Models > SG9900 > Instructions

SG9900 Maytag Washer Dryer Combo - Instructions

All Instructions for the SG9900
16 - 30 of 1495
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Clothes would come out of the spin cycle still wet
First found out where the belts were by tipping the machine backwards and saw that the belts were intact but extremely loose. Ordered two belts (Drive and Pump) . Re-tipped the machine and in less than three minutes, had installed the new belts. I re-hooked the hoses to the back and the machine operated as if new.
Parts Used:
Belt Kit Belt Kit
  • William from Cary, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
128 of 140 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer belt broke
I have a 15 year old Maytag dryer that finally broke its belt.

First I unplugged the dryer from the outlet, and then I removed the access plate in the back of the dry by removing the four screws. Once I removed the plate, it was quickly obvious that the belt had broken, as bits of belt were all over the interior of the dryer.

I removed the front panel of the dryer (where the main door is located) by removing the two retaining screws at the bottom of the panel. After removing the screws, I was able to swing the entire front assembly up and remove the panel. The door sensor is attached to the front panel by two wires; I simply pulled the two wires from the door sensor, which allowed me to completely remove the front panel from the dryer.

I removed four screws on either side of the dryer which attached the front tumbler assembly to the dryer frame. The tumbler assembly also has the lint screen attached to it as well. Removal of the lint screen allowed me greater access to the internals of the dryer. I took the opportunity to use my Shopvac to clean out the accumulated 15 years of dirt and lint from inside the dryer.

Once the front tumbler assembly was removed, the main dryer tumbler came out easily. I removed the tumbler from the dryer and inspected it for damage. I also did more cleaning inside the dryer with my Shopvac. Removal of the tumbler is required for installing the new belt.

I wrapped the new belt around the tumbler and reinserted the tumbler back inside the drier. I reinstalled the front tumbler assembly, but I didn't tighten the four screws until I was sure the main tumbler was seated correctly on both the rear and front tumbler assemblies. Only then did I tighten the four screws.

I then went to the back access panel on the dryer and threaded the belt around the dryer motor rotor and belt tensioning roller. The new belt twisted a few times in the process, so I manually rolled the tumbler to straighten out the belt.

Once I was confident the belt was seated properly around the tumbler and motor rotor, I replaced the front dryer panel loosely. I also reconnected the two wire door sensor and then plugged in the dryer. I purposely left the back access panel off, so I could observe the motor and belt while the dry was running. I turned the dryer to a non-heat setting (i.e. air fluff) and started the dryer. I observed the rotation of the belt for about 2 minutes to insure it was rolling properly. Next, I set the dryer to a heated setting and ran it again for 2 minutes to be sure all the heating elements were working. It is good to check both the rotation of the belt and the heat elements prior reinstalling the back access panel. There is nothing worse than putting the dryer back together only to discover the belt is improperly tensioned/seated or the dryer heater elements are no longer working.

I secured the dryer front panel using the two screws. I reattached the back access panel with the four screws. Finally, I reconnected the dryer hose.

Dryer is running like new and haven't had any further problems.
Parts Used:
Tumbler and Motor Belt
  • Matthew from Carrollton, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
113 of 115 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Extended drying time. Some but not enough heat. Burner would light for 15-18 seconds at first then shut off for 1-3 minutes then light for 3-6 seconds and repeat for the length of the cycle.
Determining the problem was the hardest part. With multiple parts (coils,thermostats...)possibly causing similar symptoms, I narrowed it down to the two coil valves.
Un plug the dryer. Remove two screws at the base of the front panel. Turn the front panel 180 degrees to avoid disconnecting the door switch. Gas valve with coils on top are on the right in front. Remove two screws in bracket holding coils, disconnect the wires, replace with new coils and reconnect wires. One coil has 2 terminals the other has 3 no chance of crossing the wires. I used an offset/right angle screw driver for one of the bracket screws due to close proximity to the drum. A stubby phillips head will work. You can check the burner operation with the front panel off as long as the door switch is still attached. Swing the front panel around and lift back into place securing with the two screws. Dryer works fine now.
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Matthew from Lake Worth, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
120 of 138 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
No spin. Pump working. Smell of burning rubber.
I determined that the spin bearing was bad and decided to replace the brake too. Placed the machine on its side and then removed the rubber cap, v-belt, screw, drive lug and pulley. Then used a chain-vise grip to turn the brake off with the aid of a 3 foot long pipe extender for leverage. Blocked up the tub to align the transmission and installed the new spin bearing, brake, pulley and drive lug. Adjusted the drive lug position to contact the ccw motion of the pulley at the point when I could just feel the brake pressure. Installed the screw and rubber cap. Replaced the drive belts. Tested and all works. Halleluah!
Parts Used:
Rear Bearing Brake Assembly BEARING, BRAKE ROTOR
  • John from Spring Valley, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
129 of 174 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Belt worn and blower wheel loose.
I noticed a rattling noise coming from the dryer. I disassembled the dryer to troubleshoot. I assumed the rollers were bad, but I discovered that the blower wheel was loose on the motor shaft. The rollers were fine. I also discovered the belt was worn.

