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LDE7304ACE Maytag Dryer - Instructions

All Instructions for the LDE7304ACE
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Broken Catch
Watch the video. Very, very easy
Parts Used:
Door Catch Kit
  • James from LARAMIE, WY
  • Difficulty Level:
    Very Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Nutdriver, Screw drivers
4 of 4 people found this instruction helpful.
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Squealing noise on start up.
I opened the back acess panel and started the dryer. Looking at the motor and idler pulleys it was obvious by the frequency of the squealing noise that it was coming from the idler pulley.
I pulled the retainer clip and tension spring from the idler pulley and removed it. I applied some grease to the shaft and reinstalled the idler pulley.
The squeal was gone confirming that the pulley bushing was dry. I ordered the new idler pulley and when it arrived the next day I cleaned the grease off of the shaft and installed the new idler pulley. Problem solved.
Parts Used:
Idler Pulley Wheel
  • William from Winter Park, FL
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Screw drivers
4 of 5 people found this instruction helpful.
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Heater ran constantly, except in air fluff cycle, thus operating extremely hot
Removed the frong cover and and internal sheild, removed and replaced thermostatic, wiring as original.
I had searched several other sites first for thee part, but none of them seemed accurate. Your photo matched the old exactly, giving me the confidence I wanted before ordering.
Parts Used:
Multi-Temp Cycling Thermostat with Internal Bias Heater
  • Charles from Mount Storm, WV
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
6 of 11 people found this instruction helpful.
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Loud, rumbling noise
1. Removed two screws from front panel.
2. Removed panel.
3. Removed four bolts off tumbler face.
4. Removed face.
5. Removed drum and belt.
6. Vacuumed.
7. Replaced idler spring assembly.
8. Replaced drum.
9. Replaced belt.
10. Rotated drum to make sure belt was properly seated.
11. Replaced tumbler face.
12. Replaced front panel.
Parts Used:
Tumbler and Motor Belt Idler Spring
  • Francis from Half Moon Bay, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
5 of 8 people found this instruction helpful.
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Door wasn't staying closed
popped up top of dryer -- With pliers squeezed clips on inside of latch - - with screw driver pryed latch out -- just pused new latch in.......... Thanks to parts select for sending part sooo fast.. wife was happy.. Thanks, Dale
Parts Used:
Door Catch Kit
  • Dale from Livingston, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
4 of 5 people found this instruction helpful.
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No Heat
Insure the double pole breaker in the breaker box is functioning properly.
Parts Used:
High Limit Thermostat (Limit: 200-30)
  • Mark from Napa, CA
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers
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Very noisy.
My first attemp was to replace the drum roller and idler roller, drive belt, and the felt seal for the back, since I had experience replacing these on an older machine many years ago. The dryer was very easy to work on....After installing the new parts, I reassembled and discovered it still made the same loud noise. I then, disassembled for the second time to discover the blower wheel was worn out; so i ordered another blower wheel and a drum support roller (i only ordered one the first time.). After reassembling it made an annoying high pitch sound. I attributed that to the new parts...probably the new belt and new felt seal. Gave it some time to run-in and it seems to have quieted down. Overall, i found the dryer very easy to work on. I actually found the felt seal the most onerous to install....needed to have about three hands to get the drum back in place! I just wish that the stamped metal dryer housing didn't have such sharp edges. I had to be very careful to avoid sharp burrs but still got nicked a couple of times.
Parts Used:
Idler Pulley Wheel Tumbler and Motor Belt Front or Rear Drum Felt Seal Drum Support Roller Kit
  • Benjamin from Baton Rouge, LA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
4 of 6 people found this instruction helpful.
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lint filter was frayed
used a utility knife to open the box in which the part was shipped, discarded the old filter and inserted the new one
Parts Used:
Lint Filter
  • Alan from Pacific Palisades, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
3 of 3 people found this instruction helpful.
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drum support roller had come apst from bearing and was making a squealing noise when dryer was running
first i removed the screws holding back cover. Then I remeved nut from tumbler roller shaft. Then I slid shaft from roller .I removed roller then replaced with new one. Installed new shaft then replaced back cover. recieved parts from parts direct very promptly & they were the right parts the first time thanks very much
Parts Used:
Roller Shaft Drum Support Roller Kit
  • David from Calvert City, KY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Pliers, Wrench set
3 of 3 people found this instruction helpful.
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Loud noises, primarily a shrill shreik
From the noise level and info on this site, I assumed I needed to replace the drum rollers. I ordered two, along with the Roller Shaft, and a replacement belt (I assumed that would eventually need to be replaced so why not now).
No need for me to repeat the excellent reviews/instructions already on this site. Basically, it was an easy job that took about 2 hours, mostly because I took the time to clean every nook and cranny I could find.
Once I assembled it back up, the shriek was gone but the rumble noise was still there. I now realize that the blower wheel must have a worn out d-hole that mates with the motor shaft. So, I will have to order that part, get it installed and I am confident that I will have a "new" machine once that is in place.
Parts Used:
Tumbler and Motor Belt Roller Shaft Drum Support Roller Kit
  • Robert from Glastonbury, CT
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Wrench (Adjustable)
3 of 3 people found this instruction helpful.
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Replaced door switch
Door switch was very easy to replace as it simply snaps in for the outside and you just clip on the two control wires that already have clips on them.
Parts Used:
Door Switch Kit
  • Joseph from Colts Neck, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
5 of 9 people found this instruction helpful.
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Dryer tumbler did not turn, dryer still turned on, dryer still produced heat : diagnosis broken tumbler belt..
I looked for dryer repair videos on my computer. I found several and they all showed me that what was most likely broken was the tumbler belt. I didn't even know dryers had a belt. My dryer still turned on,and still produced heat. It just wouldn't rotate. One of the videos even used the exact Maytag dryer in their video that I had. After watching it a few times, I knew I could make this repair. I am pretty good at fixing things if I can first see it done. I had never taken a dryer apart before though. I pulled the dryer away from the wall and unplugged it. I unscrewed the small access panel on the back of the dryer. This let me see the two belt pulleys back there. Then I went to the front and removed the two screws(my particular model) that held the front panel on and removed it. I then unscrewed the four screws holding on the front face plate in front of the tumbler. Next, I pulled the tumbler out, it is not screwed in. There was the broken belt. It took two days with regular shipping for the belt to come in. I put the tumbler back in, resting it on its two supports, placed the belt on, flat side down, and routed the belt through the pulleys in the back of the dryer exactly as it had been shown in the videos. I turned the tumbler clockwise two full rotations by hand to make sure the belt was seated correctly on the pulleys, and it was. I then screwed the face plate back on in front of the tumbler, put the front panel back on and screwed it in. I then reattached the back access panel. I plugged the dryer back in and turned it on. It worked. Though it may take a bit longer, this type of repair is about as easy as replacing a broken belt on a vacuum cleaner even for someone who has never done a dryer repair before. Watch a Repair Clinic video and if you enjoy fixing things, replacing a belt on a clothes dryer will be your next successful repair. It really is pretty easy.
Parts Used:
Tumbler and Motor Belt
  • Robert from Somers Point, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
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After a period of the dryer not being used, the idler pulley wheel froze up on the shaft of the idler pulley arm.
This should have been a simple repair, but turned out to be time consuming and moderately difficult. I hope these instructions will help anyone who encounters the problems described here.

