Models > LNC6766A71 > Instructions

LNC6766A71 Admiral Washer - Instructions

All installation instructions for LNC6766A71 parts

These instructions have been submitted by other PartSelect customers and can help guide you through the washer repair with useful information like difficulty of repair, length of repair, tools needed, and more.

All Instructions for the LNC6766A71
31-45 of 324
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Washer made grinding noise then stopped working.

  • Customer: David from Honesdale PA
  • Difficulty: Easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Nutdriver, Pliers
  • 13 of 14 people found this instruction helpful
First I tipped the washing machine onto its front. I removed the belt on the bottom of the machine. Then I removed the screws that held the cover in place on the back of the machine. Next I removed the two hoses that were connected to the vertical pump using pliers to pinch the clamps. I then removed three screws that held the vertical pump in place. I took the new verticle pump with pulley and mounted it to the washer and putting the washer machine back together using the previous steps in reverse order.

terrible screeching during agitation after having washer only 3 months

  • Customer: stephen from soddy daisy TN
  • Difficulty: A Bit Difficult
  • Time to Complete: More than 2 hours
  • Tools Required: Nutdriver, Pliers, Screw drivers
  • 15 of 20 people found this instruction helpful
First I disconnected the hoses and moved washer out to a larger area. Washer had to be completely torn down. Took front cover and casing off. Took all electrical and plumbing fixtures out. Removed the drum hold-down springs. Removed the drive belt. Inverted the drum/agitator section. Removed the drive pulley and bearing assembly. Removed the brake snubber. Removed the brake shoe. Reinstalled new parts. Put washer back together. It now works great.

Washing machine sqeeling to a stop after spin cycle

  • Customer: William from Middletown OH
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Nutdriver, Screw drivers
  • 13 of 16 people found this instruction helpful
By sliding the machine out away from the wall I tipped it back so that it set against the wall on an angle enough for me to work on the bottom. I removed the belt and drive pully. The brake stator can be removed from the bottom if drum is centered. The brake is under pressure from a big spring in there that applies the brake. Replacing three of its mounting screws with longer ones (10-24 x 2) allows you to let pressure off of the brake spring slowly. Replaced brake rotor and stator and compressed spring with long screws as in removal. Replaced all original screws to hold in place. Installed pulley and belt. Works like brand new, all for about $30. I bought the snubber also but did not realize that this is not part of the brake. I little confusing on the parts drawing.

Water overflowed from tub onto floor

  • Customer: Dan from Lombard IL
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Pliers, Screw drivers
  • 11 of 11 people found this instruction helpful
The problem was not in the switch but in the plastic hose from the tub to the switch. The hose was cracked and air/water leaked which therefore didn't activate the switch. I removed the top back cover to access the switch and released the hood of the machine, like a car, using a thin scaper to depress the spring loaded retaining clips. The hose was cracked at the tub just above the retainig clip. I bought new hosing at a local hardware store and replaced the switch to omit both of them as a future problem. Sell the tube with the switch as a package deal? Damage to tube may occur from violent, out of balance, spinning tub on spin cycle.

washer wouldn't spin

  • Customer: Elmer from Fort Campbell KY
  • Difficulty: A Bit Difficult
  • Time to Complete: More than 2 hours
  • Tools Required: Screw drivers, Socket set, Wrench set, Wrench(Adjustable)
  • 12 of 14 people found this instruction helpful
I took out all the tubs and the apparatus holding the gear and thrust bearing assembly. I used a homemade tool (long zipties) to pull the springs off and to put them back on. After that I just replaced the thrust bearing with the new kit and put everything back together.

Water would not stop filling

  • Customer: Hing from Toms River NJ
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Nutdriver, Pliers
  • 12 of 14 people found this instruction helpful
1. Unplug power cord.
2. Move washer away from the wall to get access to the back of the control panel.
3. Remove 5 screws from the back panel cover with 1/4" driver, & remove cover.
4. Pull the Water Level Switch knob out from the front control panel.
5. Use pliers to slide away the retaining clip holding the clear rubber tube to the water level switch, & separate the tube from the switch.
6. Use 1/4" driver to remove 2 screws holding the switch, & remove the switch.
7. Remove the electrical wires
8. Install new switch in reverse order.

