Models > LSG7804AAE > Instructions

LSG7804AAE Maytag Washer Dryer Combo - Instructions

All Instructions for the LSG7804AAE
121 - 135 of 1470
Keep searches simple. Use keywords, e.g. "leaking", "pump", "broken" or "fit".
Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
12 of 18 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
washer would stop in mid cycle
Determined that the lid switch was not completing the circuit. I then removed the 3 wires from their posts along with the 1 screw and removed the bad switch. Then, in reverse order installed the new switch. The part was 1/3rd the cost of the part sold locally. I ordered the part at 3:15pm Monday afternoon and it arrived at 1:00pm Tuesday- the next day. UNBELEIVABLE SERVICE....!
Parts Used:
Lid Check Switch
  • Phil from Grand Rapids, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
11 of 15 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
filled with water, would not wash nor spin
After I replaced the timer, the washer still would not wash or spin. So my son replaced the lid check switch. It was hard to remove the screw, but he finally managed to remove it and easily replaced the switch. The washer works perfectly. We kept the timer installed (also easy to do by removing the old and replacing it with the new by just unplugging wires and I think one screw) because the old one had not worked properly for a few years when I had a similar problem which resolved, except it would only work in main cycle with soaking which was sufficient for me. This large capacity washer is in good shape and I hope will last at least another 5 - 10 years. ).
Parts Used:
Lid Check Switch
  • ELINOR A from MEDINA, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
10 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Smoking Washing Machine.
Well, I figured out a couple of things during this process. #1 The Washer was smoking. It had happened before (a sock got suck between the basket and the tub) so I assumed that happened again. I couldn't see anything in that space this time, so I dissasbemled the washer to see if any clothing was there. Relatively easy once finding the screws to remove the front panel. #2 What I found was a sock in the pump box. I disconnected the hoses and removed it, saw nothing between the basket and tub and ran it to see if problem corrected itself. It still was smoking. That is when I checked the belts, #3 first the pump belt, replaced it, very easy, just pulled the old one off, and wheeled the new one on. It still was smoking, #4 so I replaced the drive belt, very easy and the same as the pump belt. It still was smoking so I lubed the wheels for the belts, and #5 cleaned the residual rubber around the wheel from the old, fried, dry rotted drive belt. No more smoke!!! However #6 remember to leave space between the basket and the top of the tub, as when I put the washer back together the basket didn't spin. I removed the top and ran the spin cycle, it spun fine, reconnected and it didn't spin, the tub top was touching the basket, that's when I relized the top was on too tight. I reattached and left about 1/4 in of space and all is well now.
Parts Used:
Belt Kit
  • Matthew from Wilmington, DE
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
10 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
10 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer would not heat.
First I removed the front panel on the dryer. While the dyer was running, I noticed the igniter did not turn its normal amber color and ignite the gas supply. I then disconnected the wire to the igniter and removed the screw holding the igniter in place. Next I replaced the igniter, tightened the screw and reconnected the wire. Finally, I replaced the front panel. This is a relatively simple repair.
Parts Used:
Flat Style Igniter
  • William from Batavia, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
9 of 10 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Standing water in washer tub
Thinking the water pump was not doing its job in removing all of the water after the rinse cycle, I replaced the water pump.

1. Unplug washing machine.
2. Remove front cover (2 screws).
3. Pull belt and hoses off pump body (watch for water in drain hose!).
4. Remove 3 screws holding pump to bottom pan. 5. Reverse process with new pump.

This job is straighforward, and it helps to have 2 wood blocks to prop up the front of the washer.

Unfortunately, this didn't fix my problem. Actual cause of the water in the tub was a leaking inlet valve (solenoid assy).
Parts Used:
Drain Pump
  • James from Baton Rouge, LA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
9 of 10 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Washer did not drain.
Took front panel off. Ran machine. Pump is see-through. Could not see any "aeration" of the water in the pump and no water was coming out of drain hose. Disconnected electric. Disconnected hose from drum to pump(first emptied ALL water from drom)and drained in bucket. Disconnected drain hose from pump to drain and drained any water. Checked for obstructions in hoses. Removed pump. Checked belt (was fine after 14 years). Ordered new pump. Received the next day! Replaced pump and tighten belt. Connected hoses and test it. All OK. Replace panel and did laundry.
Parts Used:
Drain Pump
  • Basil from St. Charles, MO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Socket set
9 of 10 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Noise in dryer
How to disassemble the dryer has been covered in past repair stories. I will add a make shift repair that will get you up and running until you get your replacement blower wheel. We repair gas dryers for a living and this repair works and some machines are still running for two years. Remove the blower wheel. Cut a piece of plumber strap of similar sized metal to about 3/16" x 1/2". Hold it with vise grips and then heat it with a torch. When it is hot melt it into the hole in the blower wheel. This will give you a flat spot in the shaft hole that will keep the blower from spinning on the motor shaft. Some trial and error fitting is involved. If you do it carefully the blower wheel will fit very nicely and will not vibrate or make noise.
Parts Used:
Blower Wheel with Clamp
  • Joseph from Hampton bays, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
8 of 8 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Washer would fill but not continue the cycle
I looked at the common problems in the owners manual and one item was the lid was not closed or the lid switch was bad. I took off the control panel and there was a schematic inside. This showed 2 lid switches. When trying to see if one switch was closed as it should be, touching the multimeter to the contacts was enough to get the washer going. .
Parts Used:
Lid Check Switch
  • Paul from Cedar Falls, IA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
9 of 11 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
washer fills with water wont start
checked lid switch ,plunger stuck in the in position 1 amp fuse blown took switch apart it was full of green copper corrosion stopping plunger from moving correctly. replaced switch and fuse and wow washer works
Parts Used:
Lid Check Switch
  • JOHN from ERWIN, TN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
9 of 11 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Dryer did not turn off in auto-dry mode
Unplugged the dryer (electric), removed two screws at bottom of front panel and removed front panel. Pulled electrical clips from sensor lugs near center.front of drum exterior. Located sensor inside front of drum interior, removed screw at each end. Removed old sensor, placed new sensor in position, attached with screws. Installed electrical clips on lugs, closed front panel and secured with two screws. Plugged in the dryer and it worked!
Parts Used:
RECEPTACLE SENSOR GRO Automatic Dry Sensor with Mounting Screws
  • W. Dale from Newton, KS
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
11 of 17 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
tub leaked
followed instructions elsewhere here. Procedure went flawlessly
To undo the nut I used a 1 1/2 " long x 5/16 bolt to hammer on.

