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DCVH660GH1MB General Electric Dryer - Instructions

All Instructions for the DCVH660GH1MB
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Dryer was making intermittent, loud, moaning and whistling-screeching noises (temporarily relieved by squirtin lubricant through the drum holes towards the bearing).
I used a flat head, a phillips head, and two sizes of sockets with my screwdriver to complete this project. I initially undid the control panel, but I don't think I needed to. I next took out two long screws that were holding the top of the cabinet on. These screws were just inside the doorway, directly above where the door sits when closed. I took the top off and set it aside. Being careful to mark which wire went to which lead, I undid the leads to the door open/closed switch. I next found two, black, hex-end screws, one each on the upper sides, towards the front, and undid these with a socket end on the screwdriver; being careful not to drop them as they came out. I then tilted the front panel out and up and set it aside. Note that the front opening holds the drum up so it can spin. Next, I tilted the front of the drum up, and pulled it outwards, till bearing at the back pulled out of the socket, and the drum dropped down enough that I could push the belt off the back of the drum. I then pulled the drum out through the front opening. I could see that the bearing was mostly worn away and metal was rubbing on metal. On the drum, I took off the air diffuser and the drum's half of the bearing assembly, and attached the new part of the bearing assembly, where the old one was. There was a metal disk that I was careful to reinsert in its former spot. I tried to make sure that all screws were tightened with equal force. Then I removed the entire bearing housing/blower assembly by undoing the outer screws that attached it ti the back wall of the cabinet, I rotated it outward at the top , pivoting around the compression fitting (no screws) at the base. I then removed the back half of the bearing housing, and replaced it. I needed to screw in the screws from the front while holding the spring-clip-thing in place (once installed, you can stick your finger through the hole in the bearing housing and feel the clip right behind it). I took this opportunity to clean all the excess lint out of the cabinet. I then replaced everything in reverse order until I got to the drum. I put the belt loosely arounf the drum, with the grooved/ridged side facing in. Then put the bearing (with drum), back in the socket. Feeling through the hole under the front of the drum, take the belt where it hangs off the drum TO YOUR RIGHT, run it under then up around the left side of the small pulley, then pull it to the right (above the small pulley) and around the right side of the big (tensioner) pulley, and let go. Note that there is a swithch in the tensioner that won't switch on unless there is enough tension on the belt! Put the front back on, lifting up the barrel from the inside, so that the barrel opening slides around the outside of the front's assembly. Ours seemed to fit more tightly than it had previously, into the felt padding around to bottom of the front assembly, but it seems to work fine? Screw in the two black, hex-head screws from the sides into the front, and re-attach the door-switch wires. Turn it on (carefully) to make sure it runs. Then attach the top, using the two long screws up through the door opening into the top. Ours is working much better than before - hotter, faster, quieter! Should we have lubricated the bearing with lithium grease?
Parts Used:
Rear Drum Bearing Kit
  • BJ from WHEAT RIDGE, CO
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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Squeaking noise that got gradually louder every day. And clothes getting stuck in the drum for months.
I asked my husband to repair it and he said call a repairman. I went online a read stories from others on how easy it was so I ordered the parts myself and did the repair. I strictly followed the video instructions. They were excellent! I also took the time to clean lint from the door and lint trap which i would not have done if a repairman had come to do the work. I now have the confidence to do the rear bearings if they go out!
Parts Used:
Duct Felt Seal Drum Bearing Slide - Green (Sold individually) Top Bearing Drum Bearing Slide - White (Sold individually)
  • Janise M from MAHOMET, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Squealing as drum rotated
Removed the star bit screws on the top of the control panel then removed the front by opening the door and removing the screws in the upper corners of the door jam. I then removed the top which exposed the drum slides. NOTE: This model requires 4 drum slides and NOT two as specified in the video.
Parts Used:
Drum Bearing Slide - Green (Sold individually)
  • Bill from COMSTOCK PARK, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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belt broke
had a great video to follow, made it easy to install.
Parts Used:
Drive Belt
  • joseph a from VALLEY STREAM, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
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Dryer's drum doesn't run
Follow YouTube "how to change dryer's belt" some video is very clear.
