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LDE7304AGL Maytag Dryer - Instructions

All Instructions for the LDE7304AGL
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Dryer Barrel was not turning
Looked in one of the back removable panels and saw the broken belt. Took the machines front panel off per a You Tube video and saw the repair was simple but too the time to vacuum out a large amount of Lint Debris that had accumulated over the past 34 years all over the inside of the machine which is dangerous.. After cleaning it all up I simply put the new belt on and put everything back together and it all works nicely again!
Parts Used:
Tumbler and Motor Belt
  • Frank from HAWTHORNE, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Original tumbler/motor belt broke. Gas Dryer
I UNPLUGGED TH UNIT.Removed the 2 screws holding the front panel in place, disconnected the electrical leads on the panel. These screws are located on each side of the panel 3 in. from the bottom. Removed the 4 screws holding the shroud. Disconnected the ground wire on the shroud & set both aside. Installed the new belt per the diagram & instructions. Turned the tumbler by hand a few times to verify proper installation. Re-installed the shroud & front panel including reconnecting the leads & ground wire. You need to use both hands in a tight space to install the belt on the pulley & guide(a littledificult) The new belt fit perfectly & the instructions were easy to follow & accurate.
Parts Used:
Tumbler and Motor Belt
  • Joseph from HALETHORPE, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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blower fan central stem broke off. was making a bad noise.
We had trouble getting the front of the dryer off; we tried to pry the top off. It works better if you remove the screws at the bottom of the front panel ;) Once we had the front off, we used a 1/4" ratchet wrench to take the front off the fan housing. We took off the compression clamp off easily with a pair of priers. Removing the retainer clip was harder; we ddn't have the right tool. We removed the broken fan. We ordered the part, easy peasy, from this website. Had to buy a $9 tool to put the retainer washer back on. We reassembled the fan housing and put the fron back on. It worked! Total cost: ~$30.00. Actual time (excluding waiting for parts and buying tools): 2 hours.
Parts Used:
Blower Wheel with Clamp
  • David from EASTPOINTE, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Socket set
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Blower wheel worn replaced belt became it looked worn
Fallowed instructions on YouTube
Parts Used:
Tumbler and Motor Belt Blower Wheel with Clamp
  • James from NEW CASTLE, DE
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
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replace idler pully and belt
After viewing repair video I used those instructions, after removing drum place new belt on drum, I used scotch tape to hold belt in place, tape belt with 2 inch strip about every foot around drum, leave extra belt that connects to drive motor folded down and taped to drum. After installing drum connect belt to drive motor and roll drum to remove tape. This will keep belt from sliding out of place on drum while installing.
Parts Used:
Idler Pulley Shaft Washer Idler Pulley Wheel
  • ellison from LAKE PLACID, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Part access but easy solution!
Overall, the repair was pretty easy. I'm a 52 year old woman who has never done drier repair. I replaced both front glides, both drum support roller wheels, the idler pulley wheel and the tumbler and motor belt. Including vacuuming out the inside of dryer and washing down the inside and outside of dryer with cleaning wipes, the whole project took me 2 hours. (if done individually, time would have been 20-30 minutes). You must have correct tools, so I did have to purchase two tools that I didn't have. My only suggestion in replacing the idler pulley wheel and the tumbler/motor belt would be to take the small access panel off the back of the dryer for easier access to the parts.
Parts Used:
Tumbler and Motor Belt Idler Pulley Wheel Front Glide Kit Drum Support Roller Kit
  • Amy from POCATELLO, ID
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Belt broke...drum would not turn but there was heat.
Removed front cover.removed 4 screws holding drum in place. Cleaned out lint from everywhere. Placed new belt over drum looping it over idler arm & motor pulley. Pushed drum back ; rotated drum to see that belt was engaged. Put front drum bracket in place. Put front panel in place with 2 screws at the bottom. Tested motor & rotation of drum; then checked heat. All worked fine. Took 1 hr. but most time spent cleaning lint.
Parts Used:
Tumbler and Motor Belt
  • Dirk from CHESWICK, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
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Noisy tub rollers
By watching a video I disassembled the front and took the dryer tub out and replace the two rollers and it took about 60 minute.
Parts Used:
Roller Shaft Drum Support Roller Kit
  • Johnny from MUNCIE, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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My Blower wheel had broken at the center where it attached to the axle. It made a rattling sound and no air was being blown into the drum to dry the clothes. There was also a loud skidding sound that turned out to be due to a worn felt seal.
I took off the front of the dryer with the screws at the bottom. I removed what wires would easily come off and took a picture to remember where they go. Then I took of the front panel and had to take off the cover for the blower wheel. Some screws were difficult to reach because they were in a very tight space. I used a combination of needle nose pliers and a hex screw bit to loose hared to reach hex screws.
For the felt seal on the front panel, I used a flathead screwdriver to remove the old seal and replace the new seal. The most tricky thing was making sure the seal was laying right along the drum when putting the front panel back on. Once back together, the skidding sound disappeared.
Replacing the blower wheel is pretty easy once I got past the difficult screws holding the cover down. I used snap ring pliers to remove the snap ring then put the new blower wheel on and put it all back together. I found that the tip diameter of the snap ring pliers needed to be less than 0.05'' to fit into the snap ring holes of both the snap rings for the roller wheels and the blower wheel.
Parts Used:
Front or Rear Drum Felt Seal Blower Wheel with Clamp
  • Spencer from COLUMBIA, SC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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Dryer was leaving black marks on the clothes, and was very noisy.
The video was excellent and made for an easy repair. Would highly recommend.
Parts Used:
Front Glide Kit Drum Support Roller Kit
  • Fred from GREENCASTLE, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Idler pulley arm mounting screw stripped
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Screw Idler Arm Screw Sleeve
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Noisy Dryer.
Opened your replacement part and found a broken fin on the blower wheel. no way I was going to return it and wait another week for another part. Perhaps you folks need to inspect what you send out. 1 blower wheel with a broken fin and 2 clamps. Replacement was easy and quickly accomplished. Having replaced drum rollers and the belt this dryer is almost new. Thanks
Parts Used:
Blower Wheel with Clamp
  • Rodney from FAYETTEVILLE, GA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Squeaky when in use, after replacing the drum pads.
I followed the videos provided, the only think I would added is cleaning the riding surface of the drum. In my case the drum had gunk on it from the old pads, witch got on the new pads causing it to continued to make noise.

It would be wise to also get the felt and belt, to replace them all the first time.
Parts Used:
Tumbler and Motor Belt Front or Rear Drum Felt Seal
  • Greg from CAVE CREEK, AZ
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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front glides wore out
Followed instruction video
Parts Used:
Front Glide Kit
  • james from WOODBURN, IN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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hole in filter
took out old and placed in new
Parts Used:
Lint Filter
  • Robert from WESTCHESTER, IL
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
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All Instructions for the LDE7304AGL
91 - 105 of 733