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LWC80AW Amana Washer - Instructions

All Instructions for the LWC80AW
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Water leaking on floor from "mysterious place underneath washer"
Water was leaking on the floor during the wash cycle and especially during draining of the washer. I removed the front panel at ground level and watched while draining after a rinse.

I t was obvious that water was spraying from a hole in the rubber end of the hose (the hose is a fused assembly of a plastic section and a rubber section).

So, I finished draining, removed the hose (required pliers to squeeze off a hose clamp).

Upon inspecting the hose, it was also apparent that the hole was caused by rubbing against a support bracket for the motor. This should not happen, but it did because the plastic standoff supposed to keep the hose away from the bracket was installed 180 degrees backwards.

So, I simply replaced the hose and turned the bracket around to the correct orientation.

Everything worked as planned and my repair cost was much less than if I had called someone out.
Parts Used:
Drain Hose with Rubber Elbow
  • Bryan from Chicago, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Socket set
50 of 55 people found this instruction helpful.
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The Seal On The Bottom Of The Tub Was Leaking
Removed the front of the washer, then lifted the top up and held it up with a prop. Pulled the agitator straight up and started the disasembly. Using the photos in the hub and seal kit was a big help. The large nut on the output shaft had to be cut off with my dremel tool and the hub removed with a wheeler puller. Assembly was pretty much straight forward. Primed the pump and started the machine for the stated time and was a sucess.
Parts Used:
Complete Hub and Seal Kit
  • HOWARD from CORTLAND, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench (Adjustable)
33 of 42 people found this instruction helpful.
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Bad shaking During Spin Cycle
firsted layed washer back On A Angle For Easy Acess To Motor Removed Both Hoses And Four bolts pulled Motor Assembly out replced belt @ idler Pulley Reinstalled Motor.
Parts Used:
V-Style Spin and Agitate Belt - 28-3/4 inches long Idler Pulley Wheel
  • Gary from Park Ridge, IL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers, Wrench set
35 of 53 people found this instruction helpful.
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Bearing went out causing lots of noise.
This is not a bad repair, but give yourself some time. I did not have to take the tranny and motor out, but the inner and outer tub and all related parts had to come out, along with the outer tub base. If you are replacing the tub bearing, you HAVE to order the seal kit. Don't try to skimp like I did, since you will need the seal kit as this is what causes that bearing to fail in the first place. We forgot how quiet the washer was after I fixed it, and it saved us from buying a new washer since we were ready to say the heck with it and buy a new pair. You might need an 1.5 inch socket to get the big nut off the spindle, but I was able to get with a visegrip and hammer. The nice thing about this repair is even if you screw it up, you won't have water all over the place because of the seal design. I just checked under the washer a few times for the first few weeks and all seems fine.
Parts Used:
Main Tub Bearing Assembly
  • mike from hull, IA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
24 of 26 people found this instruction helpful.
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Washer wouldn't drain
I was doing laundry one day, and noticed that the washer did not drain. I drained the water via a shop vac and checked the hoses. There was a baby sock stuck in the hose leading to the pump! I cleared the jam and the washer finally drained again. Once I ran another load, the washer wouldn't drain. I repeated the procedure, and found that the motor was spinning but the pump was not working. I disconnected the machine and proceded to remove the pump. I found that, due to blockage, the motor had reamed out the housing that turns the pump. So, at the advice of my father, who has used this site for other repairs, I entered the model make and number. I was able to view an exploded schematic of the washer in order to correctly identify the part I needed. I found the part, ordered it, and it came to me in about 2 days. I replaced the pump, and my washer has worked great ever since. Thank you PartSelect.com.
Parts Used:
Drain Pump
  • William from Fayetteville, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Socket set, Wrench (Adjustable), Wrench set
20 of 20 people found this instruction helpful.
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2 problems caused by bad brake discs
I first unplugged the washer. I removed the 2 screws that hold the front panel and removed the front panel, they are located at the very bottom outer edges of the front panel.
I then removed 4 of the large springs that are attached to the drum, this washer has six but I only removed the front 4. Removed the two hoses going to the water pump and drain hose, removed 4 bolts that attach the motor to its mounting bracket. Unplugged the wiring harnesses going to motor and what looks like a capacitor mounted to the side of the motor.Then I removed the drive belt. ( when the machine would first start to spin it would make a clacking noise which ended up being a chunk out the the drive belt causing the belt tenshioner to slap causing that noise and letting the drum spin during the wash cycle. So far very easy. I then removed the motor and when it is disconnected you can then remove the water pump. Three hex head bolts need to be removed and it pulls right off. I then removed the six bolts that hold the brake pads in place. I applied silicone grease to the new brake pads and installed them. The pad at the back of the drum was very hard to line up with the holes. I used a very small screwdriver to line up the disc brake mounting holes to get the bolts started and it worked fine. I then put it all back together and it works great. I have to add that I have been an auto mechanic for 28 years and not to brag but this is not your average repair job.
Parts Used:
Brake Pad Kit
  • daniel from angola, NY
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
18 of 19 people found this instruction helpful.
