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WGT3300SQ0 Whirlpool Washer Dryer Combo - Instructions

All Instructions for the WGT3300SQ0
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No heat to dry clothes
First I took the front of the dryer off then located the igniter. It only required removing two screws, removing old igniter, replacing with new igniter, and replacing the two screws.. While I was replacing the igniter I took the drum out and throughly cleaned the inside. Lucky me, I found 85 cents on the floor of the dryer. I am 65yrs old, married and mother of two.
This was easy to do and sure saved money. I reccommend others try to do repairs for themselves and using PartSelect was less expensive too.
Parts Used:
Igniter Kit
  • Karen from Pine Mtn. Club,, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
62 of 72 people found this instruction helpful.
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Washer would drain, agitate but not spin and was very noisy and would vibrate heavily
I first watched the youTube vidio on yhe PartSelect web site. After getting a visual of the repair, I decided to tackle the job with a better understanding and knew the repair was easy to purform. First I took the two screws out of the contrl panel on top of the washer, rolled the panel back to expose the clips that hold the metal cabinet to the back panel of the washer. After removing the cabinet I was ready to lay the washer on it's back and had a clear view of the pump, motor and clutch... I was able to easly identify these parts because I took time to watch the video. Using a flat head screwdriver I removed the clips that hold the pump to the motor... Without disconnecting the hoses connected to the pump I pushed the pump to the side and out of the way. This further exposed the motor. Using the flat head screwdriver, I removed the clips holding the motor to the transmission (they just snap off like they did on the pump). The motor was now ready to be removed from the transmission ( it just lifts off) before removing it I disconnected the power suply wire from the motor... Now the motor can be completely removed. I identified the drive couupler 1/2 was on the motor shaft the other 1/2 was on the transmission shaft.. On both halfs the splines were broken. I removed the old broken drive coupler. Since I already had the machine so far apart i figured i would replace the clutch also. Using a deep socket ratchet wit an extention I removed the agator... I then unbolted the transmission (only three bolts) I gentely pulled the transmission and shaft out of the bottom of the washer. This exposed the clutc assembly, I removed the clutc ( which wasn't bad or wore by the way) and replaced it.... I figured I had it and I was this far into the repair why not. After relpasingvthe clutch, I slid the shaft and transmission back into place tightened the bolts and that was done. I then slid/replaced the drive coupler... Placing one half on the motor shaft the other on the transmission shaft, placed the rubber bushing on the oneside of the plastic drive coupler. And mounted the motor back on the transmission utilizing the clips I took off earlier. Once the motor was in place I installed the waterpump fastened by the clips. Flipped yhe washer up, replaced the cabinet... Tightened down the the control panel and was ready to do some wash..: the washer runs perfect now and I saved myself about $700.00. It was allot easier than I thought it would be... Watching the youTube video is the secret to success. The washer is running like the day I bought it new... All for only 53.00. Hats off to everyone at PartsSelect for going above and beyond. Regards, ~ Michael
Parts Used:
Direct Drive Motor Coupling Clutch Assembly
  • Michael from Schuylkill Haen, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
59 of 63 people found this instruction helpful.
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Washing machine shook violently while on spin cycle
Disconnected the bracket screws that held the suspension springs in place - fed new springs into bracket and reattached. Local repairman told me that springs dont wear out, they break - wrong, they do lose their tension and thereby lose the ability to counterbalance the spinning load. Washing machine now spins like new - no wobble or shake.
Parts Used:
Suspension Spring Tub Spring
  • Tom from Bloomfield Hills, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable)
57 of 60 people found this instruction helpful.
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door kept coming open dryer shuts off
use screwdriver topry plastic out plyers to pull out metal latch put new parts in
Parts Used:
Door Catch Kit
  • RONALD from SALMON, ID
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
95 of 176 people found this instruction helpful.
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Very Loud Squeaking Noise
1) Disconnected power cord from wall. 2) Disconnected vent hose from back of dryer. 3)Removed dryer rear panel. 4)Disengaged tension spring on idle wheel arm. 5) Removed worn idle wheel. 6)Installed new Idler wheel assembly. 7) Vacuumed dust from rear of dryer (optional, recommended). 8) Reinstalled rear cover, vent hose and power cord. Easy repair 15-30
Parts Used:
Idler Pulley
  • GREGORY from Wilsonville, OR
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
60 of 71 people found this instruction helpful.
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The dryer would start to heat then the heat would stop
I changed out the cycling thermostat and the high limit thermostat. Mainly because that was what my research indicated was the problem. I then found some more information online that indicated the gas solenoid valves were bad. I ordered them from you and replaced them. The problem was fixed.

