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JDG1000A Jenn-Air Dryer - Instructions

All Instructions for the JDG1000A
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Klunking noise and poor drying
The top was hard to figure out but I found that it pops off at the front with a flat screw driver. Be careful not to scratch the paint. I found that a rear drum roller was bad and the drum seals were deteriorated. I ordered a new belt, roller kit, front, and rear seals. This way I hoped I will not have to take it apart again. The seal were the hardest parts to replace. Make sure you look and remember how they were on before removing them. The directions were not to clear on the seals. The rest were good. It is much better to do it once. Take a picture if possible, it might come in handy as I took mine apart a week or so before the parts came in. I also cleaned out all of the accumulated lint buildup with a shop-vac, including the vent pipe, heater area, and front door. When I was done with this it worked like brand new.
Parts Used:
Rear Drum Support Roller Kit Drum Felt Seal Multi Rib Belt - 92-1/4"
  • Harry from Atco, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
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Gas Dryer would heat for one heating cycle but no gas afterward. Ignitor would glow.
Checked four thermocouples all showed continuity with my multimeter so they were all good. I'd read that the coils commonly went out and that these were the symptoms. Hey, it's very simple in there. Not much else could be wrong. I had a Maytag repairman come out. At first he said the problem was a blocked vent. I knew he was wrong. Then he said one of the thermocouples went out. It was $80 for him to come out. It turned out that his second diagnosis was wrong too. To repair the dryer by Maytag would have cost me $240. I gave him $80 and bought the coils for $37. They are EXTREMELY easy to replace: two screws held a bracket that held two coils. With the bracket off, I took off the old coils and slid on the new ones.
Parts Used:
M Series New Style Coil Kit
  • Jim from Foothill Ranch, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
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Maytag Performa squeaking loudly when running.
My wife's dryer started squeaking very high pitched, intermittently and then continuously when running. It progressed to a loud shrieking, unbearable throughout the house. Make sure you unplug the dryer. First I replaced the Drum glide and cushion kit. This was easy to do. Pry open the top of the dryer open with a screwdrive or putty knife. Now reach in and remove the retaining screws holding the front panel against the side panels. After releasing the front panel, let it fall forward about 4 inches and then unplug the two wire connected to the door closed sensor. Now carefully slide the thin belt towards the back of the dryer, it will release eventually as it is pulled off the pulley (dont worry, getting it back on is not that hard). Now you can remove the drum. After removing the drum, there are two tan or bluse plastic drum glides that the fron of the drum rests on. They can be worn out along with the cushion beneath them. Replace them with new one. This actually did NOT fix the problem. I put everything back together and....SQUEAK!! Next I undid everything as before and removed the drum. Now I decided to lubricate the rear rollers. First I used a silicone lubricant that again did not fix the problem. I could not find hi-temp lubricant, so I decided to use Axle grease. Bingo...no more squeak. To lubricate the rollers, remove the retaining clip and pull the wheel off. I put an even thin coat on the post they rest on and the inside hole of the wheel. Replace them and remember to put the retaining clip back on. Now replace the belt onto the metal pulley first, with the threaded side of the belt down towards the drive shaft, it should loop around the drive shaft and then you can pull it around the drum, slowly feedingthe drum farther and pulling the belt back along the drom. The smooth side of the belt should be on top of the drum. Now you have to reach back under the drum on the bottom right corner below the lint trap and pull the belt over the tensioner. Sounds harder than it is. Volia...that should fix it. Its been 3 days of non-stop laundry since the repair and no squeak. Next time I will purchase the replacement roller package, but this worked for now. Good luck.
Parts Used:
Drum Glide and Cushion Kit
  • Jason from Temecula, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers
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Close would not get dry. Dryer started normal. Timer would not time out.
Getting to any of the parts in the Maytag dryer is easy. Tip the dryer back and slide a 4 x 4 block under the front edge. You remove the whole front panel after you remove two screws at the bottom corners of the front panel. You need to tip the dryer back to get a screwdriver on the screws. Swing the front panel up to release the top of the door panel from the top. Watch the short wires to the door switch. Unhook the door switch wires and move the front panel out of the way. The timer on the top is accessed by re-moving two screws along the top edge. There are four screws. Remove them all and tip the top of the front panel forward. You then see that two screws hold the panel and the other two screws just hold the trim.

