346995-1-S-Whirlpool-341241            -Multi Rib Belt - 92-1/4"
346995-1-S-Whirlpool-341241            -Multi Rib Belt - 92-1/4" 346995-2-S-Whirlpool-341241            -Multi Rib Belt - 92-1/4" 346995-3-S-Whirlpool-341241            -Multi Rib Belt - 92-1/4" http://www.partselect.com/Schematics/Maytag/Maytag_Thumb/UTGT4VNQ.gif

Multi Rib Belt - 92-1/4"

PartSelect Number PS346995

Manufacturer Part Number 341241
Manufactured by Whirlpool

This dryer drum belt has four ridges, three grooves and is 1/4" wide.

This part works with the following brands: Whirlpool, Admiral, Estate, Inglis, Kenmore, KitchenAid, Roper, Maytag, Crosley, Jenn-Air, Hardwick, Magic Chef, Amana, Caloric & Glenwood.

This part fixes the following symptoms:

  • Will not tumble.
  • Noisy.
  • Will Not Start.
  • No heat or not enough heat.
  • Takes too long to dry.
  • Heat stays on after drum has stopped.
  • Touchpad does not respond.
  • Compare At

    $12.91
  • You Save

    $2.15
  • Your Price

    $10.76
In Stock
Order within the next 7 hrs and your part ships today!
Fast Shipping Get this part fast. Average delivery time via regular ground: 1.8 days.

Videos For installing this part.

Related Parts Additional or alternate parts to consider.

Part PhotoPart DescriptionPriceAvailability

Idler Pulley Assembly

Part Number 383724

This part provides the tension required for a multi-ribbed belt. It also serves to help the belt to rotate the drum. This arm is what attaches to the idler pulley wheel.

Order within the next 7 hrs and your part ships today!
$9.85
In Stock

Maintenance Kit

Part Number 373087

NOTE: This kit is for 29" wide dryers built 1965 or later. Please verify model # before ordering as may not work for all models. This kit comes with one multi-rib belt, two drum support rollers, one idler pulley, four tri-rings, and one clip. This part can be used with both gas and electric dryers.

Order within the next 7 hrs and your part ships today!
$31.46
In Stock

Installation Instructions Provided by PartSelect customers like you.

Average Repair Rating: 3.4 / 5.0, 313 reviews What's this?
26-30 of 313
 

10 of 10 people found this instruction helpful

Parts Used

Level of DifficultyReally Easy

Time to do repair:15 - 30 mins

ToolsNutdriver, Screw drivers

CustomerJohn from Minneapolis, MN

Dryer would not tumble.

I wasn't sure if the problem was the belt (probable) or the idler pulley assembly (less likely) but the total for both parts was about $26 plus shipping. So why not replace both to be sure?

As it turns out, my original idler pulley assembly does not turn. Rather, it has a concave semi-circular piece that is fixed in place. The belt ran in a groove in that piece.

The replacement part has a nylon wheel that turns. As a result of replacing the idler pulley assembly (which I don't think was necessary to fix my tumbling problem) the dryer runs much quieter. (We used to get a fair amount of squeaking when the belt rubbed).

As for the actual repair (I would rate myself as above average on tackling household repairs), it was about the simplest repair I've ever done. I followed the video provided on this site (excellent video) and it took less than 20 minutes -- cleaning up all of the lint/odds and ends under the washer and dryer took longer than the actual repair.

My only issue (minor) was disconnecting the electric harness. It did not slide as easily as in the video. I had to coax mine a bit with a small screwdriver (make sure your dryer is unplugged!!). I suspect it was simply a function of the harness never being unplugged -- the dryer is 9 years old.

I also felt great because I'm sure I saved a $125 service call (for only $26 in parts and 20 minutes of my life).

Good luck!

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9 of 11 people found this instruction helpful

Parts Used

Level of DifficultyEasy

Time to do repair:30 - 60 mins

ToolsPliers, Screw drivers

CustomerTODD from GRASS VALLEY, CA

Badly worn idler pulley and rollers.

Braced dryer drum with a block. Removed the two rollers one at a time by using a screwdriver to pop off the triangular clip. Slid on new rollers. Would have been easier to remove the drum out the front instead of bracing it. Installed new idler pulley and belt. Dryer is 25 years old and sounds like a new one now when running.

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7 of 7 people found this instruction helpful

Parts Used

Level of DifficultyA Bit Difficult

Time to do repair:More than 2 hours

ToolsPliers, Socket set, Wrench (Adjustable), Wrench set

CustomerDerek from Missouri City, TX

Humming noise then quit after pushing start. Drum would not turn manually.

