Models > SGR351HS0 > Instructions

SGR351HS0 Westinghouse Dryer - Instructions

All installation instructions for SGR351HS0 parts

These instructions have been submitted by other PartSelect customers and can help guide you through the dryer repair with useful information like difficulty of repair, length of repair, tools needed, and more.

All Instructions for the SGR351HS0
16-30 of 349
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Drying times continued to increase over several months until finally dryer wouldn't dry any more.

  • Customer: Francisco from Arvada CO
  • Difficulty: Easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Screw drivers
  • 15 of 17 people found this instruction helpful
I did not troubleshoot my gas dryer to find the exact part that needed to be replaced. Instead, I did some research and found that the ignition coils are an extremely common problem.

The top panel of my gas dryer is attached by two snap clips located in the front, about three inches in from each side. I slid a butter knife in the space between the top panel and the front panel to push the clips and release the top panel. Front panel is attached by two screws, one on each side. I removed the front panel to access the heating system on the bottom left of my dryer and immediately saw the two ignition coils with a metal cover on top of them. Removing the metal cover was a little difficult because the two screws holding it in place were stuck. Once the metal cover is off, the two coils simply slide out. On my dryer, the bigger coil had a metal sleeve inside the core. I kept it and used it with my replacement parts.

The most difficult part of the repair was figuring out how to take appart the dryer to access the heating system. Now, the ol' lady is bragging to her friends that I didn't just fix the dryer, but that i've actually made it better than when it was new ;-)

Had 2-seperate problems; 1st was a high pitch squeel, 2nd was the cover overheating

  • Customer: Gerald from Cumming GA
  • Difficulty: Easy
  • Time to Complete: 1- 2 hours
  • Tools Required: Nutdriver, Pliers, Screw drivers, Socket set, Wrench(Adjustable)
  • 20 of 34 people found this instruction helpful
The high pitch squeel was the result of a failing drum bearing. It was particularly evident when first turning on the dryer, but became softer as the dryer heated up. In order to replace the drum bearing, I removed the top panel and front door panel.

The top panel was easily taken off by removing 2-screws from the back edge of the panel, and sliding it back to release it from the front panel seam.

The front panel is more involved, but still relatively easy for your average "do-it-yourselfer". I removed the front door panel by first removing the control panel (4-screws; 2 on top and 2 from the back of the panel). I removed 2 cable assemblies from the control panel via connecters (different sizes so didn't need to mark) and 2-wires attached to the large control panel mode selector (I marked these 2-wires). I set aside the control panel. I removed the front door panel by taking off 6-screws (2 on top, 2 on the bottom, and the remaining 2 on the inside of the panel on either side of the drum). After removing these 6-screws, I carefully pulled the front door panel away from the front of the dryer, carefully releasing 4-alignment latches (2 on either side). The front door panel was still electrically attached to the machine so I had to disconnect a couple more wires. I carefully disconnected 2-wires from the door light assembly and 3 more wires from the door switch (I marked the 3-wires on the door switch). I set aside the front door panel.

From the back of the dryer, I removed the small motor access panel on the bottom left corner. This panel also provides access to the drum belt. I released the drum belt from the motor drive wheel by releasing spring tension at the tensioner. The belt can easily be disconnected from the motor drive wheel and tensioner assemblies.

Removal of the drum was now possible. With the front door panel removed, the front of the drum is maintained in place via a small plastic stop on the top crossmember. I removed this stop prior to removing the drum. With one hand, carefully grabbing the belt that is was loosely draped across the back of the drum, and the other hand holding the front lip of the drum, I provided a quick and forceful upward motion to the back of the drum in order to dislodge the drum shaft from the bearing housing assembly. Once this was accomplished, I simple pulled the drum out of the dryer housing via the front of the machine.

The drum bearing repair kit ordered came with the replacement ball bearing, bearing housing, drum shaft, high-temperature grease, and attaching hardware.

I replaced the drum shaft on the drum via the 4-screws accessed on the drum rear panel.

I removed the old bearing/bearing housing via the 2-screws holding it in place. I wasn't too concerned about loosing the small ball bearing as the kit provided me a new one. I generously applied some high-temperature grease to coat the interior lining of the new bearing housing. I also placed a dab on the back seat where the new ball bearing sits. This helped hold the bearing in place while reattaching it. I reinstalled the bearing housing to finish replacing the repair parts.