I ordered a new blower wheel and belt. Replacement was as described elsewhere.

I couldn't get to the screws on the front panel because my screwdriver was too long. So I put a pressure treated 2x4 under the front dryer legs to elevate it. I used pressure treated lumber because that's what was in the garage. Untreated wood would also work.

After removing the front panel screws, the bottom of the front panel needs to be tilted away from the dryer. At about 20-30 degrees of tilt, the front panel will suddenly drop away from the top.

Rotate the front panel to your left so that the wires don't get stretched. It isn't necessary to unplug the wires. But after touching the wires and getting shocked, now is a good time to unplug the dryer. In fact, it would have been better to unplug the dryer before you start any work on it.

Remove the front bulkhead and lint filter housing as a unit. 4 screws hold it to the dryer.

Remove the screws holding the faceplate of the wheel assembly, and remove the faceplate.

Next remove the spring clip from the blower wheel shaft. Then remove the circlip using a circlip plier. The wheel will now slip off the motor shaft.

Put the new wheel on the shaft, making sure to align the flat part of the shaft with the flat part on the wheel. Install the circlip and spring clip.

Replace the faceplate, Note that the perimeter of the face plate goes inside a groove. Install the screws.

Replacing the belt has been covered before, so I'll leave it at that. Just make sure that the belt goes on the proper side of the belt guard.

Install the front bulkhead-lint filter housing. Make sure the lint filter housing lines up with the blower wheel housing and goes inside the felt.

Install the front panel. Make sure the felt doesn't get pinched by the drum.

The first time I disassembled the dryer, it took about 1.5 hours. The second time was only about 45 minutes. The third and subsequent times were even quicker. Practice makes perfect.
Parts Used:
Tumbler and Motor Belt Blower Wheel with Clamp
  • David from Germantown, TN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
123 of 194 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Alarming rattling/rumbling noise
I told my wife, "it's working fine. Let's just wait until it breaks, and I'll fix it." She said the noise is intolerable and if I didn't fix it, she'd "call someone to come and look at it."

The forums all suggested that noise during operation is due to worn out components that are involved with turning the tumbler. So I ordered a bunch of parts from Partselect.com and set to work. I replaced the belt, the belt idler wheel, and both of the tumbler support wheels.

I reinstalled the tumbler, plugged the dryer in, and started it up. Damn, the same noise as before. Wait! The tumbler isn't turning. In my haste to see if the noise was gone, I'd forgotten to rethread the belt. Analysis: noise unchanged but tumbler not rotating. Conclusion: the hateful noise has nothing to do with any of the components involved in turning the tumbler.

Looking and listening more closely, I determined that the noise was coming from the blower, the plastic squirrel-cage like assembly attached to the other end of the motor shaft. It seems to be rattling on the shaft, causing the noise. I remove it, clean off a couple decades of matted-on lint, and reinstall it. No change.

I do not have a replacement blower, so I remove the blower from the shaft, clean up the shaft with alcohol, then put a piece of plastic electrical tape part way around the shaft, effectively increasing its OD by a few thousandths of an inch. I reinstall the blower, put everything back together again, and start it up. No noise -- nothing but a low purring hum! Good enough for me, for as long as it lasts. When my improvised patch fails, I'll order a new blower and install that.

It's good that I was so stupid as to forget to reinstall the belt before I started the dryer the first time. Since the noise was still there, I was forced to re-examine my assumption that the noise was being caused by a worn-out tumbler-turning component. If i HAD installed the belt the first time, I'm sure I would have continued with the incorrect assumption that the noise problem was related to the tumbler.