When you are testing out the washer afterward & your spouse said still not fixed because she thought the water level is too high when the water is still running? Wait a little while longer, the water should stop. She is just not used to see it filled without a load of laundry in it.

Washing machine beat itself to death during spin cycle

  • Customer: John from Cumberland MD
  • Difficulty: Really easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Socket set
  • 12 of 15 people found this instruction helpful
Removed front cabinet, removed 6 springs holding tub down, removed pump hose, removed drive belt from motor,lifted tub out the top and placed upside down, loosened all six hex bolts(did not loosen or remove drive pulley) backed all six bolts out and left 4 threads showing, slipped old snubber out cleaned all surfaces with alchohol and slid new snubber in. Put corn starch on base where snubber rides, lifted tub back in, hooked up all six tension springs with auto brake tool.put belt back on...done..no more beating itself to death.

Pump was leaking

  • Customer: Christopher from Westwego LA
  • Difficulty: Really easy
  • Time to Complete: 15 - 30 mins
  • Tools Required: Nutdriver, Pliers
  • 11 of 13 people found this instruction helpful
I felt extremely confident when purchasing the part because I say three diagrams which clearly showed I was ordering the correct part. 0. Drain all of the water out of the machine. 1. Remove the rear panel from the washer. 2. Use the pliers to disconnect the hoses from the pump. 3. Remove the three screwa from the old pump. 4. Support the washer with the block then take the belt off pulley. 5. Remove old pump. 6. put new pump in place then reconnect the pulley, you can remove the block.. 7. Install the three screws for the pump after you tighten it up by placing the pump over ther correct screw holes.. 8. Reconnect the two hoses using the clamps you removed. 9. Secure the rear panel and screw in place. 10. Wash clothes. EASY FIX!!!

Clothes were too damp after spin cycle finished.

  • Customer: Brian from South Holland IL
  • Difficulty: A Bit Difficult
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers
  • 11 of 14 people found this instruction helpful
Unplugged and removed the drain and supply hoses from the back; some water will run out so be ready for that. I laid the machine down on two 2x4s to keep from crushing the supply and drain nipples. Just follow the instructions included with the parts, all steps are straight forward accept for two things: 1. they talk about pulling down on the transmission shaft to slip on the retaining clip. With only the end of the shaft sticking out there isn't much to grab on to. I found by using a thin blade scraper inserted into the retaining clip groove, prying downward on the shaft I could then get a regular screwdriver blade into the same groove and expose the entire groove and slip on the clip. 2. they talk about "Adjusting Brake Disengagement" after studying this for a while it just refers to which thickness of thrust washer to use. After trying both the .062 and .032 I found that only the .032 would allow the retaining clip to engage. Rechecking the brake disengagement, everthing seemed to work fine. The machine now has a stronger spin cycle and even bath towels are ready for drying after the normal spin.

Washer leaked entire load of water on the floor.

  • Customer: Kevin from Wilton CT
  • Difficulty: A Bit Difficult
  • Time to Complete: 1- 2 hours
  • Tools Required: Pliers, Socket set
  • 9 of 10 people found this instruction helpful
These gaskets and seals were relatively easy to get to. I replaced all 3. Put machine back together, but washer still leaked. I ended up having to remove more components down along the center shaft towards the transmission. I found that the "tub seal" was worn out. I also replaced the "seal nut assembly" and "O-ring" while I was at it. The seal nut and tub seal were more difficult to remove without the proper tool, but a bigger rubber mallet and strategically placed pliers were enough to break them loose. Once all parts showed up the washer went back together easily and it is now leak-free.

