Models > SG1000 > Instructions

SG1000 Maytag Washer Dryer Combo - Instructions

All Instructions for the SG1000
46 - 60 of 1474
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
belt was slipping
The job went fast an well
Parts Used:
Belt Kit Belt Kit
  • ROBERT from MORGAN CITY, LA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
38 of 50 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The dryer drive belt broke. The dryer wouldn't tumble nor blow heated air.
The repair itself was pretty easy. Though I had figured out what needed to be done on my own while I waited for the belt to arrive via Fed Ex, the belt arrived with instructions that described the plan I had already figured and if I hadn't known what I was doing, the instructions would have been a great help.

STEP ONE, UNPLUG THE UNIT (and/or shut off the gas supply), CAREFULLY. Then, I took the front of the unit off by removing the 2 screws on the front panel near the bottom of the unit and disconnected the wiring that shuts the unit off when the door is opened. Set the front door panel aside. Then I removed the front of the tumbler retainer along with the exhaust duct and lint screen assembly by removing 4 screws that affixed the reatiner frame to the rest of the outer cabinet. Set this aside as well. Remove the entire tumbler unit. Set aside. Remove 4 screws on the back of the unit that hold the tensioner and motor access panel and remove it. Set it aside. At this point, I vacuumed every bit of lint and debris from the snapped belt out of the enitre unit, lubricated/greased all moving parts, cleaned off the friction bearing surfaces, and collected loose change ($1.35).

When the belt arrived, I unwrapped it, and placed the smooth side to the tumbler and rubber banded the slack off to the bottom right side (sort of the 4:30 position as you put the tumbler back into the unit). I carefully jimmied the tumbler back into the unit BEING CAREFUL not to pinch the groved belt between the tumbler and any other parts inside the cabinet. I replaced the tumbler retainer and screwed the 4 bolts back into place. I spun the tumbler over near the tensioner assembly (so I could see the slack through the access panel hole in the back) and removed the rubber band. I threaded the belt through the tensioner and over the drive pulley and rotated the tumbler clockwise to align the drive train of the belt. I plugged the 2 wires back into the switch on the inside of the door panel and then I replaced it on the front of the unit and screwed the 2 screws back in at the bottom front of the panel. I plugged the unit back in and tested opperation. It worked great! I unplugged the unit again (I'm not finished yet). I then replaced the access panel on the back of the unit and screwed the 4 screws back in. I moved the unit back against the wall and plugged it back in. Done! The dryer is less noisey now and more efficient most likely b/c I cleaned all the lint out of the thing! Thanks for the prompt shipment of the belt!! I'll get a few more years out of this dryer before spending $700 on a new one!!! Thanks again!
Parts Used:
Tumbler and Motor Belt
  • Lee from Royal Oak, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
35 of 41 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Leaky injector nozzle
Water was leaking at the injector nozzle during the fill cycle. I could not visually see any damage to the existing part, but, ordered replacement parts, anyway. The new parts arrived and looked EXACTLY like the old ones. Clearly, the new parts would leak, too. So, I cut a three-inch length of 3/4-inch OD pipe and spliced the two hoses together, completely eliminating the troublesome parts. The washer works fine and does not leak. And, it fills much faster, now. I still have no clue as to the purpose of the injector nozzle nor do I know why it did NOT leak for 30 years.
Parts Used:
Rubber Injector Valve Plastic Injector Nozzle
  • Michael from Lindstrom, MN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
34 of 39 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Washer motor start windings burned up
The motor was easy to replace: unplug the wiring harness, slip off the belts, release the tension springs from the motor carriage with needle-nose pliers, and then unbolt the motor carriage with socket set and remove from the washer. Remove the pulley from the old motor with allen wrench and transfer the carriage to the new motor. Reverse operation for everything and you are back in business. The hardest part was the far back screw holding the carriage, a wobble extension helped.
Parts Used:
Drive Motor - One Speed - 120V
  • Eric from Seabeck, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
36 of 47 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
washer was leaking onto the floor
First I disconnected the power and turned off the water supply. Then removed the front panel of the washer by removing the two phillips head screws from the lower left and right front of the machine. I then removed the four hex screws at the corners of the top of the machine using a socket set. The two screws in the front of the top come out through the inside and the two screws in the back come out through the access holes in the top. Next I disconnected the bleach/softener tube from the upper end to allow the lid to be raised. Then I swung the right hand side of the lid up fully and rested it on the left hand side support using the braces provided on the lid and resting the weight on the attached support string. The injector valve, inector nozzle and injector bracket are right on top on the left hand side. The bracket is taken out by removing one hex screw on the underside of the bracket. The valve and nozzle are removed by loosening the hex screw on the hose clamp, To replace, first assemble the rubber sleeve and plastic injector. The large end of the plastic injector should fit squarely into the slot of the rubber sleeve. To insert this assembly back into the molded end of the injector hose I used a small amout of laundry detergent to lubricate the large end of the rubber sleeve. This allowed the part to slide in without displacing the rubber sleeve from the plastic injector nozzle. Now, I replaced the associated parts (lid and front panel) and turned the water on and plugged the washer back in. No more leak. Thanks to PartSelect.com my repair was easy. I did not need to replace the injector sleeve bracket but purchased the new one in case I broke the old one during the repair.
Parts Used:
Injector Sleeve Bracket - Side Mounting Rubber Injector Valve Plastic Injector Nozzle
  • Richard from Ashley Falls, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
32 of 36 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer would light at start and then not light.
I used the trouble shooting part of this site and bought the radiant flame sensor and the high limit thermostat. Installation was very easy. The original problem still persisted and then purchased the temp. control thermostat, cycling thermostat and thermal fuse. These parts installed easily as well and the problem still existed.

