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Models > MHW2000AWW > Instructions

MHW2000AWW Maytag Washer Dryer Combo - Instructions

All Instructions for the MHW2000AWW
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Intermittent or no gas ignition, HSI ignightor working
Removed front of gas dryer and cleaned all lint out. Checked HSI, and cleaned flame sensor. Split (3 terminal) gas coil terminals were intermittent. Read about 700 ohms across outer two terminals, but center terminal to either outer terminal was open (Infiniti on meter) 2 terminal coil measured about 550 ohms. 3 terminal coil should read about 700 ohms across outer terminals, and about 1.5K ohms center to outer terminals. Unscrewed index cover plate and replaced coil, 2 terminal coil was okay. Reassembled and finished 12 loads of laundry no problems at all.
Parts Used:
M Series New Style Coil Kit
  • Steven from Sauk Village, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
43 of 50 people found this instruction helpful.
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Worn out lint filter.
Very easy with a tip from the video that was provided from Parts Select.
Thank You
Joseph Errico
Parts Used:
Lint Filter
  • JOSEPH from WARWICK, RI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
69 of 132 people found this instruction helpful.
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Replace bearings and seal on Maytag Neptune tub.
My repair (replacement of Maytag Neptune front load washing machine tub bearings) went well — knock on wood. The reason I took on the job somewhat confidently is I read online (probably from your site) the testimonial of someone who successfully did the same repair I faced. It is this persons sharing the recount of what it takes to do this job that gave me the motivation to take it on. For me it was around an eight hour job being my Neptune is a stackable (with the drier ontop). It has been a week now of operation with about 10 loads through the washing machine. It is sooo nice not listening to the previous worn bearing sound best described as a jet plane winding-up during taking off coming from the washer during its spin cycle. I pray the shaft seals stay snug. The job definitely was a major undertaking. Replacing the seal and bearing myself I saved probably saved $900.
Scott
Parts Used:
Lip Seal Kit
  • Scott from Redmond, OR
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
42 of 53 people found this instruction helpful.
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dryer would not dry clothes, no heat
I am a seventy year old recent widow, I have never repaired any appliance before. This was the first time I had ever seen the inside mechanisms of a dryer. I read the reviews on your site and followed the instructions of other do-it-yourselfers. However I could not locate the screws to remove the front of dryer. I would like to know if this dryer can be accessed through back of dryer, for future references. This is a 20 year old dryer, very well made, and I am reluctant to give it up. I think the job would have been much quicker and easier if the dryer front could be opened, as I would have also liked to check the main burner, valve, and belts, etc. for wear and if all was working efficently, as well as do a thorough cleaning. I did locate the igniter part through small door on bottom of dryer, I loosened the screw on igniter, unplugged small plug on wire harness and removed part. Ordered new igniter part and it arrived within less than three days, excellent service, as I live on the west coast. I replaced new igniter, turned on the gas, plugged in electrical cord, checked gas valve connection on back of dryer to make sure it was secure, turned on dryer and presto, heat, works just like new so far. A $25 part sure beats a $200 service repair or the cost of a new dryer.The repair job required about 45 minutes total time, most of that time spent trying to remove front of dryer. If a seventy year old woman beginner can do this, it should be a snap for most anyone else.
Parts Used:
Flat Style Igniter
  • Shelby from La Crescenta, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
36 of 39 people found this instruction helpful.
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Gas burner would not ignite
(I knew the gas coils were bad, since the gas ignitor would glow brightly as the burner attempted to ignite. So I knew everything except the gas valve was operating normally.)

Unplug the electrical cord to the dryer. Remove the front access panel. Remove the retainer clip for the gas coils (2 screws). Remove the coils and unplug the electrical connections. Connect the new coils to their respective electricl connections. Slide the nes coils back onto their respective posts on the gas valve. Replace the retainer clip, and 2 screws to hold it in place. (I then plugged the dryer back into the wall outlet to visually check the burner operation) Everything worked fine so I then replaced the front panel.
Parts Used:
M Series New Style Coil Kit
  • Jack from Conroe, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Wrench set
37 of 42 people found this instruction helpful.
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no heat in dryer
I removed front cover of dryer and found heating unit. I needed the detailed drawings from the PartSelect web site to help me find how to get the front cover off. It was easy after that changing out the sensors and reinstalling the heating unit.
Parts Used:
Heating Element - 240V
  • Eugene from McAdoo, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
38 of 46 people found this instruction helpful.
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loud noise from tub bearings on final spin cycle
use an online repair manual for your model, but in the manual it states that the tub bearings are not replaceable, if you are a skilled person capable and competent with fixing mechanical things you should be able to replace the bearings, don't forget to put in a new seal. the bearings can be found at grainger.com , have the old ones in hand for proper size as these bearings are only sold by dimension. This repair will take some time and patience.
Parts Used:
Bellow Lip Seal Kit
  • Joel from Rosemount, MN
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
37 of 43 people found this instruction helpful.
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Belt wore off and broke
Opened the back panel of the washing machine. Removed the old belt and wrote down the part number. Shopped online for a suitable replacement and found a perfect match at part select.com. I put in an order and it was delivered in a couple of days! I opened the back panel of the washing machinie again. This time I decided to also replace the isolators that came with the kit. For this, I had to unscrew the motor and gently tug it free. I placed it on the floor of the washing machine. I then replaced the 2 isolators as described in the kit, reinstalled the motor and put the screw back on. I then proceeded to place the belt on the motor and on to the wheel. This took couple of tries to get the grooves right. I then tested the washing machine on a rinse cycle and things looked good. Its been working fine so far.
Parts Used:
Drive Belt and Motor Isolator Kit
  • DANIEL from WEST CHESTER, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
38 of 46 people found this instruction helpful.
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The Lint Filter was ripped.
I put the new one in . Nothing to it.
Parts Used:
Lint Filter
  • Sandy from Ankeny, IA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
66 of 131 people found this instruction helpful.
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Squeaking noise when dryer was on! Very annoying!
If your dryer is squeaking it is most likely either the idler pulley or drum rollers. First I took apart the dryer to see which parts I would need. I checked the drum rollers by spinning them with my hand to see if they spun freely and also checked them to see if they were loose, they were okay. Then I checked the idler pulley and found my problem, it was hard to spin it so I figured the bearing was shot. I sprayed some lubricant on the bearing to help with the squeaking while I waited for my parts. It took about 30 minutes to diagnose my problem and put the dryer back together.
I took some advise from another story saying to get the whole idler arm, shaft and pulley assembly. It might have cost me a few bucks more, but I did not want to run into the same problem he did (the pulley bearing was fused to the shaft). It took me about 20 minutes to take apart the dryer, install the part, and put it back together. If you are pretty good with fixing things, you should have no problem doing this repair.
Parts Used:
Idler Pulley Shaft Washer Idler Arm and Shaft Dryer Idler Pulley Wheel & Bearing Idler Shaft Retaining Ring
  • Scott from Davie, FL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
33 of 35 people found this instruction helpful.
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Metal on Metal Squealing Noise
After taking the dryer apart, I found that one of the drum support rollers was barely hanging on the pin and was the main cause of the metal on metal squealing noise that became increasingly worse over a month's time.