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tub leaking water
Took off the agitator, removed inner tub, exposing the hub drive. Found fusion between hub drive and agitator shaft. Rather than using a wheel puller as instructions recommended I got my masonry hammer and removed the drive hub in pieces. Removed debris from the tub. Installed sealant around lower seal as instructed. Re-assembled inner tub, agitator with new upper seal. Plugged in the washer, turned on the water. No leak. Happy happy.
Parts Used:
Complete Hub and Seal Kit
  • Raymond from East Sandwich, MA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Socket set, Wrench set
18 of 22 people found this instruction helpful.
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The washer tub seal leaked
After removing the agitator and drive bell by pulling on them HARD, I found that the lock nut and hub were corroded in place. I used grinding wheels to remove them which took over an hour. The internal and external threads needed to be cleaned up with tap and die and the splines had to be filed in order to get the new hub on the shaft. I did not use antiseize compound. The tub seal went on easily and the lock nut was guestimate torqued using a wrench made for water heater elements. The drive bell seal was very stubborn. It is normally pressed on with a special tool, but I had scrap pipe sections that fit the inner and outer press-points and used a large hammer to drive it into place. The washer does not leak any more. Total time was around four hours.
Parts Used:
Complete Hub and Seal Kit Lock Nut
  • Gerald from Seminole, FL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Wrench set
17 of 19 people found this instruction helpful.
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Washer wouldn't fill on hot selection, OK on cold
Remove the electrical power plug and disconnect the water hoses at the back. Remove the lower front panel by taking out the two screws at the bottom edge. Then lift out the upper front panel which exposes the two sheet metal screws holding down the top panel. Lift open the top panel and secure it up about 90 degrees so it doesn't flop over backwards. Twine tied to something overhead works fine. Replacement procedure for the valve is obvious, once exposed.
Parts Used:
Water Inlet Valve Kit
  • Charles from Vista, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
16 of 17 people found this instruction helpful.
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Did not know the hub nut hex wrench was needed till I got everything torn apart
I did as the directions said that came with the kit. Except everything came off by hand until I got to the hub nut. Instead of waiting for another shipment and buying a tool I would have used once and never touched again I called SEARS and a technician came to my house because I did not have the hub nut hex wrench. He called it a spanner wrench. Once he used the tool to get off the nut I was in business. Until I had to put the nut back on. I ended up wrapping a towel around the end of a 12" adjustable crescent wrenc and litle by little smacked it with a hammer until the nut looked like it was all the way down. Just to put the nut back on my way took almost an hour alone. The directions said that a puller was needed to get off the adjutator shaft (unsure of correct name), but it came off with a little wiggleing. Once I put the new one on it would not budge off so a small puller would have been needed to remove it if I needed to again. And puting it back on was a chore in it self. I ended up using a hammer and 6" 1/2" drive extension with a 20 something MM socket on the end to force it down all the way. And the shat that the large seal goes over also requires a tool which is also not mentioned until you read the directions. I was able to twist and force on the new one with a little bit of included grease around the meeting surface. For the most part the directions were correct, but left out a bunch of nice to know things that the average person who is not mechnically inclined may not have figured out. Overall the whole procedd was pretty easy once all the tools were available. Suggestions I would make are to say in the advertisement of the seal kit that the Hub nut hex wrech (spanner wrench) and seal tool will be needed inorder to complete the removal and/ or installation. Which are sold seprately.
Parts Used:
Complete Hub and Seal Kit
  • Robert from Yucaipa, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable), Wrench set
15 of 17 people found this instruction helpful.
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Leaked Water through lower tub seal
1st, I removed the top, back and side panels. Then removed the plastic parts off the top of the tubs. Next removed the agitator from it's hub. In the center of the agitator hub was a retaining bolt to be removed next using a 7/16" socket. Had to use a gear puller to get the agitator hub up off it's spline. Then there were four 1/2" socket size hex bolts to remove facilitating the removal of the inner stainless steel tub. Next was the toughest part of my task, the removal of the large hex nut holding the inner tub hub down. Since I did not have a socket large enough to fit the nut, I used a ball peen hammer to loosen it by striking it on it's hex flats in an angle that would tend to drive it in a CCW rotation. It took several blows but finally it began to loosen. Then removed it with my Channel Lock water pump pliers. Once the Inner tub hub was removed, the lower seal was accessible. Removed the old seal from the outer tub flange, and scraped off all the old sealant with a razor blade scraper. Then installed the new seal according to the instructions supplied with the new hub and seal kit. Re-assembled the washer, ran it through a cycle while it was still out in the garage to ensure the leak was fixed and was happy to find that indeed it was. Everything went fairly well if you overlook the slight cut on my right thumb I suffered while re-assembling the covers. It wasn't too bad, a band aid fixed it up.
Parts Used:
Complete Hub and Seal Kit
  • John from Greenup, IL
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable)
14 of 15 people found this instruction helpful.
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The agitator moved in slow motion at regular setting
took off the front cover.
disconected the wiring from moter.
removed the motor.
replaced the brake pads one at a time used a flat screw driver to spred the plates apart.