In order to replace the valves you need to remove the top panel. Two screws at the top of the front door assembly hold it on. Remove the screws, lift up on the front panel door assembly and move it to the side. The drum will rest in place. In the lower left corner, under the drum, you will see the solenoids. Two screws attach a plate that holds down the solenoids. Take the hold down plate off, disconnect the control wires attached to the solenoids and lift out the solenoid/control valves. To assemble everything, work backwards to the start. Good Luck
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Theodore from Riverside, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Wrench set
56 of 66 people found this instruction helpful.
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dryer would get hot for a while, then quit heating
After reading about other people with this same problem I took a chance that this would be what was wrong with my dryer.I took off the front cover of the dryer by removing two screws. I located the faulty coils and simply plugged in the 2 new coils Tah-dah Probably coud have been done without even removing the front panel, but since it was off I vacuumed out the lint ( actually my husband did all of the above, but I tell a better tale than he does and I diagnosed the problem and ordered theparts)
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Sharon from Houston, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
54 of 66 people found this instruction helpful.
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The washer wouldn't spin or agitate.
Frist I disconnected the water lines and power cord. Then I leaned the washer back against the wall. Removed the 2 pump retainers and then the pump. Next removed the 2 screws from the motor retainers and pulled off the retainers and motor. Then removed the 3 bolts from the Gear case. Then removed the cap from the top of the agitator with a flat screw driver. Then removed the bolt from the top of the gear shaft. and removed the auger and agitator assembly. Then removed the gear case from the washer. Next removed the slip ring and then the clutch from the top of the gear case. Next removed the 1/4" screws from cover of gear case and removed the cover. Found the top gear bad. Ordered the new gear and pinion kit. Couldn't find any part #'s to match what PartSelect had. Ordered the gear that they should that fit most washers. The pics they had up looked the same as the one that was bad. Had the new gear in 3 days put it back together and it still wouldn't work right. Took it apart again and looked at it and found a small clip on the bottom side of the gear was upside down. Fliped it over put the gear back in and ran the washer with the gear case out and it worked. Put it back together again. And learned a good lesson always watch how you take things apart for when it's time to put it back together!
Parts Used:
Gearcase
  • david from Monroe, MI
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
49 of 52 people found this instruction helpful.
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Washer wouldn't spin or agitate. Made louder-than-usual noise during those cycles.
1. Read many other repair stories for similar symptoms. PartSelect Forum was an excellent resource.

2. Posted my problem on PartSelect Forum and awaited reply. Read replies, and followed provided link to step-by-step guide for the procedure. PartSelect forum moderators were excellent advisors!

3. Performed the first half of the procedure to get to the diagnosed root cause. In some of the stories I had read, people had turned the washer on its back or tilted it up to get at the area from underneath. I am so glad I followed the conventional instructions, and left the washer standing and simply removed the cabinet. It was surprisingly easy. There's a reason why it was designed that way. I am also glad that I chose to remove the pump from the motor. While it is true that you don't *have* to remove the pump from the motor to get at the coupling...it hardly seems to make sense to remove the hoses instead. Removing the pump was incredibly easy, and by doing so, I never had to break any "wet" connections, and not one drop of water spilled over the course of the entire repair. (Even though I forgot to shut the water supply valves before I got started. Ooops! At least I remembered to unplug the power cord.)

4. But despite the open valves, the galoshes came into play not for their ability to repel water, but for their value as an electric insulator. I wrapped the galoshes around the handle of a long screwdriver when I discharged the motor's capacitor. :)

5. Ordered parts. Washed clothes in sink. Waited. Washed more clothes in sink. Waited some more. Washed more clothes in sink. Waited still more. Came very close to stopping payment to PartSelect because the very simple, commonly-requested part I ordered, which was supposedly in stock on the day I ordered it, didn't ship until the day it was supposed to arrive--even though I paid extra for expedited shipping. And I was never sent an e-mail to warn me that the parts were going to be delayed. And then to top it all off, rather than make up for some of the lost time caused by their own error, and ship it overnight, PartSelect chose to ship it 2nd day. All that good will generated by the excellent website completely evaporated by the failure to correctly complete the simple tasks that the business has needed to be good at since before computers were even invented. I will never use PartSelect again.

