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MGDE201YW1 Maytag Dryer - Instructions

All Instructions for the MGDE201YW1
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felt strip came off lint screen
ordered new lint screen, removed old screen, inserted new screen.
Parts Used:
Lint Filter
  • JEFFREY from FALL RIVER, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
221 of 273 people found this instruction helpful.
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catch mounted on door broke
The door had always opened with the wrong swing and it wasn't til I needed to repair this that I noticed you could change the swing. I changed the swing of the door and then noticed that the clip was included on both sides so i did not need to repair the catch. I still have the part so when it breaks again, I can just pop it in.
Parts Used:
Door Catch Kit
  • Paul from Mt. Pleasant, SC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
93 of 123 people found this instruction helpful.
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Rear tub seal failure
I removed the top cover and then the back cover, released the belt tensioner and removed the drive belt. Then slid the tub out of the unit and onto the back dack. Sanded the remnents of the old seal off. Wiped the tub lip with laquer thinner and applied the "fast" drying glue supplied with the kit. Installed the seal and re-assembled the unit...works fine
Parts Used:
Dryer Drum Seal with Adhesive
  • Jerry from Everett, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
66 of 84 people found this instruction helpful.
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No heat to dry clothes
First I took the front of the dryer off then located the igniter. It only required removing two screws, removing old igniter, replacing with new igniter, and replacing the two screws.. While I was replacing the igniter I took the drum out and throughly cleaned the inside. Lucky me, I found 85 cents on the floor of the dryer. I am 65yrs old, married and mother of two.
This was easy to do and sure saved money. I reccommend others try to do repairs for themselves and using PartSelect was less expensive too.
Parts Used:
Igniter Kit
  • Karen from Pine Mtn. Club,, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
62 of 72 people found this instruction helpful.
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Felt gasket on lint filter loose...
Found this site by googling, and it works! I searched lint filters and just ordered based on how it looked...LOL! Husband wasn't home, it looked pretty much like the one I had in my hand, so.... I ordered it. It is the perfect fit and seems to have a tighter gasket glued in all around the screen. Let's hope this one lasts longer than 6 months! Thank you Parts Select for being so fast!! Filter got here in less than 48 hrs.!
Parts Used:
Lint Filter
  • Catherine from Atascadero, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
60 of 70 people found this instruction helpful.
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Very Loud Squeaking Noise
1) Disconnected power cord from wall. 2) Disconnected vent hose from back of dryer. 3)Removed dryer rear panel. 4)Disengaged tension spring on idle wheel arm. 5) Removed worn idle wheel. 6)Installed new Idler wheel assembly. 7) Vacuumed dust from rear of dryer (optional, recommended). 8) Reinstalled rear cover, vent hose and power cord. Easy repair 15-30
Parts Used:
Idler Pulley
  • GREGORY from Wilsonville, OR
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
60 of 71 people found this instruction helpful.
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Our dryer started squealing and would then stop running.
After determining that the dryer motor was the issue I wrote down the part number and logged on to partselect.com.

I input the number into the search box and there was the exact motor I needed.

The price was fair and the delivery quick so I figured I would give yuo guys a shot and see how it goes.

The part showed up on time and as expected. It was well packed and most importantly - it was the CORRECT part.

I disassembled the dryer which involved removing the lint trap, pulling out the blower fan and removing the motor cover. The motor was held in with 2 metal screws and wiring harness.

I took the belt off of the tensioner and pulled out the old motor. The motor was mounted with 2 clips which snapped off with ease. Reassembly was a breeze since the motor fit perfectly- the entire transplant operation took all of about 35 minutes.

I crossed my fingers, turned on the gas, plugged it in and........SUCCESS!

Since the dryer was down for over a week the backlog of laundry was piled pretty high. This replacement motor would immediately be put to the test.

It has been 5 days of non-stop drying and no squeeks, no squeels and nothing but dry clothes!