While using the Multimeter to determine if the gas valve coils were getting voltage during the lighting process I moved the contacts on the two wire coil and noticed that the coil would activate sporadically. As it turned out the coil had a loose connection which would contact while cool and then lose contact when the coil warmed up.

This was a tricky issue to diagnose and am now waiting for a new coil to finish the repair.

I now have an almost complete set of spare parts for electrical issues and got them at a nice price. I will keep them in the event that I might need some of them in the future.

The repair would have been easy and very straight forward thanks to this website if the actual problem hadn't been the crazy heat related bad connection in the coil. Since the flame would light during startup the coils seemed to me to be good. Actually finding a weird issue is the sort of thing I find to be the fun part of repairing things.

Thanks Parts Select ! !

Gregg heagney
Parts Used:
High Limit Thermostat Dryer Radiant Flame Sensor
  • Gregg from Sedro Woolley, WA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
31 of 33 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer would start and heat, but after 1st cycle the burner would not fire and a buzzing sound was coming from the gas valve solenoid area. Igniter and other functions worked fine.
Removed front of dryer, unplugged each coil to determine where buzzing was coming from.....determined it was the boosting coil....ordered part and replaced. Dryer works great....we think it had be going bad over time because drying times have noticeable decreased.
Parts Used:
M Series New Style Coil Kit
  • David from Bedford, IN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
31 of 36 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Drum rubbing metal to metal on front support
1. Unplugged dryer, removed front (2 phillips screws near bottom) set aside with wires attached
2. Removed front support (4 hex head screws)
3. Drilled out pop-rivets, discarded old glides (why didn't Maytag use rollers?)
4. Riveted new glides in place.
5. (Oops!) trimmed cork pads, smeared with glue, shoved under glides, held down until firm
6. Removed drum (pushed belt back to groove, pulled drum off rollers, lifted belt off drum, worked drum out) Left belt on pulley and tension wheel as pattern when I replace it.
7. Scraped old gasket felt off back chassis and front support
8a. Folded gasket lengthwise and glued into front support channel with fold on outside diameter. It was too short.
8b. (Oops! Why didn't this come with instructions?) Pulled it out, reversed it and replaced it with fold to inside diameter. It fit. Glued ends together.
9. Glued other felt gasket into back chassis. (Good ventilation needed here!)
10. Replaced rollers. (This did have instructions, despite being easy. I didn't use any grease. Experience as a locksmith says don't lube anything that isn't sealed from dust. I also vacuumed out 15 years of dust.)
11. Replaced belt. (The old one looked fine, but I was advised to do the belt and rollers along with the glides.) The grooves touch the drive pulley, the flat goes around the tensioner, and the belt exiting to the left seems like it will rub the pulley, but it doesn't once the drum is installed.
12. Turn the drum around (Nice, it's symmetrical!) and work it back in.
13. Lift the belt around the drum edge (I used bull clips to hold it in place.)
14. Check the belt on the pulleys, move the drum in more, take off clips, move the belt to the groove.
15. put the drum on the rollers, lift the belt out of the groove, and spin the drum a little while watching the pulleys to check it.
16. Screw the front support back in place.
17. Screwed the front on and plugged it in.
It works!
Parts Used:
Tumbler and Motor Belt Tumbler Seal Front Glide Kit Drum Support Roller Kit
  • Jim from Los Angeles, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
32 of 39 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
dryer would not continuously heat, and took several cycles to dry clothes. The flame would ignite and heat the dryer at first, but then would ignite and go out quickly for the rest of the cycle. I tried the thermostats first with no luck.
