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FWT449GFS0 Frigidaire Washer - Instructions

All Instructions for the FWT449GFS0
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Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Set aside time (6-8 hours), not rocket science, but long
Clear a work space, set up bins for parts, there are a lot of them, so upon removal, put all parts in same place (motor bolts in same box as motor, etc), use a digital camera to capture where everything goes.
Remove back, remove front lower access panel. Remove all plumbing from tug. Remove belt and large pulley from back (tap gently with mallet around perimeter to remove). Unhook motor wire connector, cut the zip tie. Remove the motor (4 bolts). Separate the front seal, remove the shock absorbers (use a deep socket to push in plastic tabs). Now the fun part, carefully tilt the washer back to the floor (2 people, it is heavy), while supporting the tub, to keep it from over swaying (I cut a 2x4 to size, put it between the tub and the lips of the side walls to keep it in place).
You should now be able to remove the springs (leverage them out with old screw driver), clear all parts from the tub. You can then lift the washer housing from the tub vertically. You should then be able to access the tub clearly. Remove the counter weights, set aside carefully, they are fragile. Remove the bolts holding the tub together.
Tap out the tub.
Reverse the process to put back together. Careful not to over tighten the bolts on counter weights or motor.
Parts Used:
Inner Tub with Spider Arm and Shaft
  • David from Austin, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench set
18 of 27 people found this instruction helpful.
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H2O leaking on final spin
drum vane had a hole in it replaced it using phillips screwdriver removed one screw ,pulled drum vane towards the door then pulled up replaced it reversing the procedure. It actually seemed to fix my leak during spin cycle
Parts Used:
Drum Vane
  • judd from jax, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
14 of 16 people found this instruction helpful.
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Drained but would not spin
The hardest part was figuring out how to get the lid off. You simply remove two screws from the back of the lid and jerk and slide the lid towards the back of the machine. Take out the screws that hold the front panel on, tilt the front out and access the lock/switch assembly and replace.
Parts Used:
Front Load Washer Door Lock and Switch Assembly
  • Gregory from Louisville, KY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
15 of 19 people found this instruction helpful.
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Cracked vane in washer
Removed (1) philips screw in toward back of vane (closest to rear of drum), pulled the vane forward to remove it, slid the new one in place, replaced the screw, and was done in less than two minutes. Piece of cake.
Parts Used:
Drum Vane
  • William from Juliette, GA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
15 of 21 people found this instruction helpful.
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Noise During Spin Cycle
Using a cordless drill and driver bit I removed the back cover, bottom front cover and top. I then removed the rubber bellowed hose connecting the soap dispenser to the rubber boot in front. This one was tricky to reinstall because the fastener for the hose is twisted steel wire that needs to be undone when reinstalling. It slid off easily enough but would not slide back on easily. There is a second small bellowed hose that connects the dispenser to the outer drum casing. This needs to be removed as well. It comes off easily and went back on easily. I used a one sided razor to cut the glue dots connecting the front boot to the washer door frame. After that I removed the belt from the motor and drum pulley by hand and then removed the motor mounting bolts using a ratchet and socket. This went smoothly. I now propped up the drum using 4x4 cutoff blocks to take the weight off the springs and shocks. I then removed to the lower upper plastic pins that hold the shock onto the plastic spin drum casing. I used a wooded block and a hammer to tap the pins out. Be sure to push in the lock on the tapered end of pin shaft. The second pin was a little more difficult to remove and required quite a bit of tapping to push it all the way through. I tried adjusting the weight on the shocks several times to make it easier to come out. The pin was slightly damaged by the time I got it out from hitting it. It went back in OK so I don't think the damage will cause any problems. Next I got someone to help lift the drum to release the weight on the springs and removed then from the top end. You need to remove the spring clamps that hold the spring down at the top end. I used a wrench to remove the bolt that holds the pullet on the drum shaft. The pulley was easy to pry off shaft by placing two flat screw drivers between the shaft and the bearing casing and twisting the screw drivers. Once the pulley was removed I turned the spin drum casing upside down and supported the outer casing with two stacks of 4x4 