Looking at the schematics, it wasn't clear exactly where the motor was located. I took off the rear panel thinking I could get to the motor through the blower. Realizing that was a no-go, I did some web searching and found that the lint screen chute had to be unscrewed, the top had to be lifted to gain access to the top 2 screws holding the front panel to to the main body. The barrel was then dropped and the rib belt removed from around it so I could set it aside. The clips were removed from the front and the back of the motor to gain access to the blower shaft. .The motor shaft is screwed into the blower shaft but it took me a while to figure out how to grab the blower shaft( made of hardened plastic?) with an adjustable wrench while torquing the end of the shaft with a (3/4"?) socket wrench. Access to the rear was rough, but getting the motor out an back in was easy. The spring tensioner for the belt was the next hurdle. With the s-curve facing outward and clipped to the base, the belt with the rib side wrapped around the barrel, the belt was slid between the roller and the tensioner bracket and wrapped around the motor drive rib side inward. I had to take the old motor to kind of prop up the barrel so I could at least see the tensioner and motor interface. I had to do a balance trick where I held the barrel up while centering it to the belt and the rear panel while ensuring the cloth seal was seated to the outside of the chamber. The front panel went on, and the front cloth seal was seated by spinning the barrel. The rest was just a matter of reversing the steps. Tons of lint/dust is probably what crashed this motor. Disassembling the front and the back allowed a thorough clean up - vacuuming and wipe down. Should go another 10 years/

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7 of 7 people found this instruction helpful

Parts Used

Level of DifficultyA Bit Difficult

Time to do repair:1- 2 hours

ToolsNutdriver, Screw drivers

CustomerMartin from Lynchburg, VA

Dryer had quit turning

I first disconnected the power cord and the vent hose. I removed the screws on the top of the back side to raise the top of the unit. There are also 2 screws holding the lint filter shoot which were also removed to allow the top to be lifted up. Its not necessary to remove the top since this would require disconnecting the wiring harness etc.

Next I removed the 2 screws located on the top-inside surface, which connect the front panel to the unit. After these were removed, the front panel lifts up and off--there are two clips which slid free on the bottom of the unit. The shut off switch on the door has to be disconnected to remove the panel.

With the front panel removed, the drum can be removed. I vacuumed out the interior and retrieved the idle pulley which had popped loose when the belt broke.

I removed the old rear drum seal and cleaned the edge with some brake cleaner solvent and steel wool. I then wiped the edge with paper towel and more brake cleaner to remove any oily residues. Before applying the glue, I test fit the seal which turned out to be a bit tight, so I stretched it a bit around the drum until it would fit on easily.

I used a disposible glue brush to spread a thin layer of the contact cement along the edge of the drum. By the time I finished one round, the glue was dry where I had started and so I did a second thin coat.

I then oriented the seal as per the directions and began fitting onto the edge trying to keep the free felt surface from getting into the glue. By the time I had reach the opposite side, the belt was pretty tight and so I had to stretch it a bit to get it to go on. I then worked my way around the edge a final time insuring that the seal was positioned correctly all the way around and the glue was pressed tight. I let the glue set for several hours before reassembling.

After the glue was dry, I put the drum back into the unit and worked the seal up onto the circular back panel until the groove on the drum was correctly positioned on the rear rollers. I propped the front edge of the drum on two 2 in rolls of duck tape so that I could rotate the drum freely several times. I checked the outside and inside to be sure that the seal was not turned under any place.

Finally, I slipped the new belt over the drum and past my 2 rolls of tape and positioned it groove side in over the drum. I then reinserted the tensioning pulling back into the slot just in front of the motor. The pulley goes just to the left of the motor pulley, the end of the tap on the base inserts in a slot and then 2 pins rest in a second slot to the right of the first. A loop of the belt then passes through underneath the pulley and then over the motor pulley. This requires pulling the tensioning pulling pulley towards the motor to get enough slack. I then rotated the drum several times and made sure that the belt was not twisted and the groove side was towards the drum.

To help hold the drum up while I was fitting the front panel. I supported the drum with a piece of 2 in tape run from the top/front edge of the drum to the back panel of the unit. I removed my two rolls of tape from under the unit, slipped the front panel back onto the two bottom clips, and then worked the front open of the drum over the front seal by opening the door and pushing from the inside and rotating the drum. I replugged the door switch and made sure the wire clips were secure.

I then replaced the 2 screws to hold the front panel. I put the top back down and resecured the screws on the back before reattaching the hose and replugging the unit. I test ran the unit for several minutes empty, listening for weird noises that would indicate something didn't go together correctly.

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10 of 17 people found this instruction helpful

Parts Used

Level of DifficultyEasy

Time to do repair:1- 2 hours

ToolsPliers, Screw drivers, Socket set

CustomerWilliam from BURNET, TX

Dryer was getting hotter than blue-blazes, melted synthetics, damaged belt

Removed back of dryer, there were 3 screws on each side. There were two thermostats on the output vent and one thermostat on the heating element housing. Adjusted the temp settings on the thermostats per the instructions received with each thermostat (cross-refernece of original number required). Each thermostat had two screws and two wires. Terminals were coded "1" and "3," must get correct wires back in same place. The heating element thermostat required to splice new connector on one wire (per instructions enclosed with thermostat).. Easy as pie. BELT: Remove screws from lint screen housing, then pry up front of top of dryer and swing back (make sure you are next to the wall so it doesn't fall.) Remove the bottom front panel, remove the door tension springs, remove the two screws on the front of the front panel and remove the two top screws on the inside of the door panel (leave the door attached, but use tape to hold it shut so it doesn't hit you on the head) Careful of the door switch wire, carefully lean door up so it doesn't fall. The Drum will fall when front panel is removed, so have someone to help you hold it up. You do not have to remove the drum. With your frend holding the drum, go under and pull the tension spring roller back to slack up the belt and remove the belt from the tensioner and motor pulley. Remove belt from drum. Wrap new belt around drum (ribs down facing drum) and re-route belt around pulleys according to diagram in instructions (same way you pulled it off). I did it by myself, but I got konked in the head by the door, so be careful. Easy, but awkward. Watch for sharp sheetmetal edges.

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