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DDC5000SBLAD General Electric Dryer - Instructions

All Instructions for the DDC5000SBLAD
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The lint filter was cracked/ screen came off
Very simple. Took the old 1 out and placed new filter in.
The impressive thing was I ordered the part on a Saturday and received it on the following Wednesday. Thank you! I will for sure recommend your site to my family/friends.
Parts Used:
Lint Filter with Frame
  • Dan from Erie, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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My GE Hotpoint dryer would not completely dry clothes due to rusty and clogged flint filter.
I just pulled out the old white frame by hand and replaced it with a new one ordered online. No tools were needed. Simply easily, anyone can do with no required skills.

This saved the appliance from possible damage due to poor ventilation and also save the cost of a handyman to fix the problem.
Parts Used:
Lint Filter with Frame
  • Mark from Teaneck, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Dryer shut down completely, wouldn't start
Removed 3 torx screws on the control panel. Removed two more regular screws from the dryer opening. This allows removal of the top. Removed some panels from the back to access where belt feeds through the motor. Found the belt snapped in two inside.

Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.

Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
Parts Used:
Drive Belt
  • Rob from Valencia, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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squeaking noise then drum stopped turning
The repair in retrospect was very easy. Not knowing alot about the dryer I made one mistake. I put the bearing in backwards and broke the rubber gasket. After ordering a new gasket and paying close attention to what I was doing it worked out fine. Saved me about $200 for a repairman.
Parts Used:
Rear Drum Bearing
  • mountain ridge pet from nashua, NH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Very loud squeak with drum rotation
Key starting point is to remove top cover by removing two long screws located at the front of the cover
Remove control panel and it's bottom and side supports.
Remove short vent pipe by bending retainer tab.
Support the drum at the top using piece of rope.
Remove main rear cover (leave bottom attached).
Remove electric heating unit and install new bearing carrier from kit.
Reinstall the the heating unit
Remove three screws (inside the drum)to release the inner drum cover and release the bearing carrier.
Install new bearing carrier. Note: the three holes in the bearing carrier are not tapped, I suggest that the screws be installed (threads cut) into the bearing cover before attempting to install the bearing carrier.
Install the new bearing carrier. Note: pilot one of the holes using a small nail etc. then go on to install screws in the other two holes remove the pilot device and install the third screw.
Reassemble in reverse order.
Parts Used:
Rear Drum Bearing Kit
  • William from San Juan, TX
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Wrench set
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Tabs on gasket were not spaced as on door
Had to skip holes for tabs on corners. could not stretch gasket to fit the holes. Cut off the unused tabs in order to close door. Used pliers to push tabs in holes. New gasket fit sufficently and is better than old cracked gasket.
Parts Used:
Door Gasket
  • Ruth from Frederick, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers
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Belt broke, tumbler did not turn.
After identifying the issue, the biggest issue was trying to identify how to get the belt around the drum tumbler. After looking through the back hatch, I figured the best way was through the top. I removed the top just enough to work the belt in between the drum and the front sheet metal. Then I turned it on its side and worked the belt from the back hatch. I pulled the pulley back on the tensioner and slipped the belt under neath. Put it back together, been working great.
Parts Used:
Drive Belt
  • John from Dushore, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
Parts Used:
Rear Drum Bearing Kit Drive Belt
  • Stephen from Kendall Park, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Rythmical Squeaking
The instructions that came with the bearing were limited and the illustrations were too dark to see. However, after reading the reports of others on this website, the repair was very easy.

Prior to disassembly, remove theaccess panel on the rear of the dryer. Pull the belt drive pulley arm up and the belt will easily slide off of the motor pulley. The belt can be left on the drum.

Then, remove two screws at the inside top of the dryer door. The top of the dryer will then lift up at the front and slide forward to remove. This will allow you access to two bolt head screws on each side of the front panel. Remove these two screws and then lift the panel slightly up and forward. The front panel will then be free and the dryer drum will slide forward and out. Remove the four bolt head screws (behind the electric elements) from the heater element on the inside back of the dryer box.

You can now exchange the bearing on the drum and the bearing insert on the dryer heating element simply by removing the old and reinstalling the new just as the old was removed - four screws for each.

You will need an assistant to re-install the bearing. Someone needs to hold the three pieces behind the drum as you insert the three screws. You'll also need a star wrench set for this.

The drum is easily reinserted - just be careful to get the front of the drum placed into the front bearing surface when reinstalling the front panel. One word of caution, My wife tried to remove the felt bearing on the bottom of the front panel thinking that it was lint.