I replaced both rollers, the idler pulley, and put on a new belt after giving the dryer a thorough cleaning.

It was a 100% success and fixed the problem making the dryer work and sound like brand new again.
Parts Used:
Dryer Idler Pulley Wheel & Bearing Multi Rib Belt - 91-5/8 Inches Drum Support Roller Kit
  • John from Bethlehem, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
33 of 36 people found this instruction helpful.
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very loud noise when washing and especially spinning
Pre-ordered the spinner support & seal kit, searched online and found a repair manual, disassembled machine according to the manual, removed snap ring outside of rear bearing, used hammer and drift punch to remove bearings, went to local bearing supply store and purchased 1-6206 2RSJEM and 1-6207 2RSJEM for a total of $43. Used needle scaler to remove the ~1/8th inch of scale from inside of the outer drum and outside of the inner drum and other parts encrusted with scale. Installed new bearings and the seals and new spinner and reassembled the rest of the washer. Now we can't hear it when it spins!
Parts Used:
Spinner Support and Seal Kit
  • Fritz from Wasilla, AK
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
33 of 36 people found this instruction helpful.
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Loud noise when in spin dry
This kit came with instructions. I followed them closely. The only thing I could add is clean the tub spindle with steelwool to remove any debris or rust. then wipe down spindle to remove all steelwool particles and follow instructions to reassamble.
Parts Used:
Outer Tub with Bearing Drive Belt and Motor Isolator Kit
  • Michael from Orland Park, IL
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
33 of 37 people found this instruction helpful.
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Water would continue to flow into Washer even after washing machine was off
The best way to access the water value was through the rear of the stackable washer/dryer by removing the back access panel (3 screws with nut driver). It was also necessary to remove the large back panel where you access the drive belt to get you hands up to the valve. It was a little tight accessing the valve unit from the back but definitely better then removing alot more to access through the front.

Once the back access panels are off you will see the blue water valve. it has (3) water hose connections and (5) electrical connections. Make sure to label each of the water hoses and electrical connections before removing them. The hoses simply are held on by hose clamps (use a screw driver) and the electrical connections just slide off the contact conductors. Real simple but again it is a bit tight working from the small access panel.

I marked all of the hose and electrical connections prior to removing anything. The removed all connections and slipped out the water valve. Simple reconnected water hoses and electrical connections replaced both access panels and all systems were a go.

Definitely a relatively easy fix for a do it yourself project. Part was only $70 (included shipping). Repair cost for the Maytag man was quoted at $450 for visit labor and parts.
Parts Used:
Washer Water Inlet Valve
  • Brian from Mount Airy, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
32 of 35 people found this instruction helpful.
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Dryer would light at start and then not light.
I used the trouble shooting part of this site and bought the radiant flame sensor and the high limit thermostat. Installation was very easy. The original problem still persisted and then purchased the temp. control thermostat, cycling thermostat and thermal fuse. These parts installed easily as well and the problem still existed.

While using the Multimeter to determine if the gas valve coils were getting voltage during the lighting process I moved the contacts on the two wire coil and noticed that the coil would activate sporadically. As it turned out the coil had a loose connection which would contact while cool and then lose contact when the coil warmed up.

This was a tricky issue to diagnose and am now waiting for a new coil to finish the repair.

I now have an almost complete set of spare parts for electrical issues and got them at a nice price. I will keep them in the event that I might need some of them in the future.

The repair would have been easy and very straight forward thanks to this website if the actual problem hadn't been the crazy heat related bad connection in the coil. Since the flame would light during startup the coils seemed to me to be good. Actually finding a weird issue is the sort of thing I find to be the fun part of repairing things.

Thanks Parts Select ! !

Gregg heagney
Parts Used:
High Limit Thermostat Dryer Radiant Flame Sensor
  • Gregg from Sedro Woolley, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
31 of 33 people found this instruction helpful.
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All Instructions for the MHW2000AWW
31 - 45 of 1278