The dryer started normal. The drum motor run when the start button was operated. The fluff cycle operated normal to indicate the timer motor was OK. On the dry cycles, the igniter heated up. The gas came on. The dryer run for some period of time and then the flame went off. The thought was that the low temp cycle thermostat sensed the dryer was hot and thus switched over to time the cycle to its end. However, the low temp cycle thermostat tested good with a meter when the sensor was removed from the dryer and heated with a light bulb. Burnt contacts in the sensor were a possible problem. I also though the radiant sensor may be bad and not recycling after it got hot. After time, the igniter would cycle on but the gas flame would not come on. I thought the radiant heater might not be tripping the secondary coil on the gas valve. The gas valve coils tested good. I was checking them cold after the dryer had cooled down. I ordered a number of parts.

I got lucky and did a test on the coils while the dryer was still hot. One of the coils in the dual booster holding coil was going open when hot. When cold it had enough continuity to let the gas valve cycle on once. After the coil got warm it went open and shut the gas valve off. When the coil did cool off, it again had continuity. I was about ready to trash the dryer when I finely found the problem. I am happy I persisted and worked the problem through to a solution. I purchased several extra sensors but saved money in the long-run. I rate this problem at the high end of complexity for the do-it your self home owner to solve. The problem was an easy fix once the real problem was found. Only 4 screws and 3 push on wire connectors (two were on the front panel for the door switch).
Parts Used:
M Series New Style Coil Kit M Series New Style Coil Kit
  • Roger from Westminster, SC
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
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noisy blower wheel
unplug dryer---pop the top up---remove 2-1/4 metal screws that attach front to sides---unclip door switch & wires-lift up on front & set it aside--locate blower housing-remove 6-7 1/4 & 5/16 head metal screws--tough part is i had to buy a snap ring plier to get snap ring off motor shaft--use regular pliers,remove spring clip from blo-wheel hub--wiggle & pull blo-wheel from shaft--befoe re-assembling,,vac out all areas inside dryer case-carful not to damage wires & heat element--when clean re-assemble in order removed--also when ordering parts,,my dryer is series 11 (first two digits in serial #)--parts list showed wheel for series 10 & another for series 12---per instructions from a very nice lady on the other end of the parts select phone,always select the lower series--i my case,series 10
Parts Used:
Blower Wheel - B/10 Models
  • Ernie from St Ignace, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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extremely noisy operation
unplugged unit, opened lid, removed 2 screws & door switch from front panel, removed front panel & drum.
Removed clips & washers from rear roller shafts, removed 2 screws (each) attaching rear roller shafts to rear of unit. Replaced rear roller shafts, thrust washers, rollers & clips. Removed clip from belt tensioner idler arm, replaced idler pulley wheel & clip.
pulled tensioner toward motor side and locked in place with broomstick. Placed new belt over drum & installed drum/belt into unit, engaging rear drum lip over new rear drum support rollers. Guided belt
over motor shaft and slowly released broomstick to
tension belt. Turned drum by hand to ckeck belt tracking. Reinstalled front panel & door switch, installed 2 screws holding front panel to case. Closed lid. Plugged unit in & tested for proper operation-OK.
Parts Used:
Multi Rib Belt - 92-1/4" Rear Drum Support Roller Kit Idler Pulley Wheel
  • Paul from Daly City, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Dryer belt broke- drum would not turn
This was so much easier than I though it was going to be. Pulled up on the top part of the dryer and folded it over to the back. Removed 2 screws for the front panel and disconnected some wires. Laying down I fed the new belt on and made sure the tensioner was put back into the right spot, because when the belt broke the tensioner sprung to the other end of its travel. Put everything back together. This was made super easy because you guys had the parts and the shipping was super fast. Alot of the local shops in the area didnt even carry the belt or were not helpful..
Parts Used:
Multi Rib Belt - 92-1/4"
  • Ronald from Oakdale, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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pull out lint screen holder broke
used a flat blade screw driver to open top up(like a car hood) then removed two screws that held the front panel on. Two more screws held the lint colector part in place. The only problem that I had was that I had to use Elmers white glue to hold the gasket that ran around the lint colector in place.Just a little dab, not enough to soak it.When I took the part out there was about a volleyball's worth of lint in the fan blower. Ordered the part and 2 or three days later I had it. If I need another part I will be back...