I found that the inside of my ten year old dryer was unbelievably full of lint. I'm sure that the efficiency improvements by cleaning the air passages will be substantial and I've just saved $400 on the price of a similar dryer ($900 if my wife and I decided to upgrade to the "new" model that we wanted but really didn't need.
Parts Used:
Rear Drum Bearing Kit
  • Michael from Edmond, OK
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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No heat
This is kind of embarrassing but ... Originally checked this site for what to get for the symptom and said 61% of time was high limit thermostat which was fairly cheap (14.95) but assumed with my luck, it would be the more expensive part the heating element coil with housing, so ordered that. (It was second on the list) Received it in no time, like less then 48 hrs. Was told when a friend stopped by that I shouldnt of ordered that, it was probably a thermostat as that is what they had to replace on theirs. So I said ok, I could always send the first thing back, so ordered the thermostat. It came quickly again. Took it out of the package and laid it down to change clothes to take the dryer apart and could not find where I laid it. Spent all evening looking and never did find it! So I ordered another one. (Figured by this time PartSelect was thinking this woman is crazy but good for business) Again it came quickly. Got it on fine but when I got to check the old one with the ohm meter (which I borrowed), nothing wrong with it. Nor with any of the other 4 thermostats. Finally took the drum off ( thanks to Youtube video for instructions) and obviously it was the initial part that I had ordered that needed replaced. Was a bit awkward to remove all the screws to get to it but not bad. Plugged everything back in and got the machine back together and works wonderfully! Lessons learned: 1st check the elements with an ohm meter (I will definitely be investing in one) 2nd do not open package until ready to use it especially after a bad day at work and 3rd go with initial gut instinct! I was very pleased with Part Select service!
Parts Used:
Heating Element Coil with Housing - 240V
  • Mavadene from Keosauqua, IA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Bad Drive-Belt, Follower wheel and two front slider pads.
Unplug the AC cord. Open dryer door and unscrew 4 small Phillips screws that hold the top panel to the front panel. Tilt up the top panel.
To remove the front panel: Look on the inside of the front panel, disconnect all the wire connections that go to/from the front panel, such as the light and door switch. Remove 2 screws that attach the top of front panel to the side panels using a 8mm or 5/16" wrench. Undo or loosen 2 Phillips screws at the bottom of the front panel, one at each bottom corner. Remove the front panel. Go to the back of the dryer. Remove the 8 screws holding the lower access panel (8mm or 5/16"). Remove the access panel. Also, remove the 2"x4" access plate in the center of the back panel (2 8mm/5/16"). Reach inside the small panel opening with a needle nose pliers and remove a Cir-clip and washer that holds the rear drum bearing shaft in place. Now you can remove the drum straight forward. Clean, clean, clean the insides. Replace the worn drive belt, follower wheel and front slider pads as needed. Reverse the procedure to reassemble. Plug in and test. Drink beer.
Parts Used:
Drive Belt
  • Joe R from BUELLTON, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Wrench set
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Only heating on 'high' setting
Per suggestion of "Parts Select", I replaced the "high limit thermostat"....very simple task on the dryer: 1 - unplug from power source; 2 - remove screws securing top to front (open door, screws located beneath lip of unit); 3 - tilt top up allowing access to everything; 4 - remove connections to 'thermostat' (note which wires go where); 5 - loosen screws securing thermostat to unit and remove thermostat; 6 - vacuum any and all lint while unit is apart; 7 - install new thermostat and put everything back together; 8 - test dryer to see if repairs worked!
Parts Used:
High Limit Thermostat
  • E J from S HAMILTON, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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When tub was turning it had a grinding sound.
First unplug the dryer from power. Now open the dryer door and remove the two phillips head screws that hold the top down. Then lift the top off and turn the dryer on it's back (this is not necessary but if you have the room it makes the job easier). Now remove the two hex head screws that hold the front on and remove the wires from the door switch. Now you can lift the front of the dryer off, door and all. This now allows you to replace the three (on this model) slide bearings and the felt. I also removed the belt and lifted the drum out and checked both the belt and the rear bearing. You can do it!
Parts Used:
Air Duct Felt Seal Drum Slide
  • Chuck from Cowiche, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Dryer Don't turn
I removed the 2 screws and lock assemblies from both sides on the back. Then i removed 4 screws (two from each side) on the control panel and lifted that up as i tipped the cover forward to disconnect the wires from the door switch. I found the wiring diagram inside the control panel cover, which included a belt routing diagram (very helpful, being the belt was laying in the bottom. I then removed 3 torx srews holding the drum to the bearing, and removed the drum. Let the fun begin! i proceded to put the belt onto the motor pulley and around the tensioner. i needed some help from my wife to set the drum back in as i held the belt up around it. once the drum was back in, i found the beld had fallen away from the tensioner. I lifted the front of the drum up just enough to get both arms below it and move the tensioner back to slip the belt over it correctly. With the new belt on i started to put the screws back in the drum. This got very frustrating, as you have to correctly line up all the holes again, while holding the drum in the correct angle to start the screws. this was the hardest part, not physically, but wears on a person's nerves quickly! Once all the screws were in and tight, i took a deep sigh of relief before i tipped the front cover up just enought to get the wires hooked back up for the door. I turned the unit on to verify the repair before re-assembly. Yep! works again, for well under $20.00! Thanks PartSelect!
Parts Used:
Drive Belt
  • Matthew from Alma, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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All Instructions for the DDC5000SBLAD
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