My time and money weren't wasted, I don't think. The various wheels and the belt were over 16 years old and due for replacement anyhow.
Parts Used:
Idler Pulley Wheel Drum Support Roller Kit
  • Wayne from Minneapolis, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
90 of 95 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Switch sticking in on position
FIRST unplug dryer from electrical source, CAUTION, the top of this dryer does not open with clips, do not pry on top to open! On the front of the dryer look under the lower panel, and find two screws, one on the left side, and one on the right, remove these screws, and pull slightly down on panel to remove. Behind this panel find two screws holding the door panel, one on the left, and one on the right, remove the left, and support the door panel while removing the right side. Gently pull the bottom of door panel outward, and the clips on top of door panel will unhinge from top, carefully rotate left side of door panel to floor, and note the wire connections on switch, and orientation of switch, then unplug wires, and move door panel to a comfortable working positon. Door must be open to remove switch, then depress the two plastic retaining keepers on each side of switch, and push switch through toward door. Replace with new switch, reconnect the wires, and reassymble in reverse order. Remember, door assymbly must be inserted in dryer top at an angle, and then bottom rotated downward, and bottom panel nylon guildes inserted into door panel bottom.
Parts Used:
Door Switch Kit
  • Don from Jacksonville, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
99 of 133 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer would only heat cycle once
I removed the two screws holding the front panel to expose the lower works and verified the heating cycle failure. After a check of the vent system, checking the sensors for continuity and coils for resistance, I retired to the 'net for support. Accepting the general consensus that the most frequent, common and likely failure to be the coils, I rechecked them with the meter and found the two pronged coil to have significantly more resistance than the three prong coil. That was enough evidence to point to the coils. While I waited for the part to arrive, I replace the vent ducting. When the parts arrived I removed the two Phillips screws holding the coils, removed the old ones, installed the new ones, replaced the bracket, put the front cover back on and in less then ten minutes clothes where drying.
Parts Used:
M Series New Style Coil Kit
  • Robert from Seattle, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
80 of 89 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
damaged filter
replace it
Parts Used:
Lint Filter
  • Jaime from Miami, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
72 of 72 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Lint filter ripped
I took out the old lint filter...and slipped the new one in. Pefect fit.
Parts Used:
Lint Filter
  • Joni from Auberry, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
100 of 163 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Loud rumbling at startup, periodic rumbling during drying, rumbling after motor stopped
After removing more bolts and screws than I needed to, here's how to replace the blower wheel on the stacked washer/dryer Maytag SG1000.

Turn off the power.

Remove the two screws on the access panel, which is the canted panel just below the dryer door, and remove the panel.

Remove the two screws at the top of the dryer door. These screws are on top of the dryer facing downward, and unless you're Yao Ming, you won't see them without a stepstool. You can then lift up the door and swing it out from the bottom.

There are two wires attached to the door which you should disconnect. You can set the door aside without disconnecting any other wires.

Next, remove the lint filter and the housing assembly it fits into. First, disconnect the ground wire connected to the upper-left corner of the housing, then remove 4 hex-screws accessed from inside the dryer tumbler.

You should take this opportunity to thoroughly remove lint from inside the housing.

The blower housing is now accessible. Remove the screws on the periphery of the blower housing cover (a.k.a. faceplate), and remove the cover.

The blower wheel is held in place by an external retaining ring and by a blower clamp. The replacement blower wheel came with a new blower clamp, and that clamp can be manipulated with a regular pair of pliers. I went out and bought a pair of snap ring pliers to deal with the retaining ring.

After removing the retaining ring and then taking off the blower clamp, I removed the old wheel. The new wheel was a little tough to put on, but after reading the story of the people who used a hammer to break their wheel, I just pushed on it until it popped on. I used my pliers to install the new clamp, then re-installed the retaining ring and the blower housing cover.

Reinstall the lint duct housing, making sure housing duct centers into the blower seal (looks like a felt circle). Reconnect the ground wire.

While you're inside the tumbler, at the front end of the tumbler just below the door there is a black plastic sensor with two metal bars on it called an automatic dry sensor. Fabric softener can coat the metal bars and cause the sensor to not function. Lightly sand the metal bars to remove any buildup.