The Plasatic Helix Drive Lup
took bolt at the botom of shaft off
this released the Helix drive lug.
took old lug off and inatalled new
replaced bolt and washer.
Parts Used:
Brake Pad Kit Plastic Helix Drive Lug
  • Alvin W. from Reidsville, NC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Wrench set
13 of 13 people found this instruction helpful.
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Squeak and slight burning smell during spin cycle.
I took off the lower front panel and “watched” with a flashlight during the spin cycle. I could see that the idler pulley was intermittently stopping and starting. The back of the drive belt was also worn in the center. When the idler pulley was moving, it squeaked, when it didn’t, the friction wore the belt and made the smell.

To replace the Idler Pulley Wheel:
1. Take off the lower and upper front panels to access the motor assembly.
2. Remove motor by loosening four bolts.
3. Remove spring that applies tension to the idler pulley.
4. Remove the electrical connector by squeezing the plastic tab on top.
5. Remove hoses by gripping clamps with pliers (put down rags first to catch water)
6. Unhook belt from tub pulley
7. Remove 1 cabinet spring to make it easier to remove motor
8. Remove motor.
9. Remove allen screws holding the pump to the motor
10. Remove the pump and belt (take note of the location of the belt before removing).
11. Remove retaining ring to replace Idler Pulley Wheel (this was probably the trickiest part; I used a very tiny needle nose pliers and straight screwdriver).
12. Replace the washers on either side of the Idler Pulley Wheel as well as the retaining ring.
13. Replace belt.
14. Reassemble in reverse order.
15. Be thankful for the money you saved on a service call.
Parts Used:
Idler Pulley Wheel V-Style Spin and Agitate Belt - 28-3/4 inches long Retaining Ring Thrust Washer
  • Jim from Swanton, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
13 of 15 people found this instruction helpful.
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Washer began to leak about a pint of water per load. Water was stained black by residual belt abd brake dust the water was picking up as it dripped throught the machine.
I followed the instructions that came with the hub and seal kit, which were pretty well written but not terribly detailed. Once I got into the job though, I felt confident that the instructions told me all of the important information--the rest was common sense. If you're reasonably handy you can pull this off.

