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DDG7187RCL General Electric Dryer - Instructions

All Instructions for the DDG7187RCL
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Dryer motor was running, but the drum stopped turning. The drive belt was broken.
I followed the instructions in your detailed online video. Fortunately on my model there was a removable panel on the back of the dryer which provided easy access to install the drive belt on the motor pulley and the idler pulley. Great video and very easy repair.
Parts Used:
Drive Belt
  • Charles from POINT HARBOR, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Replaced dyer belt
First unplug dryer... very important. You have to identify the appropriate size socket wrench and locate all necessary screws to remove top panel of dryer and front panel. Locate belt drive. Remove old belt , replacing it with new belt attaching belt to dryer drum . Remove back panel of dryer to better reach and adjust belt onto tension wheels. Put dyer back together. YouTube gives you an idea of how to properly change a belt on dryer
Parts Used:
Drive Belt
  • Vernon from BALTIMORE, MD
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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Timed dry cycle didn't work and "dryness" cycle never stopped once started.
Unplugged the dryer from the 240V supply. Unscrewed the 5 hex screws securing the sheet aluminum panel on the back of the dryer's front panel. Slid into the back panel was a schematic and diagnostic flow chart. The flow chart indicated that either the timer or resistor was at fault. (The chances of a resistor failing is very low. But, I checked it's resistance and connections just to be sure.) Ordered the new timer and installed it. In addition to removing the 5 hex screws securing the back panel, the timer was secured by two additional hex screws of the same size. I disconnected the electrical connectors and slid out the timer. The timer's dial needed to be pried off and installed on the timer. Reassembly involved doing the same steps above in reverse order.
Parts Used:
Timer
  • Gregg from SAN JOSE, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
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broken belt
Took the top and front off. DO NOT TAKE DRUM OFF!! Lifted drum slightly and worked belt around drum. Replaced front and top. Took off rear panel at bottom near vent pipe. Put belt around motor and then tension pulley. Buttoned everything up and that was it!
Parts Used:
Drive Belt
  • John from Perry, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
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Broken dryer belt on 30-year-old dryer
Found excellent instructions and diagrams online by searching under the model number. Best of all was the service from PartSelect. Belt arrived 24 hours after ordering. It was the right part, it was easy to install, and the dryer is running beautifully.
Parts Used:
Drive Belt
  • James from Marco Island, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Lint filter showing signs of wear. Can it be replaced?
I wanted to be sure a replacement would be available when the need arose. The dryer might be 30+ years old. Within a very few minutes I found the filter and placed an order. It arrived in 2 days. Now I won't have to worry about it in this aging lifetime.
Parts Used:
Lint Filter with Frame
  • Robert from Concord, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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My lint filter had broken sections in the screen
Just took it out and installed the new one--thanks so much
Parts Used:
Lint Filter with Frame
  • GERI from ROCHESTER, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Dryer Don't turn
I removed the 2 screws and lock assemblies from both sides on the back. Then i removed 4 screws (two from each side) on the control panel and lifted that up as i tipped the cover forward to disconnect the wires from the door switch. I found the wiring diagram inside the control panel cover, which included a belt routing diagram (very helpful, being the belt was laying in the bottom. I then removed 3 torx srews holding the drum to the bearing, and removed the drum. Let the fun begin! i proceded to put the belt onto the motor pulley and around the tensioner. i needed some help from my wife to set the drum back in as i held the belt up around it. once the drum was back in, i found the beld had fallen away from the tensioner. I lifted the front of the drum up just enough to get both arms below it and move the tensioner back to slip the belt over it correctly. With the new belt on i started to put the screws back in the drum. This got very frustrating, as you have to correctly line up all the holes again, while holding the drum in the correct angle to start the screws. this was the hardest part, not physically, but wears on a person's nerves quickly! Once all the screws were in and tight, i took a deep sigh of relief before i tipped the front cover up just enought to get the wires hooked back up for the door. I turned the unit on to verify the repair before re-assembly. Yep! works again, for well under $20.00! Thanks PartSelect!
Parts Used:
Drive Belt
  • Matthew from Alma, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Drum Would Not Turn
Remove the bottom cover of dryer to look at the motor, see belt hanging remove broken belt. Remove screws from the top and front, slide belt over drum put small piece of tape to hole belt in place replace screws go back to the rear pull belt over the motor pulley close back panel
Parts Used:
Drive Belt
  • PRESTON from CINCINNATI, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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sqeekysqueeky rear drum bearing
Open top by removing 4 phillips head screws above opened door, pop top up. Remove rear access panel, remove belt from drive & tension pully. Loosen top front screws, remove front panel to gain access to remove drum. After drum removed, I realized why rear bearing went bad- two front guides were worn causing rear bearing to angle and wear out. Replaced front pads, buttoned her up and now quite as new. Also replaced drive belt while in there.
