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DDC4492AFL Dryer - Instructions

All Instructions for the DDC4492AFL
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Drum not turning, machine 20 years old
I read all the reviews first, and decided on the best method, which is, disconnect utilities, remove four phillips screws under front of top,swing top open like a box lid, pull the two spade connectors off of the door switch, loosen the two hex head screws under the front of the front panel,remove the 2 hex head screws near the top of the front panel, and free the wire harness along right side of machine, this will allow you to swing the entire front panel to the right side,now remove the three torx screws inside the drum,this will allow the drum to be removed, exposing the bearing assembly at the rear of the drum. My machine is 20 years old, and when ordering parts, my machine #s were not listed, but they looked identical, but my bearing's shaft had a circlip retaining it in the bearing receiver, which had to be removed,( the newer shaft just inserts into the receiver, which is screwed into the back of the machine). Make sure to install the ground strap like the one you removed.My best advice for someone thinking about this repair, take it apart first and survey the parts needed before making the decision to repair your old machine, my drum's old bearing allowed the machine to function, and the shaft wore through the bottom of the receiver, allowing the defector, a round disc of thin sheet metal at the back of the drum (a $128 part), to make contact with it's housing, severely damaging both parts, making further investment in this machine unwise,even if I replaced the disc, the cut in the back, would allow really hot gases to escape into the dryer's interior, a scary scenario. I cut my losses and bought a new dryer last week. Anybody want to buy a brand new rear bearing assembly & belt for a GE dryer?. If you only have to replace the bearing, the job is a snap, but prepare to do a lot of dust removal!. Steve
Parts Used:
Rear Drum Bearing Kit Drive Belt
  • Stephen from Kendall Park, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Dryer shut down completely, wouldn't start
Removed 3 torx screws on the control panel. Removed two more regular screws from the dryer opening. This allows removal of the top. Removed some panels from the back to access where belt feeds through the motor. Found the belt snapped in two inside.

Now that I knew what the problem was I found partselect.com on Google. Ordered the part friday morning with ground. The belt arrived SATURDAY MORNING! I didn't even know fedex would deliver ground shipments on Saturday. Less than 24 hours later I had it. AWESOME.

Removed the front panel by removing two hex bolts to allow me to drape the belt over the drum. Not having seen how the belt was originally around the tensioner and the bad diagrams included with the dryer, it took some figuring to get it back on right. But we did it and we're back in business. I will absolutely buy from PartSelect.com again!
Parts Used:
Drive Belt
  • Rob from Valencia, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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Replaced dyer belt
First unplug dryer... very important. You have to identify the appropriate size socket wrench and locate all necessary screws to remove top panel of dryer and front panel. Locate belt drive. Remove old belt , replacing it with new belt attaching belt to dryer drum . Remove back panel of dryer to better reach and adjust belt onto tension wheels. Put dyer back together. YouTube gives you an idea of how to properly change a belt on dryer
Parts Used:
Drive Belt
  • Vernon from BALTIMORE, MD
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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Dryer leaving marks on clothes. Clothes were getting caught between drum and outside ring. Worn slides.
Remove top panel and front panel. 12 Screws. Be sure to vacuum entire inside of cabinet free of lint.
Parts Used:
Drive Belt Front Drum Slide Kit
  • E. Thomas from REDONDO BEACH, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Dryer motor was running, but the drum stopped turning. The drive belt was broken.
I followed the instructions in your detailed online video. Fortunately on my model there was a removable panel on the back of the dryer which provided easy access to install the drive belt on the motor pulley and the idler pulley. Great video and very easy repair.
Parts Used:
Drive Belt
  • Charles from POINT HARBOR, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Dryer Don't turn
I removed the 2 screws and lock assemblies from both sides on the back. Then i removed 4 screws (two from each side) on the control panel and lifted that up as i tipped the cover forward to disconnect the wires from the door switch. I found the wiring diagram inside the control panel cover, which included a belt routing diagram (very helpful, being the belt was laying in the bottom. I then removed 3 torx srews holding the drum to the bearing, and removed the drum. Let the fun begin! i proceded to put the belt onto the motor pulley and around the tensioner. i needed some help from my wife to set the drum back in as i held the belt up around it. once the drum was back in, i found the beld had fallen away from the tensioner. I lifted the front of the drum up just enough to get both arms below it and move the tensioner back to slip the belt over it correctly. With the new belt on i started to put the screws back in the drum. This got very frustrating, as you have to correctly line up all the holes again, while holding the drum in the correct angle to start the screws. this was the hardest part, not physically, but wears on a person's nerves quickly! Once all the screws were in and tight, i took a deep sigh of relief before i tipped the front cover up just enought to get the wires hooked back up for the door. I turned the unit on to verify the repair before re-assembly. Yep! works again, for well under $20.00! Thanks PartSelect!
Parts Used:
Drive Belt
  • Matthew from Alma, WI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
2 of 3 people found this instruction helpful.
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no heat
just changed out the gas igniter very simple to do thanks
Parts Used:
Gas Igniter
  • pauline from Upper Saddle River, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver
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broken belt
Took the top and front off. DO NOT TAKE DRUM OFF!! Lifted drum slightly and worked belt around drum. Replaced front and top. Took off rear panel at bottom near vent pipe. Put belt around motor and then tension pulley. Buttoned everything up and that was it!
Parts Used:
Drive Belt
  • John from Perry, FL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
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Broken dryer belt on 30-year-old dryer
Found excellent instructions and diagrams online by searching under the model number. Best of all was the service from PartSelect. Belt arrived 24 hours after ordering. It was the right part, it was easy to install, and the dryer is running beautifully.
Parts Used:
Drive Belt
  • James from Marco Island, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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Dryer suddenly start making a rattling noise
I follow the easy instruction by a user in your web site to reach the problem area and discoverd the drive belt was broken.
As it turned out, the problem was compounded when I discovered also that the Heating element needed replacement.
At this point I decided it was time to let go and got a new dryer, choosing the same brand that lasted 25 years: GE
Parts Used:
Drive Belt
  • Ricardo from Hicksville, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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dryer had a loud sqeaking noise
removed top, 2 hex screws, removed front 2 hex screws & 2 star screws. removed belt, slid drum out. Removed old bearing and replaced with new bearing kit. assembled in reverse.
It would help to have another person assist you.
Parts Used:
Rear Drum Bearing Kit
  • Barbara from Sugar Valley, GA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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loud noise when ran for 5 min.
Replaced the rear drum bearing. Not doing it before ,it took about 1 1/2 hrs. Problem was fixed.
Parts Used:
Rear Drum Bearing Kit
  • Joseph from Freeland, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
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dryer not heating( after replacing the high temp. thermostat
i removed the door and front panel then removed the two screws holding the coil bracket,disconnected the two wires on coils,set new coils in place and reversed the above process
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • james from HURON, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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rear dryer bearing assembly not threaded
The rear bearing plate had no threads where the screws go to hold it to the back of the dryer drum. I have never bought anything else that needed threads cut in it to be used as a replacement part.
Parts Used:
Drive Belt Front Drum Slide Kit Rear Drum Bearing Kit
  • Frank from Glendive, MT
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench set
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All Instructions for the DDC4492AFL
91 - 105 of 333