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MDE13PDAEW Maytag Dryer - Instructions

All Instructions for the MDE13PDAEW
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Broken Tumbler & Motor Belt
Disassembled per instructions. Additional time used to clean inside unit.. Its much easier to install belt on motor pulley and tension pulley ( Roller) from rear access panel. Also ensures proper belt alignment on all items.
Parts Used:
Tumbler and Motor Belt
  • John from ELBRIDGE, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Much noise when drying clothes.
Installation of drum support kit was difficult because my snap ring pliers would not fit in the snap ring holes. Had to use pliers and screw driver to get them off and to put them back on. That took much patience and time. Installation of front guides was a bit difficult because the rivets were loose and turned when trying to drill them out. Also they were bigger and I needed a larger drill bit than the 1/8 told about in the video. Used drill, screw driver and pliers to get the rivets out. Also took more time and patience to do this. Belt did not need replacement but felt it a good idea to do it as long as I was in there. Belt installation was easy because my dryer has a rear view opening and I could use it to thread the belt. Tried it from the front as shown in the video just to see if I could and found it impossible. Could not even get my hands to hold the belt. Also vacuumed out 20 years of lint and dust that was inside the dryer. The videos were excellent in showing what to do and how to do it. Not sure how well I would have done without them.
Parts Used:
Tumbler and Motor Belt Front Glide Kit Drum Support Roller Kit
  • Roger from RALEIGH, NC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Noisy Dryer operation and eventually no air movement through dryer
Every two to three years, the blower wheel gets chewed out in the center where it attaches to the motor shaft. I have learned the sound of it starting to rattle so I know to order a new blower before the air stops moving altogether. Replacing it is very easy if you have tiny sockets or nut drivers and a pair of snap ring pliers.

When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
Parts Used:
Blower Wheel with Clamp
  • Russell from ELK GROVE, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
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old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
Parts Used:
Tumbler and Motor Belt Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm Idler Arm Screw Sleeve
  • William from ORANGEBURG, SC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
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When the dryer grumbles check the blower wheel too.
If your dryer is making a rumbling noise, change the blower wheel. It's plastic and the heating and cooling cycles causes the keyway in the plastic to give out and the wheel just spins causing the noise and the slower dry time. The other parts I replaced see below. Like many other repairs, remove screws below dryer door. Mark all wires and locations for re-assembly. Next remove front tumbler/lint screen assembly (4 sheet metal screws 2/L 2/R. Work belt off back of tumbler and remove. Use flathead screw driver to release tabs that hold felts on both front and back tumble supports. Make sure you know rotation of tumbler and install new felts so the overlap goes in direction of spin. Use a drum stick or 3/8 ratchet extension, something dull and flat to press tabs back down on felts. A screwdriver could slip off and tear cloth. Next drill out heads of the rivets on the glides and remove teflon glide and cork backer. Make sure all rivet material is removed front and back. Install new cork and glide. Rivet one side back in, then the other. Repeat on 2nd glide. Re-assemble dryer. Super smooth, super quiet.
Parts Used:
Tumbler and Motor Belt Front or Rear Drum Felt Seal Front Glide Kit
  • Chris from MArietta, GA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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I relaced our worn out lint filter
My part was not amazing. What was genuinely cool: I ordered it one day and it was here the next, took out the old and put in the new. Thanks for getting it here so quickly.
Parts Used:
Lint Filter
  • Robert from Sacramento, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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One of the roller shafts was worn
Replaced both rollers,shafts, bearings and snap rings.
Parts Used:
Roller Shaft Drum Roller Shaft Washer Drum Support Roller Kit Retaining Ring
  • William from Springfield, OH
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
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electric dryer had no heat
I removed the cover from the control panel, took out the schematic, removed the rear cover by the motor, followed the schematic, powered the heater by taking the blue hot leg wire off the right side of the switch and touching it to the black lead for the heater on the left side, and I could hear the heater power on. Since bypassing the motor start switch powered the heater, I ordered the part. When it came, I installed it in about 5 minutes and the dryer worked perfectly.
