Models > TDG336RBW1 > Instructions

TDG336RBW1 Tappan Dryer - Instructions

All installation instructions for TDG336RBW1 parts

These instructions have been submitted by other PartSelect customers and can help guide you through the dryer repair with useful information like difficulty of repair, length of repair, tools needed, and more.

All Instructions for the TDG336RBW1
31-45 of 231
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Bearing wore out in original idler pulley

  • Customer: Paul from Placerville CA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Nutdriver, Socket set
  • 3 of 4 people found this instruction helpful
Removed rear inspection plate, removed pulley spring and one hex bolt, replaced in reverse order. Very simple removal and install for this. Glad to see that Part Select still had parts for this 22 year old drier.

old screen rusty and torn off from frame - the dryer is quite old but works very well.

  • Customer: Bindy from Memphis TN
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 3 of 4 people found this instruction helpful
Unscrewed old frame, removed it and put in the new one. Now I have a brand new dryer. Thanks!

Dryer wasn't heating

  • Customer: Jack from Huntingdon PA
  • Difficulty: Easy
  • Time to Complete: 1- 2 hours
  • Tools Required: Pliers, Screw drivers
  • 3 of 4 people found this instruction helpful
Determined that the coil on the gas valve wasn't pulling in to ignite. Using an ohmmeter, I determined the coil was open. The coil was removed by pulling off the wire connecter and removing the two phillips screws holding the bracket over the two coils. The coil then slides out. I slid the new coil into place, replaced the bracket and two screws and reconnected the wire connector. It worked immediately. The actual repair only took 15 minutes. The bulk of the time was spent tracking down which part had failed.

The lint screen had tears on it which could cause a serious problem, possibly a fire.

  • Customer: Joyce from North Dighton MA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
I unscrewed the old the lint screen FRAME and easily removed it, replacing it with the new one. The new lint -- SCREEN -- just needed to be squeezed here and there, and molded into a better shape. The screen itself, arrived flattened on the bottom, causing it to be too wide and difficult to remove from the frame. I easily molded it with my hands into the shape of the previous one and it slipped right into place. ( Shaped like an oval, flexible sack.) VERY easy!

Small burn marks on light clothing

  • Customer: Gordon from Canton PA
  • Difficulty: Really easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
First I unpluged the machine, then opened the top with a flat head screw driver. Then I removed the two screws inside, unpluged the door sensor. (makes it stop when opened) Removed old gasket, cleaned with emery cloth, cleaned the residue and applied the glue provided. Waited about 1 min. and applied the new gasket leaving about 1/8'' of it hanging over the door facing the drum.

screen fell out of lint screan frame

  • Customer: steve from scottsville KY
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
remove 2 screws,pull frame out. put new in. tighten 2 screws. put lint screen in

Lint screen had torn

  • Customer: Luann from Huntersville NC
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 2 of 2 people found this instruction helpful
For me it wasn't even a repair, but rather, open the package, take out and discard the old lint tray and pop the new one in! Done. I didn't have to replace the frame. I would like to comment on how easy ordering was from partselect.com and how quickly the part arrived. Very satisfied customer! Thank you!

WIRE MESHING HAD BROKEN AWAY FROM THE RUBBER FRAMING THA WAS TO HOLD IT TOGETHER AND LINT WAS BYPASSING THE SCREEN AND GETTING INTO THE VENT TUBE.

  • Customer: JOHN from NAUGATUCK CT
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
OPENED THE DRYER DOOR UNSREWED THE TWO PHILLIPS HOLDING THE FILTER FRAMEWORK IN PLACE DID A TWO SECOND SWAP-OUT DROPPED THE NEW UNIT INTO PLACE THE NEW UNIT AND REFASTENED IT WITH THE 2 SCREWS THAT HELD THE OLD ONE IN PLACE . AND WAS DRYING A LOAD OF CLOTHES WITHIN TWO MINUTES ..
THANK YOU JG

replaced broken belt

  • Customer: Shelia from Elizabethtown IL
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Wrench set
  • 2 of 2 people found this instruction helpful
Romoved front from dryer . Then loosened tub , slid belt on , reached in back and put belt on pulley , turned tub till belt went into place and reassembled dryer all with the help of a 3 year old and an8 year old,so in my oppinion it was one of the easiest fixes i've ever done!

Gas dryer wouldn't stay hot.

  • Customer: David from Petaluma CA
  • Difficulty: Really easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Screw drivers, Socket set
  • 2 of 2 people found this instruction helpful
I definitely would not have tried to do this had it not been for the other testimonials written here. But it sounded so easy, I had to just try it (the repair man estimated that with parts and labor, we would be looking at somewhere between $250 and $300!).

The repair itself took less than 15 min, but I spend a good deal of time looking around the garage for a few screwdrivers and my socket set (me and tools don't meet too often). I could simply pry up the top cover on the dryer with my hands, then got it all the way up after removing two screws from the lint trap and undoing this really annoying wire connector thing. From there the front panel lifted off. To remove the drum, just had to release the tensonier on the belt, and it came right out. From this point it was really obvious where the replacement parts would be going. A few screws later, and I could swap the parts, and put humpty dumpty back together again.

It works!!!

dryer lint screen rplacement

  • Customer: Frank from Las Vegas NV
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
removed two screws - replaced lint screen replacement, TIME TO REPLACE UNIT - ONE MINUTE. What made this project a snap was the pictures and graphs( parts replace) uses to ensure you are ordering the exact screen .

clothes not drying in one cycle

  • Customer: Aaron from Kerhonkson NY
  • Difficulty: Easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
remove top cover, remove front of dryer, unscrew two #2 screws from gas valve coil hol down bracket. replace coils. reassemble dryer.. works great.. had already replaced the thermostate and flame sensor.. didn't change anything.. the coil set did the trick..

replace old screen

  • Customer: charles from nantucket MA
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 2 of 2 people found this instruction helpful
take out of box remove old screen drop in new screen

Well we ordered one and that didn't fit so had to return then we ordered the 2nd one and that worked but really only need the lint screen not the whole frame so it was to expensive for what you need why not sell it separate?

  • Customer: Delaine from Fort Atkinson WI
  • Difficulty: A Bit Difficult
  • Time to Complete: Less than 15 mins
  • Tools Required:
  • 2 of 2 people found this instruction helpful
put it in the lint screen spot.

The old drum seal top had torn off.

  • Customer: jeffrey from round lake heights IL
  • Difficulty: Easy
  • Time to Complete: 1- 2 hours
  • Tools Required: Screw drivers
  • 2 of 2 people found this instruction helpful
Opened the drayer top and then removed the front panel.
Removed the bottom seal from the acr as it was warn.
Carefully scarped off the remaining bits of felt from the arc.
Applied the supplied adhesive to the top half of the cleaned arc.
Placed the seal and held in place with small spring clamps.
Let it dry for an hour, then I repeated the process with the bottom seal.
I let it dry over night, overkill probably but I wanted it to stay.
Replaced the front with new seal and closed up the top.
It has been working well since. Thanks for stocking parts that help out homeowner's on tight budgets.
All Instructions for the TDG336RBW1
31-45 of 231