The instructions call for some specialty tools, which I was able to do without by using the following:

• Drive Bell:
The old drive bell slid right off without a puller--I think I got lucky on this one.

To install the new drive bell I used a long 1/4-20 bolt, nut and fender washers. I spun a nut way up the bolt then slid the fender washers on. I threaded all of this down into the transmission output shaft until it bottomed out. Then I turned the nut down to push the washers and drive bell down until it hit bottom. Then I backed out out the bolt and washers and installed the shoulder screw.

• Hub:
I used a generic wheel-puller I already had to get this off and it came off with little effort. I put the old shoulder screw back into the top of the shaft for the point of the puller to sit on so it wouldn't mess up the transmission output shaft or threads (obvious, I know but a bad thing to overlook).

Drive Bell Seal:
• This calls for seal tool #293P4. I'm sure the seal can be installed by hand but it happened that the two extension tubes from my Shop-Vac were exactly the right diameters to seat the bottom and top parts of the seal.

• Lint filter:
The instructions just say "remove lint filter" but it was pretty stuck on and seems pretty fragile so I took it easy. I used a small scrap of 1/8-inch plywood to slide under the edge until it popped off.

The instructions say not to use the four rubber washers on the bolts that attach the inner tub to the hub if the machine has a stainless tub. Mine has a stainless tub and the original bolts had rubber washers on them so I used the new washers when i reinstalled the inner tub.

I found the 3M-800 Scotch Seal industrial sealant at a local appliance pats distributor. I researched it and it seemed like a specific enough product that it wasn't worth risking the whole job to use something I already had like Lexel. I learned that the reason it doesn't come with the kit is that it requires Haz-Mat handling, which would probably double the cost of the parts kit. One set of instructions I read from Maytag said that "the customer can use the machine after 15 minutes". But the sealant tube says it fully cures in 1 - 3 days. So I squirted out a ribbon on a piece of paper when I did the job so I could monitor the drying time and split the difference, allowing it to dry overnight. Seems as though that's long enough.

I did the job step-by-step and it seems to have worked. The first load is running right now and so far it's dry as a bone.

One thing I noticed is that some of the parts seem to have been updated over the original ones to improve performance. The drive bell and associated seal have a more sophisticated mating relationship that seems as though it will provide a better seal than the original.

Good luck
Parts Used:
Complete Hub and Seal Kit
  • Sheldon from North Yarmouth, ME
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
12 of 13 people found this instruction helpful.
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Seal on water pump was leaking
Unplug the washer to prevent shock while handling motor. Remove the front botton access panel. Move the drive belt off the idler pulley to provide slack to move belt off the other pulleys. Note position or take picture of belt position before removal to aid in getting it in the correct position for reinstallation. Move the hose clamps up the hoses far enough to remove the hoses from the pump. A towel is handy here as there is still a little water in the hoses and pump. Remove the four bolts holding the motor bracket to the bottom of the washer. The wiring to the motor does not need to be disconnected. Rotate the bracket with motor and pump attached so that the assembly is horizontal and the pump is to the right hand side. Use the torx bit to remove the bolts holding the pump in place. Install the new pump, being careful to get the drive belt in the proper position while doing so. Do not over tighten the bolts on the new pump since it is plastic. Rotate the motor bracket back to its original position and install the four bolts. Get all four bolts installed loosely before tightening any fully to insure the bracket is aligned properly and none of the bolts will be in a bind. Once the bolts are tight, put the drive belt on the small pulley and then work in around to position on the large pulley. Position the belt back into its position on the idler pulley. Put the hoses on the pump as far as they will go then slide the hose clamps back into their original position. Replace the bottom access panel and plug the washer back in.
Parts Used:
Drain Pump
  • Douglas from Spring, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Socket set
10 of 10 people found this instruction helpful.
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All Instructions for the LWC80AW
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