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MGD6200KW2 Maytag Dryer - Instructions

All Instructions for the MGD6200KW2
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My dryer handle broke off when i opened it
My son got it in the mail for me and snapped it right back on.
Parts Used:
Dryer Door Handle - White
  • Kathy from CORNING, IA
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
12 of 15 people found this instruction helpful.
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When using the dryer the cycle would stop and display E1 as the reason
Unscrewed the bottom panelof the dryer and located the thermistor through the schematic for my machine. Removed the old one and put the new one in the same way. No more E1 problems and all cycles now complete themselves.
Parts Used:
Thermostat, Internal-Bias
  • Joyce from Holbrook, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
12 of 17 people found this instruction helpful.
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The handle to my dryer broke
Just popped it into place needing no tools at all. Took less than a minute.
Parts Used:
Dryer Door Handle - White
  • Elouise from ORLANDO, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
10 of 11 people found this instruction helpful.
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Had to convert from natural gas to propane
Well, here's the rub...in order to find out what part I needed to order, I needed to take the dryer apart to where the gas controls are, and there on a sticker was a part number for an LP conversion kit. But, in order to get to that gas valve unit, I fumbled about figuring out how to take this brand new dryer apart, since there were absolutely no instructions whatsoever in the owners manual. And once apart, and pretty much all apart, I wondered how it would be that the Maytag repair man would be so lonely, as he'd have plenty to do.
However, the kit had great instructions as to how to take it apart and change out the orifices.
Parts Used:
Liquid Propane Conversion Kit
  • Peter from The Rock, GA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
12 of 18 people found this instruction helpful.
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
10 of 12 people found this instruction helpful.
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LP gas conversion
Followed instructions, except to advoid sharp edges, and completed the job in under an hour.
Parts Used:
Liquid Propane Conversion Kit
  • Robert from Palmdale, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Socket set
11 of 15 people found this instruction helpful.
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
12 of 18 people found this instruction helpful.
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Old motor was making noise and tripping after a few minutes
I disassembled the dryer once to clean the motor and compartment. After reasembly, the problem persistes. I ordered the motor and the second diasasssembly was accomplished in 10 minutes and the entire job took 45 minutes and the dryer was running like new. Tip- Leave the motor secured while removing the blower fan.
Parts Used:
Drive Motor with Pulley
  • John from Midland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
10 of 13 people found this instruction helpful.
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Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
Parts Used:
Multi Rib Belt - 92-1/4"
  • Ronald from Oakdale, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
10 of 13 people found this instruction helpful.
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Humming noise then quit after pushing start. Drum would not turn manually.
Looking at the schematics, it wasn't clear exactly where the motor was located. I took off the rear panel thinking I could get to the motor through the blower. Realizing that was a no-go, I did some web searching and found that the lint screen chute had to be unscrewed, the top had to be lifted to gain access to the top 2 screws holding the front panel to to the main body. The barrel was then dropped and the rib belt removed from around it so I could set it aside. The clips were removed from the front and the back of the motor to gain access to the blower shaft. .The motor shaft is screwed into the blower shaft but it took me a while to figure out how to grab the blower shaft( made of hardened plastic?) with an adjustable wrench while torquing the end of the shaft with a (3/4"?) socket wrench. Access to the rear was rough, but getting the motor out an back in was easy. The spring tensioner for the belt was the next hurdle. With the s-curve facing outward and clipped to the base, the belt with the rib side wrapped around the barrel, the belt was slid between the roller and the tensioner bracket and wrapped around the motor drive rib side inward. I had to take the old motor to kind of prop up the barrel so I could at least see the tensioner and motor interface. I had to do a balance trick where I held the barrel up while centering it to the belt and the rear panel while ensuring the cloth seal was seated to the outside of the chamber. The front panel went on, and the front cloth seal was seated by spinning the barrel. The rest was just a matter of reversing the steps. Tons of lint/dust is probably what crashed this motor. Disassembling the front and the back allowed a thorough clean up - vacuuming and wipe down. Should go another 10 years/
Parts Used:
Multi Rib Belt - 92-1/4" Drive Motor with Pulley
  • Derek from Missouri City, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Socket set, Wrench (Adjustable), Wrench set
8 of 8 people found this instruction helpful.
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Replaced a broken pulley.
Half of my pulley was broken off so there were no wrench flats to take it off. I was able to remove it using Channel Locks and the 7/16 wrench shown in the video.

Hint: Use a one gallon ice cream bucket to hold up the drum while connecting the belt. It makes it much easier and gives you more clearance.
Parts Used:
Motor Pulley - 60 Hz.
  • Brian from IMLAY CITY, MI
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
9 of 11 people found this instruction helpful.
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dryer would not heat or turn off
removed front of dryer located igniter removed two screws disconnected wires then put new one in also replace thermal fuse and thermostat on back of dryer works great.
Parts Used:
Igniter Kit
  • michael from eldridge, IA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench (Adjustable)
9 of 12 people found this instruction helpful.
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No Heat
I suspected a faulty igniter and disconnected the cable to the igniter and measured the resistance of the igniter and found it to be 70 ohms then I checked the voltage at the same cable towards the power source and found it to be 25 volts ac which should be 120 volts ac. Next I checked the radiant flame sensor and found it to be open (it should be a closed circuit when cold). I removed the flame sensor (with the power off) using a small box wrench and found a broken lead. Replacing the flame sensor solved the problem.
Parts Used:
Dryer Radiant Flame Sensor
  • NICHOLAS from PARMA, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench set
9 of 12 people found this instruction helpful.
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dryer drum belt broke
I needed to remove the front lower cover, very easy as it is held on with clips only so I used a flat head screw driver to pop it off. I had to remove the lint filter and then there are two screws attaching the top cover of the dryer to the internal lint filter tray. The top of the dryer can then be opened front to back I again used the flat head screw driver to pop the top open as it has two clips at the front corners. It helps to have someone to hold it open or a rod of some type to keep it open. You can now lay the belt on the top of the drum and work it down the back side by pulling forward on the drum itself to seperate the drum from the seal that presses aginst the back side of the drum. I then went from the lower front to retrieve the belt now draped over the drum and pinched the belt to pass it through the tensioner and over the drive pulley. looking at it from the front the belt will come down the right side of the drum under the tensioner pulley around the drive pulley across the bottom of the drum and up the left side. The belt sits almost in the middle of the drum not against the back lip where there is a groove that might be confused as a place for the belt to ride that is where the seal sits then reverse the process to reattach the top to lint tunnel and reattach front cover and you are good to go . i would suggest vaccuming any old dust/ lint whlie everything is open as this reduces the chance for catching on fire I was supprised as to how much lint was loose inside the dryer cavity itself and our dryer is gas and the flame is an open flame.
Parts Used:
Multi Rib Belt - 92-1/4"
  • Paul from Athens, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
7 of 7 people found this instruction helpful.
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Dryer not Drying
Replaced both Coils. Purchased M Series coils much less expensive buying coils together instead of seperately. Problem solved.
Parts Used:
M Series New Style Coil Kit
  • Manuel from Jurupa Valley, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
8 of 10 people found this instruction helpful.
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All Instructions for the MGD6200KW2
61 - 75 of 787