I first ordered the coils from a different web site and they sent the wrong ones. The job would have been much eaiser if i had just returned and ordered from here. Instead i cut wires and tried the others but since they were worng, it did not work. I didn't label the wires so it was a puzzle to put it back together. Once i had the wires connected properly it was a simple fix. You just open the top and take the front pannel off, remove the drum and it is right there at the bottom. Two screws take the cover off of the coils and they slide off the gas valve. Slide the new ones on and replace the cover. Put the front pannel back on, close the top and its good to go. I first tried the highlimit thermostat, and termostat with no luck. The flame would light when it was cold, but once warmed up, the flame would ignite and immediatly go out. The coils did the trick.
Parts Used:
M Series New Style Coil Kit
  • Ryan from Livonia, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
30 of 34 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
My dryer only heats up at the beginning of cycle so my clothes will not dry.
I remove the front control panel and to get to the bottom front dryer door off. Using my volt meter i checked all the sensors and thermal. I surf the internet for hint and some one mention to replace the coil since some time you could have one goes out and the other working still. After i replaced the coil kit it works like a champ.
Parts Used:
M Series New Style Coil Kit
  • Monique from Mission Viejo, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
31 of 38 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Clothes would not dry on automatic setting
1: (Automatic Dry Sensor) Removed 2 screws holding front panel, then removed 2 screws holding automatic dry sensor to inside of tub. Disconnected 2 wires from under side of sensor and removed sensor. Placed new sensor in place, reconnected wires, and reinstalled 2 screws. Finally, put cover in position and secured with 2 screws.

2: (Pilot Lamp) Removed 2 screws at bottom of washer front panel. Pulled bottom of front panel forward and removed from unit. Pulled lamp socket from clip, replaced bulb, and replaced lamp socket in clip. Reattached front cover.
Parts Used:
Automatic Dry Sensor with Mounting Screws Cylinder Light Bulb
  • George from Smithfield, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
33 of 46 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Broken contact on high limit thermostat - dryer no start
First I unplugged the dryer! Then unscrewed the two screws at the bottom of the front door. To remove the front door, swing the bottom up about 30 degrees until the two triangular hooks at the top of the door release. Then release the two wires going to the door switch from their harness so as to gain more slack to move the door out of the way. The switch was secured by 2 hex head sheet metal screws1/4inch in diameter. I used a small right angle socket wrench to get these loose. I only had to remove the front screw completely to be able to take the switch out for exchange purposes. Once this was done, reverse the process and plug it in! (BTW, the electrical schematic for this dryer is up under the top console)
Parts Used:
High Limit Thermostat (Limit: 200-30)
  • Nova from Hudson, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set
30 of 38 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
The water didn't pump out during the spin cycle
I took out the two screws in the bottom front panel of the washer, and rotated the front panel from the bottom away from the machine until the top or the panel was released from the machine frame. I then tilted the washer back to get access to the bottom of the machine. The pump pulley had split in half, and the bottom half fell off the drive motor shaft. The only problem I had was breaking free the set screw that holds the pulley to the drive motor shaft. I used a long arm Allen wrench and an adjustable "Cresent" wrench to apply enough force to break the set screw loose. Iclamped the upper transmission belts tightly to keep the motor shaft from turning while I loosened the set screw.
Parts Used:
Motor Pulley
  • Robert from Menomonee Falls, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Wrench (Adjustable)
30 of 38 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Clamp rusted through permitting upper & lower tub to separate
Clamp was already in multiple pieces so easy to get off.