Thanks to Part Select for getting everything right the first time. It made a potentially very bad experience turn out as good as I could have ever hoped.
Parts Used:
Drive Motor with Threaded Shaft - 120V 60Hz
  • Kelly from Aptos, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Wrench (Adjustable)
53 of 67 people found this instruction helpful.
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Gas Flame Would Drop Out
First it was a process of alimination to find out why it was dropping out. After the problem was found it was just a matter of replacing the holding coil on the gas valve. Thank you fred kenney sr
Parts Used:
Dryer Radiant Flame Sensor
  • FRED from BRIELLE, NJ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
47 of 64 people found this instruction helpful.
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Scratches in Surface
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.
Parts Used:
Touch-Up Paint - White
  • Michelle from Richardson, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
64 of 125 people found this instruction helpful.
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worn out part
The repair was fairly easy. The most timely part of the repair was removing the twelve screws from the back panel to expose the repair.
Parts Used:
Dryer Drum Support Roller Drum Support Shaft - Rear Shaft with Right Hand Threads WASHER Roller Support Tri-Ring
  • John from Tucson, AZ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers, Wrench (Adjustable)
41 of 60 people found this instruction helpful.
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TOb stopped turning after a week or so of high pitched "squeals" coming from inside the dryer.
I recommend you order the idler pulley as soon as you start to hear the unusual noise indicating metal against metal. Replace the idler pulley before it fails and possibly causes more damage to the drive system. Simply removed the power cord at the back of the dryer and then the multiple screws holding the back panel in place as well as the clip holding the exhaust vent in place. You may need to remove the top panel to access a few of these screws. A diagram of the belt routing is in the paperwork I found behind the front lower panel of the dryer. This too is easily removed with just a few screws.
Parts Used:
Idler Pulley
  • Robert from Princeton, WV
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
29 of 33 people found this instruction helpful.
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converting to LP gas
First I removed the front panel which allowed access to the burner assembly. Then I removed the gas connector and elbow from the back of the dryer. Then I removed 2 screws that hold burner assembly in place and 2 screws that hold an angle brace for the burner assembly. Had to loosen the screw that clamps around the gas pipe holding it in place clear in the back inside dryer housing. Unplugged all wiring connectors, then I removed the burner assembly and removed the 2 screws holding the burner tube to the valve. Remove the orifice and replaced with the proper size for LP gas. Then removed the blocking pin and replaced with one for LP gas. Then reassembled in reverse order. Actually pretty easy.
Parts Used:
LP GAS CON
  • Robert from Tenino, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Socket set, Wrench (Adjustable)
30 of 36 people found this instruction helpful.
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Unit would shut down in the middle of cycle and flash E1 trouble code
Had to remove the back of unit to access the area of subject part by removeing 12 to 14 screws also the gas line had to be removed. Two screws held the part in place. Unit now runs normal.Saved alot on repair costs!!!!!
Parts Used:
Thermostat, Internal-Bias
  • Jim from Tucson, AZ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
30 of 40 people found this instruction helpful.
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Dryer would not heat up.
I unplugged the dryer,removed the two small screws on the front of the dryer and pulled the bottom forward. The two wires connected to the door do not have to be removed. With an electrical tester using the Ohm setting I tested the Radiant sensor and the Gas Valve coils. The two terminal coil was DOA. The dryer can be operated with the front open as long as the door wires are connected. Symptons: The igniter would heat up and not release gas. My repair was successfull due to this awesome website and the super fast shipping service. AAAA++++
Parts Used:
Dryer Radiant Flame Sensor
  • Roger from Bonners Ferry, ID
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
26 of 29 people found this instruction helpful.
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no heat
the ignitor did not glow red checked thermal fuse by exhaust duct. fuse open replaced thermal fuse
Parts Used:
Igniter Kit
  • rex from streator, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Wrench (Adjustable)
28 of 36 people found this instruction helpful.
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All Instructions for the MGDE201YW1
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