Parts Used:
Lint Duct Housing
  • steve from madison, WI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers
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No Heat
I suspected a faulty igniter and disconnected the cable to the igniter and measured the resistance of the igniter and found it to be 70 ohms then I checked the voltage at the same cable towards the power source and found it to be 25 volts ac which should be 120 volts ac. Next I checked the radiant flame sensor and found it to be open (it should be a closed circuit when cold). I removed the flame sensor (with the power off) using a small box wrench and found a broken lead. Replacing the flame sensor solved the problem.
Parts Used:
Dryer Radiant Flame Sensor
  • NICHOLAS from PARMA, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench set
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dryer drum belt broke
I needed to remove the front lower cover, very easy as it is held on with clips only so I used a flat head screw driver to pop it off. I had to remove the lint filter and then there are two screws attaching the top cover of the dryer to the internal lint filter tray. The top of the dryer can then be opened front to back I again used the flat head screw driver to pop the top open as it has two clips at the front corners. It helps to have someone to hold it open or a rod of some type to keep it open. You can now lay the belt on the top of the drum and work it down the back side by pulling forward on the drum itself to seperate the drum from the seal that presses aginst the back side of the drum. I then went from the lower front to retrieve the belt now draped over the drum and pinched the belt to pass it through the tensioner and over the drive pulley. looking at it from the front the belt will come down the right side of the drum under the tensioner pulley around the drive pulley across the bottom of the drum and up the left side. The belt sits almost in the middle of the drum not against the back lip where there is a groove that might be confused as a place for the belt to ride that is where the seal sits then reverse the process to reattach the top to lint tunnel and reattach front cover and you are good to go . i would suggest vaccuming any old dust/ lint whlie everything is open as this reduces the chance for catching on fire I was supprised as to how much lint was loose inside the dryer cavity itself and our dryer is gas and the flame is an open flame.
Parts Used:
Multi Rib Belt - 92-1/4"
  • Paul from Athens, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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No heat
Took everything apart, replaced the igniter flint, and still didn't get heat. Then found out the thermal sensor wasn't running a electrical current through it with voltmeter and just replaced that, now it we have heat again!
Parts Used:
Dryer Radiant Flame Sensor
  • Philip from La Palma, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench set
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Lint screen assembly holder had broken
First I removed the 2 screws located on front panel securing dust collector in place, then I removed the two screws on the side of the dryer that secure the front panel. I also "popped" the top
of the dryer from the front panel. The front of the panel was then detached from the dryer. I thenpulled the gasket away from the collector, removed the old one and installed the new collector. Part of the kit also contained a new gasket to the exhaust duct, I merely removed the old gasket and installed the new one.. All this was notas hard asit sounds. The diagram from PartsSelect site helped
Parts Used:
Lint Duct Housing
  • George from Vernon, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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gas dryer would fire, but shut down before getting warm enough to dry clothes
Removed lower front cover of dryer, located coils, removed old coils by disconnecting the wires and removing the hold down bracket screws. Pulled the old coils out replaced them with the new coils by aligning the index pins on the coils with the holes in the bracket then reattached the bracket and plugged the wires into the new coils. Then closed the cover on the front of the dryer. Dryer now ignites and stays on to heat up and dry clothes.
Parts Used:
M Series New Style Coil Kit
  • Glenn from Ossian, IN
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set, Wrench set
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Dryer not Drying
Replaced both Coils. Purchased M Series coils much less expensive buying coils together instead of seperately. Problem solved.
Parts Used:
M Series New Style Coil Kit
  • Manuel from Jurupa Valley, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers
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the glow ignitor would not cycle on
I had an issue where I was not getting any power to my ignitor. After replacing the ignitor with a fresh one, the problem persisted. Next, I went hunting all the fuses and therrmostats for continuity. All seemed fine. So finally I decided to jump the flame sensor which is located on the outside of the flame tube. WHALLA! It ignited the glow plug. So with one 1/4"" nut driver I removed the single bolt from the unit, then I used a pliers to remove the two wires from the old unit. I replaced the sensor with Tue new unit and all was well. It took less than 5 min once I diagnosed the problem.
Parts Used:
Dryer Radiant Flame Sensor
  • Georgio from Oradell, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Pliers
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All Instructions for the JDG1000A
46 - 60 of 766