cutoff blocks. This would allow the stainless steel drum to be supported above the floor and drop freely as the shaft worked it way out of the bearing casing. Getting the drum shaft out of the outer housing bearing was the most difficult part of this whole process. The shaft was rusty and therefore did not easily slide through the two bearing casings. Before hitting the drum shaft to remove it from the bearing casing I put the washer and bolt back on the shaft to protect the shaft from hammer/mallet damage. I tried a mallet but it only moved the shaft part way and then it wouldn't slide further. I then used a 1/2" steel pipe cutoff as a punch seated around the pulley bolt to alloy me to use a hammer to beat the shaft out of the bearing casing. It required a tremendous amount of force to move the shaft. Once the shaft was removed from the old drum casing I spent some time cleaning the back of the stainless steel drum including using emery cloth to remove the rust from the shaft and polish it the best I could. Be sure not to damage the brass bushing that the rubber bearing seal rides on to prevent water leakage. Once the drum and shaft were cleaned up the reassembly process when smoothly I simply reassembled the washer in the reverse order or the disassembly. The shaft went into the new bearings snugly which I was pleased to see since the snug fit meant that the water would be sealed in and the drum would spin true. The hardest part was reattaching the large bellowed hose onto the soap dispenser because it require undoing the twisted steel wire clamp and getting it back together in a very tight space. I use a combination of a flat screw driving and a needle nose pliers to wrestle it back together. The finished job resulted in a very quiet smoothly operating washer which we expect will give us another 5 years of service.
Parts Used:
Rear Outer Tub Assembly
  • Bernie from Point Roberts, WA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
13 of 15 people found this instruction helpful.
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door assembely had a snapped piece of plastic in unit.
I released the door gasket and unscrewed the unit .Labeled the connections. then reconnected reattached, then put gasket back on. Worked like a charm!
Parts Used:
Front Load Washer Door Lock and Switch Assembly
  • DANIEL from STRATFORD, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
12 of 14 people found this instruction helpful.
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Pump leaked
First I turned off the water. Since the pump is at the front of the machine,it was easy to get too. I then removed the hoses by squeezing the hose clamps with pliers. I removed the electrical plug and then removed the 3 screws holding the pump to the base. I changed orientation of the outlets per instructions,which was very easy. Installation of the new pump was performed in reverse. I had difficulty getting one of the hose clamps back on and changed it to a screw clamp. I turned the water on,ran the machine and checked for leaks. Partselect saved me several hundred dollars in repair costs.
Parts Used:
Remote Style Pump with Motor
  • Robert from Roswell, GA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Socket set
12 of 14 people found this instruction helpful.
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Broken Timer Knob
Knob treasds onto machine shaft. Grab remaining part of broken assy with pliers and spin loose (left). Spin new assy on to the machine. Very easy repair. Quick service from Partselect.com
Parts Used:
Timer Knob Assembly
  • David from San Pedro, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers
11 of 11 people found this instruction helpful.
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Stainless tub in front loader broke 2 out of 3 spider arms
Removed entire tub assembly, replaced bearings and seal in rear outer tub assembly, had spider arms welded by aluminum welder. alot of work ,saved 150.00 on parts by replacing bearings, savings untold hundreds by doing it myself instead of replare man.. BIG JOB. But just plug away and it goes rather smoothly.
Parts Used:
O-Ring/Gasket
  • Ed from International Falls, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
13 of 18 people found this instruction helpful.
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Falling apart!
It started out with the tub not draining. No problem, has happened before. Remove bottom panel, take boot off of extractor motor, clear out book & check impeller for obstructions. Noticed belot was off. Got new belt. Belt would not stay on, bearings shot. Bearings are pressed into rear outer tub shell. Must remove pulley to get tubs apart. Good luck! Pulley was corroded onto shaft of inner tub. Used various tools, finally ended up grabbing hammer and beating it. Screwed up threads, broke pulley, but got it apart. Re-tapped threads, ordered new pulley. Finally got everything together. Worked intermittantly. Thought it was motor going out. Ordered new motor. It was door switch. Done spending money, bypassed door sensor. Whew! We have clean clothes! Ended up costing about half the price of a new unit, but it basically IS a new unit! Plus I have a spare motor for when that finally goes out!