Parts Used:
Drive Belt
  • ruoli from Germantown, MD
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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Bearings worn out
Had back in service within a hour of receiving parts
Parts Used:
Light Bulb Duct Felt Seal Drum Bearing Slide - Green (Sold individually) Top Bearing Drum Bearing Slide - White (Sold individually)
  • Wayne from KERNERSVILLE, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Dryer was shutting off too early, before clothes could dry
Replaced High limit thermostat per video on the website. However, the flange of new thermostat is flat, while chassis it mounts on is round to conform to drum of dryer. So new thermostat was not flush with chassis. Dryer did not shut off early (that problem solved), but instead continued to dry clothes beyond time necessary. Note that old thermostat had one side of flange slightly bent and probably more flush with chassis, and better able to sense when hot temperatures were reached. I dismantled dryer again, slightly bent new flange, re-installed. Seems to work better now .
Parts Used:
High Limit Thermostat - L290-40F
  • Anthony from LAWRENCE, MA
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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belt broke on dryer
good replacement procedure on you tube.
Parts Used:
Drive Belt
  • rodney from VANCEBORO, NC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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evidently the pulley spring on video was very very very weak
the pulley spring took so much pressure to hold it down it took 3 men and a boy to hold it and place it in position to to get the belt on. Also there is not enough room to get your arms and hands in without getting some small cuts.Ultimately I removed the screws in the back of the dryer and spread the side of the dryer out to gain proper access. It was an easy repair if the spring would not have been so strong.
Parts Used:
Drive Belt
  • tim from NEW PRT RCHY, FL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers
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Dryer was making a loud squealing noise.
I replaced the dryer bearing ( a plastic part) and all of the slides on the bearing. It now operates like new.
Parts Used:
Drum Bearing Slide - Green (Sold individually)
  • Patrick from Albuquerque, NM
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Rubbing noise while dryer was running
Removed too of dryer and placed the parts on. Runs like a brand new one. Thanks so much!
Parts Used:
Drum Bearing Slide - Green (Sold individually)
  • Carol from Simpsonville, SC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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not drying clothes, felt seal hanging in the dryer
Took dryer apart replaced felt seal and the four drum slides put it back together works better now than when it was new!!!!!!
Parts Used:
Duct Felt Seal Drum Bearing Slide - Green (Sold individually) Drum Bearing Slide - White (Sold individually)
  • Adrian from Rutland, VT
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Dryer Not Starting
First I replaced the timer, but dryer still did not start. took apart dryer, jumper out door and componet near motor to see what problem was and to be able to run dryer while opened up. Actually motor had seized up just enough to not allow motor to start rotating. Lubricated motor shaft and rotated motor for oil to work its way in. Tried starting again and motor started. Buttoned dryer back up and reconnected wires to appropriate places and started dryer again and again.Worked for 4 loads of laundry and still working for 3 loads on Wednesday. Working fine
Parts Used:
Drive Belt
  • Scott from Poughkeepsie, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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There was screeching noise during the drying cycle. Clothes being dried were getting stuck in the upper bearing.
I followed the instructions given in the video I watched when ordering the parts. Very easy.
Parts Used:
Drum Bearing Slide - Green (Sold individually) Top Bearing Drum Bearing Slide - White (Sold individually)
  • Barbara from SICKLERVILLE, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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Rear drum bearing gone (only 4 years old). Decided to replace belt while I was at it.
I first watched the video on how to. Being mechecanically inclined I dismantled and removed everything needed to replace the drum bearing. Also removed belt at the same time. I replaced the bearing, then the belt. The belt could be a little tricky for some people. Getting the belt on the tension pulley could be a problem. What I did was I got a large nylon tie and put it around the armature of the motor. I then retracted the pulley just enough to be able to slip the belt over it. Of course this is all performed through the limited space on the bottom left, between the drum and the dryer shell. Once on the pulley, I cut the tie with wire cutters and it snapped into place. Rotated the drum a couple of times to line the belt with the pulley, perfect. I then put everything back together. I also cleaned any and all the lint that had gathered throughout the exhaust. Pluged the dryer in, perfect. Just like new. One more note getting the parts was so easy also. Your website and how to demo was a great help. Thank you, thank you very much. The words of the late Elvis Presley. They never get old.
Parts Used:
Drive Belt Rear Drum Bearing Kit
  • Robert from Salem, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set
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All Instructions for the DCVH660GH1MB
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