Models > YMED9600TK0 > Instructions

YMED9600TK0 Maytag Dryer - Instructions

All installation instructions for YMED9600TK0 parts

These instructions have been submitted by other PartSelect customers and can help guide you through the dryer repair with useful information like difficulty of repair, length of repair, tools needed, and more.

All Instructions for the YMED9600TK0
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felt strip came off lint screen

  • Customer: JEFFREY from FALL RIVER MA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 69 of 89 people found this instruction helpful
ordered new lint screen, removed old screen, inserted new screen.

catch mounted on door broke

  • Customer: Paul from Mt. Pleasant SC
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 33 of 44 people found this instruction helpful
The door had always opened with the wrong swing and it wasn't til I needed to repair this that I noticed you could change the swing. I changed the swing of the door and then noticed that the clip was included on both sides so i did not need to repair the catch. I still have the part so when it breaks again, I can just pop it in.

Our dryer started squealing and would then stop running.

  • Customer: Kelly from Aptos CA
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Nutdriver, Pliers, Wrench(Adjustable)
  • 26 of 32 people found this instruction helpful
After determining that the dryer motor was the issue I wrote down the part number and logged on to partselect.com.

I input the number into the search box and there was the exact motor I needed.

The price was fair and the delivery quick so I figured I would give yuo guys a shot and see how it goes.

The part showed up on time and as expected. It was well packed and most importantly - it was the CORRECT part.

I disassembled the dryer which involved removing the lint trap, pulling out the blower fan and removing the motor cover. The motor was held in with 2 metal screws and wiring harness.

I took the belt off of the tensioner and pulled out the old motor. The motor was mounted with 2 clips which snapped off with ease. Reassembly was a breeze since the motor fit perfectly- the entire transplant operation took all of about 35 minutes.

I crossed my fingers, turned on the gas, plugged it in and........SUCCESS!

Since the dryer was down for over a week the backlog of laundry was piled pretty high. This replacement motor would immediately be put to the test.

It has been 5 days of non-stop drying and no squeeks, no squeels and nothing but dry clothes!

Thanks to Part Select for getting everything right the first time. It made a potentially very bad experience turn out as good as I could have ever hoped.

Rear tub seal failure

  • Customer: Jerry from Everett WA
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers, Socket set
  • 21 of 29 people found this instruction helpful
I removed the top cover and then the back cover, released the belt tensioner and removed the drive belt. Then slid the tub out of the unit and onto the back dack. Sanded the remnents of the old seal off. Wiped the tub lip with laquer thinner and applied the "fast" drying glue supplied with the kit. Installed the seal and re-assembled the unit...works fine

Felt gasket on lint filter loose...

  • Customer: Catherine from Atascadero CA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 17 of 20 people found this instruction helpful
Found this site by googling, and it works! I searched lint filters and just ordered based on how it looked...LOL! Husband wasn't home, it looked pretty much like the one I had in my hand, so.... I ordered it. It is the perfect fit and seems to have a tighter gasket glued in all around the screen. Let's hope this one lasts longer than 6 months! Thank you Parts Select for being so fast!! Filter got here in less than 48 hrs.!

Needed to change rear exhaust to the side to fit dryer into my closet.

  • Customer: Mark from San Diego CA
  • Difficulty: Really easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers, Wrench(Adjustable)
  • 29 of 57 people found this instruction helpful
First, I opened up the front of the dryer and then unscrewed the entire back piece. I assembled the new exhaust piece from the kit. Next, I took out the old straight rear exhaust and then replaced it with the elbow shaped left eshaust from the kit. Lastly, reattache the back and front pieces of the dryer.

Very Loud Squeaking Noise

  • Customer: GREGORY from Wilsonville OR
  • Difficulty: Easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Nutdriver, Pliers, Screw drivers
  • 12 of 15 people found this instruction helpful
1) Disconnected power cord from wall. 2) Disconnected vent hose from back of dryer. 3)Removed dryer rear panel. 4)Disengaged tension spring on idle wheel arm. 5) Removed worn idle wheel. 6)Installed new Idler wheel assembly. 7) Vacuumed dust from rear of dryer (optional, recommended). 8) Reinstalled rear cover, vent hose and power cord. Easy repair 15-30

Unit would shut down in the middle of cycle and flash E1 trouble code

  • Customer: Jim from Tucson AZ
  • Difficulty: A Bit Difficult
  • Time to Complete: 15 - 30 mins
  • Tools Required: Nutdriver, Screw drivers, Socket set
  • 11 of 14 people found this instruction helpful
Had to remove the back of unit to access the area of subject part by removeing 12 to 14 screws also the gas line had to be removed. Two screws held the part in place. Unit now runs normal.Saved alot on repair costs!!!!!

Poorly designed lint filter/ gasket falls off

  • Customer: John from Madison WI
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 11 of 15 people found this instruction helpful
Replaced

seal for lint filter came off

  • Customer: John from Midland TX
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 9 of 12 people found this instruction helpful
Pulled out the old and slid in the new filter

The felt strip on the filter had come undone.

  • Customer: Rebecca from Laredo TX
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 10 of 16 people found this instruction helpful
Took the old filter out and inserted the new one- works great!!

Door Catch was broken

  • Customer: Inocencio from Edinburg TX
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 7 of 8 people found this instruction helpful
I just inserted the door catch, which by the way fit in perfectly. Thanks. Took 5 seconds to repair.

Scratches in Surface

  • Customer: Michelle from Richardson TX
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 7 of 9 people found this instruction helpful
This product comes in a bottle with a brush like Liquid Paper. It goes on incredibly easy. A second coat might be needed. I wanted to prevent rust from setting in so I covered the scratches and dings. The paint is a little brighter since my washer is 10 years old but it still looks great.

Flashing E1 code for a bad thermistor

  • Customer: John from Cedar Rapids IA
  • Difficulty: A Bit Difficult
  • Time to Complete: 30 - 60 mins
  • Tools Required: Nutdriver, Pliers, Screw drivers
  • 8 of 13 people found this instruction helpful
I replaced the thermistor earlier, but the code was still flashing. I noticed the heater terminals were charred and pretty well covered in carbon. So, I replaced the heater, the thermostat and thermal fuse and replaced the 3/8" spade terminals on the heater wires. (These are hard to find - most electrical spades terminals are .250. Also, I crimped and soldered these for a connection with the lowest resistance possible). After all that, the code still flashed! I let the explatives fly, calmed down, and ran the control board test. (This is done by pressing "more time" "less time" "more time" "less time" in succession.) The control board was passing all the tests, but the thermistor test, and the only thing is in this circuit is the thermistor, the wires, the connector to the control board, and some circuit on the control board that involves a few resistors and the "brain" chip. So, I checked the terminals at the thermistor, the wires up to the control board and the connector at the board. The control board connector was fairly dust encrusted, so I unplugged it, cleaned the control board terminals and sucked away all the lint and dust. Finally, I carefully removed earch crimp terminal from the Molex connector (the white female connector) and cleaned and bent them to yield a better connection to the terminals on the control board. I put it all back together, and thus far it is working fine.

Felt piece coming out of filter

  • Customer: Sara from Solon IA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 6 of 7 people found this instruction helpful
Removed old filter and put in new one.
All Instructions for the YMED9600TK0
1-15 of 138