water pump was noisy

  • Customer: Patsy from Brookfield, MO
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Screw drivers, Socket set
  • 9 of 10 people found this instruction helpful
Removed the front panel, Removed the belt from pump in the back of machine. Removed the pump from the back of machine, Put the pump in reconnected the belt, Replaced all the screws. My husband did the repair work in a matter of 45 minutes. Machine works fine now. The part came when I was told it would. I am very pleased with your service.

agitator kept coming off during spin cycle

  • Customer: Dara from Demarest NJ
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Socket set
  • 12 of 19 people found this instruction helpful
After using my existing parts for about 6 months, and constantly having to tighten the bolt, I though that the parts might be stripped. It took one minute to unscrew the bolt that holds the two parts of the agitator together with a socket and 10" extension. After taking those parts off, it took another minute to put the pieces back and screw the new bolt back in place. Extremely easy - and much less expensive then having a repairman come out to fix it.

Washer was shaking and noisy, wasn't spining fast and overall running poor.

  • Customer: joseph from columbus OH
  • Difficulty: Easy
  • Time to Complete: 1- 2 hours
  • Tools Required: Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
  • 9 of 11 people found this instruction helpful
The hardest part of this is the springs. The best way to disconnect and reconnect was to tilt the tub towards the spring I was trying to work on (thus putting less tension on the spring and cutting down the distance). I took a large boot and jammed it into the oposite side wall to hold it in a tilted position before I disconnected the spring and then redid that to reconnect using a vice grip wrench. I replaced all three things, snubber, brake roto and stator and it went back together very easily. The key on the pully shaft was hard to reattach but there was a trick to that as well. The shaft has to move up slightly to slide ring on so you need to have something under the tub to help raise it. After that was back together it was 15 mins. to finish and now the washer is running like new.

High pitched screech from brake at end of spin cycles.

  • Customer: William from Lithia FL
  • Difficulty: Easy
  • Time to Complete: 30 - 60 mins
  • Tools Required: Pliers, Screw drivers, Socket set
  • 8 of 8 people found this instruction helpful
I disconnected and moved the washer into the garage for optimum work space. Then I opened the top panel (by releasing the two retainer clips between the top and front panels with a putty knife inserted approx 2" in from each side) and taped a spacer block between the back of the tub and the back panel of the washer, to keep the tub from moving toward the back when the washer is tilted.

Then I tilted the washer back against my 2 1/2' high workmate bench (backstopped against the wall). After adjusting the tilt angle to provide adequate access to the bottom of the washer and insure it was was beyond the forward center of gravity, I began the repair.

Working from the bottom, I first removed the drive belt. Then the white dust cap, shaft retaining ring, plastic cam, pulley, and the various washers and bearings leading up to the brake assembly, making note of their order.

Then I removed three of the six 1/2" 10x24 brake stator retaining screws at alternating positions replacing each with one of the three 2" 10x24 screws I had previously purchased the hardware store. Then I removed the three remaining 1/2" screws, and slowly began to remove the three 2" screws alternating a few turns on each in rotation to evenly ease the 200 pounds of pressure from the brake rotor spring.

When the pressure was released, I removed the old brake stator and rotor and placed the new ones on the shaft, then re-compresed the brake rotor spring with the three 2" screws in alternating positions. Then placed three of the original 1/2" screws in the threee open positions, then replaced the three 2" screws with the remaining three 1/2" screws.

Then I reinstalled the remainder ot the parts in reverse order of removal.

Machine was very noisy, tub spun slowly when loaded & lid switch actuator was broken. Drive belt had very little tension on it.

  • Customer: Larry from Smithville MO
  • Difficulty: Really easy
  • Time to Complete: Less than 15 mins
  • Tools Required: Screw drivers, Socket set
  • 12 of 20 people found this instruction helpful
Remove the access panel at the back of the machine. Locate the Motor Pivot Spring. It is about the same diameter as a coat hanger and is attached to the motor and the motor base. I was able to remove the old spring and install the new spring with my fingers. When removing the old spring, remove the motor end first, then the motor base end. When installing the new spring, attach the motor base end first, then the motor end.
All Instructions for the LNC6766A71
31-45 of 324