Parts Used:
Rear Outer Tub Assembly
  • Michael from El Cajon, CA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
12 of 16 people found this instruction helpful.
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Thumping vibration on spin cycle
Remove the front lower panel. Remove the 4 plastic pins mounting the shocks using 1/2 inch short socket to hold the detent down as per included instructions. All plastic pins were stuck in place so used needle nose pliers to pull or push out. Lube the pins with grease before reinstall to help them go through the new shocks. Use the included lock nuts to lock the four legs in place as low as possible. Start the washer and level each leg while running so you can tell if the vibration is going away. Tedious method but worked.
Parts Used:
Shock Absorber Kit
  • Kerry from Pasadena, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
11 of 13 people found this instruction helpful.
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Tub to pump hose leaking
From the front of the washer, I removed two sheet metal screws at the bottom of the access panel. The panel pulled off with a just a little effort due to the nylon inserts installed on either side of the panel that keep it in place. The tub-to-pump hose is located on the right hand side and easy to access. The hose includes a screw clamp and two tension retainer (?) clamps that need to be removed.Make sure to save them for the new hose! I used a phillips head screwdriver for the screw clamp and a pair of channel locks to remove the tension retainer clamps. The tension retainer clamps were easy to remove but tricky to put back on. There must be another tool used for them that I'm not familiar with. With just a little patience though, it's an easy enough repair for anyone to do.
Parts Used:
Tub-To-Pump Hose
  • Barbara from Los Angeles, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
11 of 13 people found this instruction helpful.
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Knob was broken from use
Very easy to replace the assembly. Just twist counterclockwise to unscrew and replace with new assembly. You can probably complete without any tools, but the pliers will give you some leverage if needed.
Parts Used:
Timer Knob Assembly
  • Brian from Woodridge, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers
10 of 11 people found this instruction helpful.
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Leak in pump seal & cracked drum veins (2)
Very easy - veins are held in with one screw, when removed just slide to front of the washer and lift out. Pump assembly is a remote unit complete with drive motor. Take 2 screws out of the water shield, then unplug power to the pump motor and the green ground wire. Slide a cloth under the machine at the area of the pump to catch the water when the hoses are removed. Remove the hose clamp from the rear of the pump and the clamp on the discharge hose. You may be able th remove the hoses now, but if not remove the two bolts that hold the pump to the washer base & then remove the hoses. When you have the pump out you have to change the mounting base to the new pump. Also you may have to rotate the new pump discharge side with the motor (instructions are included with the new pump) - mount new pump, attach hoses, clamps,wires and water cover. Install front door that was removed at the start - pump in in the front right corner after removing the access door in front.
Parts Used:
Drum Vane Remote Style Pump with Motor
  • Paul from Lewiston, ID
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Socket set
12 of 17 people found this instruction helpful.
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Washer would function for 2 to 3 minutes and then pause. "PAU" appearing on the display.
Apparently the faulty switch was causing the washer to think that the door was open which would pause the wash cycle. The temporary fix was to disconnect/reconnect the door lock/switch assembly, thereby resetting the switch. Eventually though, the switch had to be replaced. The repair was simple. Unplug washer from power. Remove the metal band and spring from around the perimeter of the door seal. (I had to use needle-nose pliers for this step). Loosen the rubber seal near the door latch area only. Remove old latch by unscrewing the two screws, and disconnect all wired connections. Reconnect wired connectors using the new part and screw back on to the washer using the two screws. Reseat the rubber door seal and hold in place using the metal ring and spring you removed in the first step. Plug washer back in to power. That's it.
Parts Used:
Front Load Washer Door Lock and Switch Assembly
  • Stephen from Amarillo, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
9 of 10 people found this instruction helpful.
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All Instructions for the FWT449GFS0
46 - 60 of 349