Reassembly of the drum is in the reverse order. I paid particular attention to making sure the new drum shaft properly seated with the new drum bearing housing.

After reinstalling the drum and while the front door panel was still off the dryer, it was easy to inspect the blower housing. I found the squirrel cage had broken loose from the molded nut that attaches it to the motor shaft. That would explain the heat problem; the heat was not being exhausted through the duct.

THE SQUIRREL CAGE IS REVERSE THREADED. I was unable to remove the nut from the motor shaft as the design encompasses a metal bushing molded into a plastic nut shaped form. The plastic would not hold up to the force I was applying trying to loosen the squirrel cage. So I ended up removing the entire motor and blower housing assembly from the base

no heat in the dryer

  • Customer: Joy from Lakeville MN
  • Difficulty: A Bit Difficult
  • Time to Complete: 15 - 30 mins
  • Tools Required: Screw drivers
  • 14 of 17 people found this instruction helpful
unplugged the dryer, discontected the sensor and unscrewed the bracket, replaced the new one and put the connectors back on, screwed the bracket back on and that was it. Very easy fix for a female who does not do much of these sort of repairs but learning.

No heat, but everything else works. Ran continuity tests on everything and found gas valve solenoid coils open.

  • Customer: Barry from Fremont CA
  • Difficulty: Really easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Screw drivers, Wrench set
  • 14 of 17 people found this instruction helpful
Just as others described in your forum, getting to the gas valve solenoid coils is relatively easy. Pop the top lid and lay it back, remove 2 inside screws that fasten the front cover and pull back off the snap clips and lift up and off. Remove 3 screws that hold the entire gas control assembly to the bottom of the dryer and remove. Unfasten 2 screws on the valve that lock the plate on top of the two coils, unplug the electrical spade lug connections and remove. Install the new coils and do everything in reverse. Easy as 1-2-3.

Drum would not turn

  • Customer: jeana from houston TX
  • Difficulty: Really easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Screw drivers
  • 13 of 15 people found this instruction helpful
remove the rear lower left vent cover to get access the belt tensioner and pulley. then pop the top section up with a flathead screwdriver in the front, freeing it from the popclips. Then remove two screws from the back side of the front section releasing the drum. loop the belt around the drum.

Motor shaft broke

  • Customer: Beverly from Blairsville GA
  • Difficulty: A Bit Difficult
  • Time to Complete: 30 - 60 mins
  • Tools Required: Socket set
  • 12 of 14 people found this instruction helpful
had to remove the belt and drum and then remove the motor and replace it...put the belt on and then the hard part was to get the drum in place without the belt coming off. New Motor works quieter than the old one did, so I assume the dryer came with a defective motor to begin with and then the shaft finally broke. It runs very quiet now, but never did before. Even a service man came when it was new but said that was normal. Now we know it was not....there was a problem from the start.

lint filter did not fit "squarely" into its place

  • Customer: Jeff from Bethalto IL
  • Difficulty: Easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 11 of 11 people found this instruction helpful
replaced old filter, only to find that the new one had the same issue. After closer examination, I determined the filter guide that screws into place, which I had removed earlier to clean lint out, did not hold the lint casing correctly. I removed and reinstalled the piece that has the metal moisture sensors, and replaced it, ensure both screws held the lint casing as it should. Now I have two lint filters that fit perfectly! So, if you ever remove the piece wtih the metal sensors, make sure that the lint casing is screwed in correctly when replacing.

DOOR LATCH & DOOR STRIKE BROKEN ON DRYER

  • Customer: Bruce from Seminole FL
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Pliers
  • 13 of 18 people found this instruction helpful
I REMOVED THE BROKEN DOOR LATCH & STRIKE WITH PLIERS. THEN I PUSHED THE NEW PARTS INTO PLACE

Drum making thumping noises, clothes getting caught behind drum.