6. Prying the old coupler halves off of the motor and the washer took some effort, but was not overly difficult. I wound up removing the motor mounting plate in order to get better access to the half that was stuck on / needed to be attached to the drive train of the washing machine. Mounting plate was a breeze to remove and attach with a socket driver. I used one of those stubby flat-head screwdrivers to pry the old parts off. This was the one time where I thought it might have been easier to have the washing machine tilted up or on its back...but I muddled on through without even removing the bottom panel, and it wasn't too awkward. I used a large socket and a full-size hammer to not-so-gently tap the new parts into place. Putting all of the parts back together took a bit longer than it took to break them down, but it was easy. The instructions for putting the electronic control panel into test mode had been rolled up and taped to the cabinet inside the top panel. After I put the cabinet back on, I used those instructions to test all the cycles before fastening the top panel and testing the machine with an actual load. So far, so good...
Parts Used:
Direct Drive Motor Coupling
  • Paul from Boonton, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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I smelled smoke and then it quit working
First unplug the electrical chord and disconnect the water supply after you have turned it off. Drain all water you can by putting the drain hose into a bucket or water container lower then the drain hose. Remove the two screws at base of the front panel. Then go to the back side of the machine remove the two screws at the top of the back panel, this allow you to remove the top switch panel. Remove the two screws at the bottom outside corners of the back panel and then you can lift the panel up and away from the base. I leaned the back against my dryer because I did not have a helper. Go to the front of the machine, lift the lid and grasp with one hand the machine's sheet metal lift and pull it off the base. There are two metal clips attaching the pump to the motor. The pump slides off and I did not have to remove the hoses. Unclip the electrical connectors from the motor and capacitor. The motor is mounted with two clips with a screw secure it in place. Unscrew and unclip and the motor should slide out. Be sure to inspect the direct drive coupler, the parts not too expensive. I had replaced mine just 4 months ago so I was good to go. Reverse the procedure and you should be in business.
Parts Used:
2-Speed Drive Motor - 60Hz 120V
  • Paul from Lakewood, WA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
43 of 48 people found this instruction helpful.
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Intermittent or no gas ignition, HSI ignightor working
Removed front of gas dryer and cleaned all lint out. Checked HSI, and cleaned flame sensor. Split (3 terminal) gas coil terminals were intermittent. Read about 700 ohms across outer two terminals, but center terminal to either outer terminal was open (Infiniti on meter) 2 terminal coil measured about 550 ohms. 3 terminal coil should read about 700 ohms across outer terminals, and about 1.5K ohms center to outer terminals. Unscrewed index cover plate and replaced coil, 2 terminal coil was okay. Reassembled and finished 12 loads of laundry no problems at all.
Parts Used:
M Series New Style Coil Kit
  • Steven from Sauk Village, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
43 of 48 people found this instruction helpful.
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Unbalanced and walk across the floor on spin cycle
Part Select provided the problem determination information and the video on how to install the replacement parts. I ran into one problem, I could not remove the lock nut to remove the inter and outer tub. I should have bought the special wrench for $14, no local DYI or hardware store had the wrench. So, after examination I used a large screwdriver and wood block to lift the tubs up just enough to remove the old pads and replace with the new. The old pads showed only a wear, but was enough to spin the tubs off balance. The new tabs made the washing machine work like new. New washer $500, repair man $150, parts and information from Part Select $20 bucks, priceless.
Parts Used:
Tub Wear Pads - Package of 3 Suspension Pads - Package of 3
  • James M from Elkhart, IN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
44 of 54 people found this instruction helpful.
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Gas Flame Would Drop Out
First it was a process of alimination to find out why it was dropping out. After the problem was found it was just a matter of replacing the holding coil on the gas valve. Thank you fred kenney sr
Parts Used:
Dryer Radiant Flame Sensor
  • FRED from BRIELLE, NJ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
47 of 64 people found this instruction helpful.
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machine was out of balance
Removed the washing machine from the wall and found a broken spring on the floor. Began disassembling the unit before accessing your sight. (Later I viewed your video of the more simple dis assembly).Used your parts breakdown to identify the 6 parts I needed (3 springs and 3 retainers),and ordered them. They arrived on time and as per the video, installed them with ease and reassembled the unit. My wife is very happy. Thank you, Rusty
Parts Used:
Suspension Spring Suspension Spring Retainer
  • RUSSELL from SOUTHOLD, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
45 of 59 people found this instruction helpful.
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Spin cycle stopped working
Farly easy repair, once I figured out the problem. The clutch assebly plastic part broke (over 15 yrs old), which is the part that engages the drum for the spin cycle. Following the very helpful diagram on Part Select, I removed the agitator cap and bolt from inside the agitator assembly, and pulled the assembly out of the drum. Then I put the washer on its side and removed the three bolts and two hose claps that hold the motor assembly. I pulled the motor assembly along with the drive shaft out to access the clutch/brake assembly area, removed the broken plastic drive piece and re-assembled.
Parts Used:
Clutch Lining Kit
  • Brent from Highlands Ranch, CO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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All Instructions for the WGT3300SQ0
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