Reconnect the wires to the dryer door. Reinstall the door by tilting the bottom in first, guiding the clips on the bottom of the door into the slots they fit in, then push the top of the door into position. Reinstall the screws at the top.

Reinstall the access door.

Turn the power back on! Done!
Parts Used:
Blower Wheel with Clamp
  • Ed from Long Beach, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
93 of 155 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
For several years the washer has moaned and groaned while filling, and filled slower than when new. It seemed to be associated with the inlet water valves. Then, it began to leak water from time to time, with the frequency and amount increasing.
I thought I had only a water valve problem - both the noise and leak seemed to come from the water valve assembly - but I had two. After replaced the water valve (a job which was easy to do as the assembly was easily accessed from the rear of the machine) the moaning stopped but I was surprised to discover that I had a stream of water pouring from under the machine.

I pulled the front panel (two phillips head screws needed to be removed) and raised opened the top assembly after removing two hex screws. (The diagram on PartSelect.com was helpful in understanding what I had to deal with).

I observed the fill action, and found that the water was leaking from the slots in the fill nozzle sleeve, in the water injector hose line. (The new inlet water valves had increased the pressure at the fill nozzle and increased the leak from that point which I had not suspected to be the source of the leaking water).

The basic problem was that the rubber valve sleeve had shrunk in length and was no longer flexible, allowing water to come out of the sleeve slots. I ordered an injector nozzle and valve and installed them in the original sleeve bracket in just a few minutes (two clamps had to be loosened, and the hose sections pulled back to insert the valve and nozzle assembly). (I had also ordered a replacement bracket just in case the old one might break, but it was not the correct part and the old one was fine.)

I checked for leaks and closed up the machine. Problems solved! It is now both quiet and leak-free.

(Moral, open the machine and check the nozzle for leaks - even if you suspect only the water valve assembly. The nozzle valve is located above the water valve and its leaks drop onto the water valve, making it look like the water valve assembly is the source of the leak.)
Parts Used:
Rubber Injector Valve Plastic Injector Nozzle
  • David from Macungie, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
64 of 69 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The belts were not staying tight enough to agitate properly.
Firstly, remove ac power from washer!
After removing the front panel of the washer (two philips screws), I loosened and removed the plastic motor cover and removed three hex head screws holding the motor. Have someone help you tilt the washer so you can remove the belts by "rolling" them off of the pullies (pump pully and motor pully). What I did was use a chemical degreaser to clean the motor base metal channel where the nylon sliders reside. After doing that and letting it dry, I removed the two old
springs. I ended up reinstalling the old springs because they were not stretched and I installed a new spring (total three) on the right side of the mount. A stiff metal rod with a hook on the end will help you install the springs. Squirt some of the included silicone lubricant on both sides of the motor mount channel and exercise the lube. Reinstall the motor and plastic cover over top of motor. Clean hands and clean belts while you have them out, reinstall belts and front cover and you're finished. My wife said it never ran better!
Parts Used:
Glide and Spring Kit
  • dominic from weirton, WV
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
64 of 69 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The dryer heated up for a few minutes and then cooled down.
1 Unplug power.
2. Remove the front of the unit by removing the two screws at the bottom of the front panel. Front dryer panel will swing out from the bottom and then the clips will release the top of the panel, careful not to disconnect the dryer door switch. ( can be unplugged to remove the front panel out of the way.)
3. Looking inside the unit on the right side you will see the gas value. On top of the gas unit you will see two small coils the coil closest to the burner has two leads on it. Remove the two screws to get to the coils, remove the medal plate, remove the connector then lift off the secondary coil. Replace and test. You can test unit with the front panel off. (be careful). If no heat, check that the Flat Style igniter is glowing. (ohm out both coils) before ordering parts. Intermittent heat problems. I replaced the secondary coil, it did ohm out o:k but it had swollen and was very tight on the shaft.
Parts Used:
M Series New Style Coil Kit
  • James from Limington, ME
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
65 of 73 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Washer wouldn't spin
My washer stopped spinning, even though I could hear the motor running. I did some research and found out there was two belts, opened mine up and it was broken. I replaced the belt in five minutes, start to finish. Now it's running like new.
Parts Used:
Belt Kit
  • Ben from Truro, AL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
81 of 133 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the SG9900
16 - 30 of 1495