Got clamp from partselect.com in 1 day which was great.

Removed two PH screws from front cover then pulled bottom of front cover outward and down to remove.

Caution for those doing this: take a piece of 220 or 240 grit paper and sand all the edges of the clamp. Trying to put it on without doing so will result in countless paper cuts in hands.

Before putting new clamp on be sure to use either some soap or silicon lube on the rubber V seal between upper and lover tub.

Also need to put some 1/4" to 3/8" spacers at three equally spaced places beneath the upper tub and the lower tub. If this isn't done the upper tub will drop down too far inside the lower tub and the inner lower tub, when it starts to spin, will rub on the underside of the upper tub = cause the main drive belt to smoke and tub to "freeze up"

Spacers I used were simply 3 pieces of multi strand sheathed electrical wire 3/8" so that I could bend them down at an angle and put them out once clamp was in place. Wire pieces need to be about 4-5" long.

Assemble one bolt in clamp and thread around tub in CCW direction.

Position one bolt of the clamp in right rear corner. this is important so that when tub goes out of balance, there's clearance for the clamp bolts and they don't contact the cabinet.

Make sure before threading clamp arount tub that the screw that will end up in the front left corner has a hex head on it so that you can apply some clamping "muscle" with a socket wrench.

I had trouble getting the front left screw inserted in the clamp (its only 2" long) so I used a 3" bolt to make the preliminary connection to pull the clamp semi tight. I planned ahead and got a light wire coat hanger to use as a "tie-tie" in the event that I had to remove the 3" slotted screw to revert back to the 2" hex head screw. Luckily when I removed the 3" screw I was able to quickly pop the 2" hex head back in and tighten completely.

Before putting front cover on, do one load with front cover off to make sure that upper and lower/inner tub don't rub each other.

If ok, turn power back off and put front cover back on.

Note: Would advised ordering the rubber V-seal if you are ordreing the clamp. If you buy the seal there are four bolts in the lid that let you lift the lid to work on the tub, clamp and seal MUCH more easily. Sticky part is getting water fill tube in top left rear disconnected so that new rubber v-seal can slide over tub.

Note also that in order to get to front left lid bolt that single bolt holding diaphram onto front left upright must be removed so as the let diaphram assembly drop away to access front left lid bolt. The two bolts in the rear can be accessed from the top very easily. Also need to disconnect the bleach fill tube in order to lift the lid (right side lifts up to vertical position)
Parts Used:
Outer Tub Clamp Seal
  • George from Fort Myers Beach, FL
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Socket set, Wrench (Adjustable), Wrench set
27 of 31 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer would dry for 5-10 minuets then no heat
I tested the dryer coils and found that they were getting a voltage but would not open the gas valve. Coils were not bad but weak. After they warmed up they would not open the gas valve. It took 10 min to repace both coils and the heat sensor.
Parts Used:
Dryer Radiant Flame Sensor M Series New Style Coil Kit
  • Richard from Jerome, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers, Socket set
35 of 55 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the SG1000
46 - 60 of 1474