STILL LEAKS. Needed PS2347235 =Tub Bearing Kit . Going back in...
THe remainder concerns the bearing procedure:
The 3 bolts holding the outer tub to the legs have rectangular washers. Those are not totally flat, and are marked for outside, top ... so pay attention. It might make a difference.
Outer tub came off the rubber bushing. Took some pulling the bushing off the shaft, and removing the sleeve bearing was a challenge at first, it would not move on the transmission shaft. Soaked with wd40 overnight. Drove it off with cold chisel (driving upward). For re-attaching the 3 tub bolts I used a ratchet tiedown strap to pull the 3 legs together to get enough thread to start, what with all those washers and things.
Ran spin cycle dry for 3 minutes as per instructions before filling with water. Success.
Parts Used:
Mounting Stem/Tub Seal Kit
  • Fritz from Redway, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench (Adjustable), Wrench set
8 of 8 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
dryer wouldn't heat
First I unplugged the dryer. I shut off the gas line to the dryer. I opened the access door on the lower front of the dryer. I illuminated the interior of the dryer with a small flashlight that was mounted on two legs with magnets on the end to allow the light to be specifically directed. I took few digital pictures of the electrical connections to the dryer gas valve and the various sensors attached to the unit. I shut off the gas line valve to which the dryer gas valve was attached. I removed the two screws holding the dryer gas valve an lifted the unit out of the dryer. I vacuumed the inside of the dryer with an electric vacuum and also vacuumed the lint and dust off the gas valve I took out of the dryer. The flat style igniter was mounted on the front of the gas value. I removed two screws and took off the old flat style igniter. I reattached the new flat style igniter (carefully holding it by the ceramic mounting area to avoid breaking the igniter itself). I reinserted the gas valve into the dryer and reattached the two screws holding the gas valve into the dryer. I reattached the gas valve to the gas line in the dryer. I reattached the electrical connectors to the gas line and the sensors in the dryer. I turned the gas line in the house to the dryer back on. I plugged in the dryer and started it. No ignition.! I unplugged the dryer and reached in through the access door. I angled the flashlight to each of the sensors attached to the gas valve and the dryer electrical harness and pushed each one to make sure the electrical contacts were solid. When I checked the flame sensor ( a little box with a window mounted over a rectangle cut in the wall of the cylinder in which the flame burns when the gas is shooting out of the valve) the lower wire was unattached to the sensor. (Because the sensor sits on the side of the cylinder pointing towards the interior of the dryer its connections at the sensor was not visible. I bought a new flame sensor. I detached the old flame sensor from its connector, removed the screw mounting it to the cylinder and lifted it out of the tab holding it to the cylinder. I installed the new flame sensor by putting its tab in the slot for the tab in the cylinder and reattached the screw holding the flame sensor to the cylinder. I reconnected the electrical connection from the flame sensor to the dryer electrical harness. I plugged in the dryer. I turned the dryer on and got ignition of the dryer heater flame. Repair complete!
Parts Used:
Flat Style Igniter
  • Barry from Highland Park, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
9 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
Floor floded when washer started.
Thirty year old Maytag washer. Remove two screws at bottom of front panel with Philips screw driver. Hinge panel up to disconnect front panel from top of machine. Tilt washer back against wall to gain access to pulley at underside of washer. Then remove Philips head screw from bottom of center shaft. Remove bevel washer with screw. Remove stop block from end of center shaft and wind the pulley off center shaft. Clean center shaft of any debris and lightly coat with grease. Install belt on new pulley and motor, wind new pulley on center shaft. Replace stop block, washer, screw, and front cover.
Parts Used:
Transmission Drive Pulley
  • Keith from Big Sur, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
9 of 12 people found this instruction helpful.
Was this instruction helpful to you?
Thank you for voting!
All Instructions for the LSG7804AAE
121 - 135 of 1470