Parts Used:
Rear Drum Bearing Kit Drive Belt
  • mitchell from Warren, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Belt Broken that turns the drum
First I shut off the gas and unhooked the gas line. Then opened the door and removed the screws that hold the top down in the front. I then tipped the top back so I could get to the top of the drum. I removed the screws ( 4 ) inside the door opening and slid the felt seal back. Next I put the belt in the drum and feed part out the crack between the drum and the dryer frame, being careful not to cut the belt. I woorked the belt around the crack and pulled it toward the drum. When I got the belt through it was all the way around the drum and I just put the belt over the motor pully and pulled the tensioner back and wrapped the belt over it. Put all the screws back in and the back on and fired it up. Works as good as it ever did.
Parts Used:
Drive Belt
  • Wayne from Williamston, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Wrench (Adjustable)
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Dryer squeaked when running
Took the dryer apart to get to the rear bearing. Took the bearing assembly out, kept the e-ring from the old bearing shaft, replaced the bearing kit, took the o-ring off the new shaft and replaced it with the e-ring, then reassembled the unit. Make sure to place a nail or long screw into into the rear of the drum, so that you can realign bearing on the drum. It is easier with two people when reassembling.
Parts Used:
Rear Drum Bearing Kit
  • George from Dassel, MN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set, Wrench set
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Noisy Bearing "SWEEKING"
The first thing I did was move the dryer out so I could "unplug it" !
Then I took the 4 philps head screws out that hold down the top of the dryer, then I lifted up the top and moved it off to the side making sure the wires didn't get pulled out.
Then I removed the 2 5/16 cap screws that holds the front panel on and lifted that off "Make sure you mark the down were the 2 wires for the door swich go" Like white on pin 1 and yellow on pin 2!!!
The next thing is to slide the drum foward so you can remove the element package then remove the 3 philps screws in the back of the drum make sure you have someone hold the element package there is a sheild between the drum and the element package that may fall that is a watch out you will need to move the element package up so you can work on it there will be wires hooked to this ring so becare full you don't break them off.
remove the element package you will see the bearing kit attached to that.
There are 4 5/16 cap screws that hold the bearing kit to that remove them and then remove the old bearing kit you may find and E Ring holding the old bearing kit in place (this would be found in the older models).
Before you install the new bearing kit take the new self tapping screws and tap the holes in the new bearing kit mounting plates this will make things go faster!!!
Now mount the bearing plate with the 4 holes to the element package there is a tab that needs to be mount in there too so look at the old one when you are taking it off.
Pick up the sheild that fell pick it up have a second person help you hold everything in place while you line up the holes for the front plate to the back of the drum and start your screws.
Now tighten them down check to make sure your belt didn't slide off the tensioner that is next to the motor before you slide the drum back in place if it did take the time to figure out how to get it back on the right way our you will be pulling things apart again.
What I did was spin the Drum by hand to make sure everything was ok. you will know if the belt is off it will not move when you spin the drum by hand.
Now that you made sure the belt is on you can put the front back on there are 2 studs on the bottom that you need to set the frount panel on before you can put the screws back in in it.
Now that you have the fron back on it hook your 2 wires back up to the door switch like you took them off!
Now move your top back over and you will see 2 clips on the back of it that slide into a grove in the back now that you have that in place start putting the screws back in put the middle 2 in first and tighten them down them put the last 2 in.
Now plug it back in if your vent pipe fell off hook it back up as you slide your dryer back in place now try it to make sure everything is working right and you will hear the differance.
Good Luck with your repairs....
Just a quick note this dryer is over 40 years old and still going.
I have replace 6 elements and 1 drive belt since it was bought new now the bearing kit.
Clean it once a year and the vent pipe every 6 months it will last!!!
Parts Used:
Rear Drum Bearing Kit
  • Russell P. from Dushore, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Dryer suddenly start making a rattling noise
I follow the easy instruction by a user in your web site to reach the problem area and discoverd the drive belt was broken.
As it turned out, the problem was compounded when I discovered also that the Heating element needed replacement.
At this point I decided it was time to let go and got a new dryer, choosing the same brand that lasted 25 years: GE
Parts Used:
Drive Belt
  • Ricardo from Hicksville, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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All Instructions for the DDG7187RCL
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