Parts Used:
DISCONTINUED
  • David from Lower Burrell, PA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Squeaking noise
I had replaced belt, but the noise continued. Ordered new rollers and washer. Removed the front panel by tipping the dryer back against the wall and removing two screws at the bottom of the panel. Tipping the dryer makes it easy to remove the front panel. Removed the front drum support by removing four (4) screws. I was then able to just move the drum enough to have access to the rollers. Didn't even have to remove the belt. Replaced the rollers. Needed special pliers to remove and replace the retaining rings. Put the drum back into position and mounted the front drum support. Tightened four screws and then put the front panel back on. Plugged it in and tested it. Problem solved. Took about 35 minutes. Thanks
Parts Used:
Drum Roller Shaft Washer Drum Support Roller Kit Retaining Ring
  • Charles from Daphne, AL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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squeaky sound when drying
Removed front panel and tumbler, replaced roller axle,
wheel, and front glides. Anybody can do this.
Parts Used:
Roller Shaft Front Glide Kit
  • Chris from Sherman, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers, Wrench set
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motor had loud bearing noise
There are some really good blow-by-blow descriptions on how to go about the repair already listed here. The main thing is to go slowly and take your time. It was really quite logical for a weekend handy man. The best advise was to use a digital camera to record every step of the way as you disassemble the dryer. I referenced the pictures more than once when I was putting all of the wires and pieces back together. Also, I didn't have a pair of snap ring pliers. My neighbor told me how to use two ice picks to poke in the tiny holes and spread the rings...just be careful! Keep a vacuum handy, there will be lots of lint to clean up. The new motor, belt and pulley work great and I pleased with how well the repair went.
Parts Used:
Motor Pulley - No Set Screw Tumbler and Motor Belt Drive Motor - 60Hz 115V SET SCREW-
  • Lee from Maidens, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Rattling noise and slow drying.
Turn off circuit breaker or unplug. Remove two screws 4 inches from bottom front panel of cabinet with stubby phillips head. Pull panel towards you about 30 degrees; then wiggle it down, to free two steel spring clips holding it to cabinet. Pull off red and yellow wire from door switch. Now set front panel aside. Blower assembly is facing you at lower left. Open the housing by removing six small screws from cover and one attached to dryer base. Remove spring clip from end of shaft. (A circlip pliers helps to prevent it from springing off somewhere.). Squeeze spring retainer surrounding blower wheel shaft with regular pliers, and wiggle the blower off. Replace in reverse order. Be sure insulation around blower wheel housing seats properly into front panel. This keeps the hot air flowing up past the lint trap.
Easy job, about half hour. Mine took longer, because I had removed the belt and drum, thinking the noise came from bad drum support rollers. It was just the plastic blower wheel shaft seat, which had worn itself round. Cost $20 (including shipping) and my 29-year old Maytag is as good as new--at least for now.
Parts Used:
Blower Wheel with Clamp
  • Laurence from Leesburg, VA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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Dryer was noisy and stalling. Taking twice as long to dry clothes and using more electricity
I had my oldest son who was home from college help me. We removed the front face of the dryer and put the unit on it's back. We removed the door switch and the blower unit. I didn't get a good look at how the belt was routed when we removed the drum but was able to figure it out when we put it back together. Not only was the belt frayed and dry rotted, the blower squirrel cage was free-wheeling on the shaft. I found a tab of metal I was able to insert in the flat of the shaft between the cage bushing and the shaft and I put the squeeze ring and snap ring back in place. We also discovered the source of much of the rattling noise we had grown accustomed to was actually change pieces trapped under the drum ribs. We removed them and put the ribs back in place and we installed the new belt and figured out how the belt routed around the shaft and tensioning pulley. We cleaned all the trapped lint out of the dryer and reassembled the unit. It now works like new. Thanks!
Parts Used:
Tumbler and Motor Belt
  • RIchard from New Era, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Initially the dryer made a loud rumble during startup, It progressed until the noise was continuous during operation.
Because of the nature of the noise, and knowing nothing of appliance repair, I assumed that there was a loose belt. I figured that the belt would be accessible from the rear of the machine. After much disassembly, I discovered that the belt was in fine shape and not the problem. But every time I spun the drum, I could still hear the rumbling sound. Eventually, I discovered that the from paned of the dryer is the easiest to remove. Once I removed that, I discovered the blower fan housing. A few screws later and I could see that the plastic fan center was worn out. I had a part number so I simply did a quick internet search and found several sites that stocked it. PartSelect had the best price and the best shipping prices as well. I placed the order on Saturday afternoon. I got the confirmation immediately, and the shipping information on Monday. On Wednesday the part was waiting at my door! It took about 15 minutes to re-assemble the dryer and now, about 18 loads later, it's perfect!
Thank you PartSelect!!!!
Joe G
Parts Used:
Blower Wheel with Clamp
  • Joseph from Ontario, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set
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All Instructions for the MDE13PDAEW
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