted out the inner tub, unscrewed springs from the bottom and removed; then removed the bearing with a little prying (had to raise the tub slightly and tap the center splined shaft to push out) and lifted out the outer tub. Outer tub had few rust spots about to penetrate, so sanded off rust, primed with etching auto primer and sprayed enamel topcoat to prevent further corrosion. Reassembled in the same order.

When done, there was still a loud noise on the spin cycle, so obtained a spin bearing and brake assembly (need to replace both most always). Tilted the machine on its back and removed the pulley, then put a special wrench on the brake assembly and broke loose (counterclockwise) with a 3 foot extension after placing a 2x4 section in the tub between wall and one of the bases for the spring arms (to keep the tub from turning). When the brake came off it was full of water and corroded from the leaking tub bearing previously replaced. Reassembled in reverse order and replaced two belts on the bottom for good measure. Works perfectly now and is very quiet.

In my estimation, the repair should have included both the tub bearing/seal and the spin bearing/brake assy from the outset. Could have used a chain visegrip wrench instead of special tool to remove the brake assy - whatever is available. The tool costs a lot and will never be used again.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Barry from Brooklyn, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
19 of 22 people found this instruction helpful.
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Stripped leveler screw making impossible to level my washer
Put blocks under the washer where the leveling leg was needed and screwed the part into the washer. Then it was just a matter of moving the washer into place and leveling. Pretty easy.
Parts Used:
Adjustable Leveling Leg Rubber Foot Pad
  • Rebecca from Wylie, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Wrench set
21 of 28 people found this instruction helpful.
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Dryer had burning Smell - Start/Run windings problem
** Your best bet is to use a digital camera to take pictures of the various stages as you take apart the dryer - especially the wiring. And, use masking tape to label all the wires.
** I removed the Blower Housing which made the process much easier.
** Find a friend with or buy the snap ring pliers
** Big Secret not mentioned anywhere - the Motor Support (diag. #20) can be removed ! Hence - the entire Motor assembly can be taken out to remove those irascible Motor Clips.
** For the Green ground wire going from the dryer frame to the motor, you need to take the screw from the old motor and use it to screw into a hole marked with a black "slash" on the new motor.
** After 3 days of WD 40 and an allen wrench, I could not remove the Motor Pully from the old motor, so I would buy one if I were you.
** Hardest Parts - Removing the Motor Clips, reattaching the idler spring!, having another person hold the drum while I installed the Belt and reattached the front drum frame thingy, and deciphering my wiring schematic and reassembly diagrams ! That is why a digital camera is so helpful.
** The process is really very easy if you use the suggestions above and read the others.
** Find the "Model Diagram" on the PartSelect website - an excellent resource !!
** A twenty+ year old Maytag - up and running again !! Many thanks to others who shared their story.
Parts Used:
Tumbler and Motor Belt MOTOR PULL Drive Motor Retaining Ring
  • Thomas from Raleigh, NC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
18 of 20 people found this instruction helpful.
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no water drain
removed old pully, put new one on with hex driver, removed belts, put new belts on and finished.
Parts Used:
Belt Kit Belt Kit Motor Pulley
  • Franz from Lakeland, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
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washer would not fill with water
The trouble-shooting section on this website described the above problem and suggested that the proper course of action was to replace the water inlet valve, which I ordered and replaced. Replacement of this part was quick and easy.
Parts Used:
Water Inlet Valve
  • Fredrick from Clinton Corners, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
20 of 26 people found this instruction helpful.
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My washer stopped draining
My washer filled up and wouldn't drain at all.

I tried checking the fuses, then read that the belt could be broken or worn. I checked under the hood and the belt was broken right in two. I drained the washer manually then ordered the new belt.

I was able to replace the belt in no time with no effort at all.
Parts Used:
Belt Kit
  • Jenna from St. Louis, MO
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Water leaking from the underside center of the tub. Only on the rinse cycle.
I want to mention only the difficult parts.
The removal of the retaining ring/nut (which is under the agitator) . After 10 + years, it was very hard to move this part and it was eventually broke it to remove it. WD40 was used but not effective (to much calicum build up). You must turn the cone shaped piece (located under the inner tub) clock wise to get it to remove. A spanner wrench was not used to remove this. I used a punch and a tack hammer. We could not remove the old tub bearing (closest to the shaft), so we just cleaned it up with emory cloth and used the new tub seal/outer bearing. Spins great but have not been able to check the water leakage problem yet.
Caution: there are two dark colored ring (very thin) that go back on top of the rubber collar. These must be reused. These are hard to see. I pushed the old tub seal/bearing out with the end of a 2x4 (very slowly and carefully). I put the tub up on two of the 2x4's, for clearance off of the floor and used the third to knock the old bearing out. Old machine are very messy.
Parts Used:
Tub Bearing Kit
  • Mark from King George, VA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
19 of 24 people found this instruction helpful.
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Machine would shake violently while tub was spinning
I followed the supplied directions to remove covers, unbolt tub springs, and expose the area needed to replace the damper pads. I cleaned the area with acetone and applied a rubber adhesive (not supplied). I used tire patch compound because that is what I had on-hand. I positioned the pads and after they had dried 1/2 hour, lubricated them with the supplied grease. I reassembled the washer and it is now smooth and well behaved.
Parts Used:
Damper Pad Kit
  • Gary from Alhambra, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
16 of 17 people found this instruction helpful.
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Loud rumble in dryer. Blower wheel broken.
First I unplugged the machine. I removed the two screws in the front panel and tilted the bottom of the panel out unclipping it at the top. I removed the lint duct whichis held in place with several 1/4" hex head screws. Then I removed the blower cover, also held on wth 1/4" hex head screws, exposing the blower wheel. Using snap ring pliers I removed the snap ring at the end of the motor shaft. Using needle nose liers I removed the spring clamp around the center hub of the old blower wheel and pull the blower wheel off the motor shaft. After cleaning as much lint out as I could I put the new blower wheel on the motor, secured with spring clamp and snap ring. Then I put the blower cover and lint duct back on and put front panel back on.
Parts Used:
Blower Wheel with Clamp
  • Ernest from York, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
16 of 17 people found this instruction helpful.
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Clothes were not drying, three hours still damp
Followed the instructions on the video, and saved 500 hundred dollars. I was already shopping for a new dryer. Thanks so much!
Parts Used:
Blower Wheel with Clamp
  • STEVEN from BELLEROSE, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
16 of 17 people found this instruction helpful.
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lint on clothes
replace lint filter under agitator, remove 1 screw, lift out agitator and replace filter screen.
Parts Used:
Self-Cleaning Filter
  • gene from longmont, CO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
22 of 35 people found this instruction helpful.
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All Instructions for the LSE7806ACE
46 - 60 of 1125