  • Customer: Gerald from Baltimore MD
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers
  • 10 of 10 people found this instruction helpful
I've always been a "do it yourselfer". If I can fix it, I save money. I took the dryer apart by lifting the top up like car hood. Then I removed the front panel. The front drum glide snapped into place easily where the other one had broken off. The felt strip that you sent was much shorter than the one on the dryer, so once I used the wire wheel to remove the old glue, I cut off the section of the felt that was bad and replaced it with the new felt. The turns much quieter and clothing doesnt get caught behind the drum anymore.

the burner wouldn't ignite

  • Customer: Michael from Newbury Park CA
  • Difficulty: Easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 8 of 8 people found this instruction helpful
UNPLUG the appliance. After removing the top of the dryer the front is easily removed. To make life simple I disconnected the wire harrness at the quick disconnect and placed the door/front away from the workspace. I removed the bracket holding the coils in place and replaced the old with the new coils. replaced the front and top panels and pugged it in! Good as new!! I originally ordered the wrong part and PART'S SELCET.COM refunded my money no problem! I will bookmark this site and use it again.

My husband ruined the old latch by trying to shut the door too hard, and the old latch fell down into the inside of the dryer.

  • Customer: Michelle from Dallas TX
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 9 of 12 people found this instruction helpful
I took the new latch out of the package and snapped it into place. It took about 15 seconds, and that included the walk to the laundry room!

switch burnt out

  • Customer: paul from west keansburg NJ
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 7 of 7 people found this instruction helpful
first you had to take back top panel off remove wires from switch turn old switch to the right pull it out then connect wires to new switch put switch back in screw back panel back on very easy 10 minutes tops thank you

The dryer drum wouldnt turn

  • Customer: Kara from Beckly WV
  • Difficulty: Really easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers, Socket set
  • 8 of 11 people found this instruction helpful
Had to pretty much disassemble the entire dryer. The schematics on the web site made it a snap to do. One word of advice. I you have to replace the rear drum assembly, the drum has to come out the front of the dryer. Part select made this a very positive experience.

Dryer Knob inside piece broke

  • Customer: FELIPE from TULSA OK
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 6 of 6 people found this instruction helpful
Like the review of the guy who said "no story to tell. received knob and popped it on." I did not realize when I spoke to the Fridgedaire 1-800 number that I needed the model number; even though, I had the part number of the knob. When I came across your website, I entered the part number which was on the back of the knob and your website brought up the correct item I needed. I had seen the part on another website and your pricing was more than half off their price. Plus you shipped it directly to me two days later.

Thanks, fm

dryer drum squealing loudly!

  • Customer: john from waynesboro VA
  • Difficulty: A Bit Difficult
  • Time to Complete: 1- 2 hours
  • Tools Required: Pliers, Screw drivers, Socket set
  • 6 of 6 people found this instruction helpful
THIS UNIT IS A STACKABLE WASHER&DRYER,SO FIRST PULL UNIT AWAY FROM WALL ATLEAST 4 FOOT.UNPLUG POWER CORD,THEN TAKE10 DAGREE FRONT PANEL OFF THEN THE CONTROL PANEL OFF AND UNPLUG THE 5 CONNETORS IF YOUR UNIT HAS THAT MANY,THEN LAY PANEL ASSIDE.TAKE DRYER DOOR OFF,MAKES IT EASIER WHEN PUTTING IT ALL BACK TOGETHER.NOW TAKE FRONT PANEL OFF AND THE DRYER LENT TUBE,NOW JUST TAKE THE 3 CENTER PHILLIPS HEAD SCREWS OUT AND SLIDE DRUM OUT.PULL UPWARD ON WHAT THEY CALL THE SHAFT WHICH HELD DRUM ON.NOW THESE ARE THE PARTS YOU SHOULD ORDER.BELT,GROUNDING BALL CLIP,GROUNDING BALL,DRUM SUPPORT BEARING,BEARING BRACKET,AND MOST IMPORTANT PART IS THE SHAFT.THE SHAFT IS UR INSURANCE FOR THE WHOLE JOB.USE A GOOD GREASE LIKE WHITE LITHIUM GREASE AND COAT THE SHAFT END AND THE DRUM SUPPORT BEARING.THE GREASE WILL CUT DOWN ON FRICTION FOR A WHILE,AND RE ASSEMBLE THE WAY YOU TOOK APART.REMINDER GROUNDING BALL GOES BEHIND DRUM SUPPORT BEARING NOT IN FRONT.GOOD LUCK AND PLEASE VACCUM.
All Instructions for the SGR351HS0
16-30 of 349