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DE18CS Maytag Dryer - Instructions

All Instructions for the DE18CS
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Dryer made screetching, chirping noise then would stop running alltogether.
Turned off breaker, then unplugged it anyway. I need some room to attack this old dog! Pulled out of its hole beside the washer and went to work. Opps, don't forget the flexible vent, I broke it off about a foot from the dryer. Four screws on back, lower right to remove acccess panel. Next two screws under front panel, pull bottom out about a foot and it unclips at top. Read the 5 repair stories about replacing the motor as I took everything apart, all were helpful. Had to put motor in a vise to loosen set screw on pulley, lucky I had a 3/16 allen socket, that was the only hard part, unless you count getting screws out from under the freezer where I kicked them. Be careful. Still ended up with belt in v-groove on back part of drum (where it does NOT go) so had to reach in from front and pull it out about 4 or 5 inches. Things a quiet now and I am a hero around here. Thanks for the good help fellows.
Parts Used:
Tumbler and Motor Belt Drive Motor - 60Hz 115V Motor Clip Retaining Ring
  • Mark from Bethpage, TN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Blower noisy no air flow.
I did it the hard way from the back by removing the motor. The easy way is from the front. From the front there are 2 screws about 5 inches above the floor. Also, remove the 4 screws in the tumbler behind the lent filter. Swing out the front panel from the bottom and it will release at the top. Remove 2 screws on left and right side of the front tumbler cover. It will come out now and you can get to the blower wheel which in my case was just spinning on the motor shaft.
Parts Used:
Blower Wheel with Clamp
  • Gary from Liberty, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Blower fan came loose and broke
No manual on this so had to remove about 12 screws to figger out disassembly,after locating the right ones[front]the job was easy.Remove front plate,remove drum bearing,remove blower front cover,remove snap ring,remove broken fan,clean fan shaft,slide new fan onto shaft[there is a flat in the bore of new fan]instal fan retainer on stub of fan,reinstal snap ring,reinstal the rest of the parts,test drive system[all sat]The part was exactly as ordered,thanks,Jim Thompson
Parts Used:
Blower Wheel with Clamp
  • jim from sierra vista, AZ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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replaced the lint filter
No big deal about replacing a lint filter , take the old one out and put the new one in.
Parts Used:
Lint Filter
  • michael from farmington, NH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Dryer tumbler belt broke.
I followed the videos on your website, but had to clean 30 years of dust and lint out in the process. Cleaning took the longest time.
Parts Used:
Tumbler and Motor Belt Idler Pulley Shaft Washer Idler Pulley Wheel Drum Support Roller Kit
  • Robert from Fort Worth, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
6 of 10 people found this instruction helpful.
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Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
Parts Used:
Idler Pulley Wheel
  • William from Winter Park, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
Parts Used:
Tumbler and Motor Belt Idler Spring
  • Francis from Half Moon Bay, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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Slide Was Worn Down To Bare Metal
Took the front off , removed front drum support, drilled out existing rivets, & replaced slides,riveted them in place,and re-assembled.
Parts Used:
Lint Filter Front Glide Kit
  • Bill from Frisco, TX
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
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drum support roller had come apst from bearing and was making a squealing noise when dryer was running
first i removed the screws holding back cover. Then I remeved nut from tumbler roller shaft. Then I slid shaft from roller .I removed roller then replaced with new one. Installed new shaft then replaced back cover. recieved parts from parts direct very promptly & they were the right parts the first time thanks very much
Parts Used:
Roller Shaft Drum Support Roller Kit
  • David from Calvert City, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Wrench set
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Loud noises, primarily a shrill shreik
From the noise level and info on this site, I assumed I needed to replace the drum rollers. I ordered two, along with the Roller Shaft, and a replacement belt (I assumed that would eventually need to be replaced so why not now).
No need for me to repeat the excellent reviews/instructions already on this site. Basically, it was an easy job that took about 2 hours, mostly because I took the time to clean every nook and cranny I could find.
Once I assembled it back up, the shriek was gone but the rumble noise was still there. I now realize that the blower wheel must have a worn out d-hole that mates with the motor shaft. So, I will have to order that part, get it installed and I am confident that I will have a "new" machine once that is in place.
Parts Used:
Tumbler and Motor Belt Roller Shaft Drum Support Roller Kit
  • Robert from Glastonbury, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Wrench (Adjustable)
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Dryer door would not stay closed
1. Popped out old latch from dryer with a screw driver and pressed in new latch with fingers. Did not need to replace the part that is in the door. Very simple repair.
2. Lint filter was worn out and needed replacing.
Parts Used:
Lint Filter Door Latch Kit
  • William from Fullerton, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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Replaced door switch
Door switch was very easy to replace as it simply snaps in for the outside and you just clip on the two control wires that already have clips on them.
Parts Used:
Door Switch Kit
  • Joseph from Colts Neck, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Noisy Dryer operation and eventually no air movement through dryer
Every two to three years, the blower wheel gets chewed out in the center where it attaches to the motor shaft. I have learned the sound of it starting to rattle so I know to order a new blower before the air stops moving altogether. Replacing it is very easy if you have tiny sockets or nut drivers and a pair of snap ring pliers.

When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
Parts Used:
Blower Wheel with Clamp
  • Russell from ELK GROVE, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
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old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
Parts Used:
Tumbler and Motor Belt Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm Idler Arm Screw Sleeve
  • William from ORANGEBURG, SC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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All Instructions for the DE18CS
61 - 75 of 788