After a period of the dryer not being used, the idler pulley wheel froze on the shaft of the idler pulley arm, so I needed to replace both parts. After mounting the new wheel and two washers on the new arm and securing with a retaining ring, I went to install this assembly by going in through the small access panel at the rear of the dryer. I slid the belt off the old idler pulley wheel and unhooked the spring from the idler pulley arm; the arm was mounted on a sleeve fastened to the motor bracket by one screw. All that should have been necessary was to back out that screw and replace the old idler pulley assembly with the new one.

That is where the trouble started. Backing out the screw with a socket driver, I found it would go a few turns, then start to bind. I tried turning it in and out to get the threads to engage, but it kept binding. Eventually I gave the screw a hard turn, and then it would turn freely but not move in or out.

Looking on the internet for advice, I found a video that asserts for another model Maytag dryer using the same type of mounting for the idler arm, that there is a design flaw. You can find the video by searching for “Maytag dryer idler pulley defect”. According to the video, the sheet metal screw used to mount the idler pulley arm can gradually loosen due to the pressure and vibration, and begins to “waggle” which eventually damages the threads. I believe this is what happened to my dryer. The video suggests replacing the sheet metal screw with a machine screw and nut for a more durable union.

So now I understood how the screw could be stripped just sitting in the dryer, but that didn’t help me get the screw out. Working through the rear access panel, I tried pulling on the screw head with several types of pliers, pushing the point from behind with a piece of wood while turning the head with a socket driver; eventually I was able to use a pry bar under the screw head and sleeve to apply pressure while turning the head, and with that method the screw backed out. With the screw removed, it could be seen that the threads in the middle part of the thread length were almost completely worn away.

The screw sleeve got somewhat deformed in this process so I ordered a new one, along with an exact replacement sheet metal screw, hoping the threads in the hole were still intact. With the old idler pulley arm now removed, I could transfer the old idler bracket spacer to the new idler pulley arm. When the ordered parts arrived and I tried to mount the idler pulley arm, the new screw would go in only a couple of turns before binding. Rather than risk winding up in the same situation by forcing the screw, I decided to use a machine screw and nut instead.

The original sheet metal screw was a #10. A machine screw the same size would not fit through the hole, and I could not fit my drill into the dryer cabinet in a position to enlarge the hole, so I used a #8 machine screw with a nut and lock washer. First I put some grease on the contact areas of the screw sleeve and idler bracket spacer, then inserted the machine screw through the hole and put the lock washer and nut on the other side of the mounting. The space around the nut is very limited, and most of my tools were too large to hold the nut while the screw was tightened. It was too small for a socket or adjustable wrench, and the clearance from the exhaust duct was too small for the handles of most tools. Eventually, I found a needle nose pliers with short handles that did the job. A thin open end wrench might also work. Then I reconnected the spring and belt to the idler pulley assembly, and closed the access panel. So far the dryer works, but if the #8 screw turns out to be not strong enough, I could get an extension for my drill and enlarge the hole to fit a #10 machine screw and nut.

Looking back on the job, the most difficult part of this repair was removing the damaged screw. This and several other steps might have been a lot easier if I had removed the motor bracket (where the idler pulley arm is mounted) from the dryer and worked outside the cabinet. Part Select has an excellent video “Replacing the Drive Motor” that shows how to do this. It would be a lot of disassembly work, but for someone with good assembly skills could be easier in the long run.

Hopefully most folks out there who replace the idler pulley arm on a dryer will find an easier situation than I did. But for any who have to deal with a stripped mounting screw, I hope this summary will help you resolve it.
Parts Used:
Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm
  • Alan from BETHESDA, MD
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Noisy Dryer operation and eventually no air movement through dryer
Every two to three years, the blower wheel gets chewed out in the center where it attaches to the motor shaft. I have learned the sound of it starting to rattle so I know to order a new blower before the air stops moving altogether. Replacing it is very easy if you have tiny sockets or nut drivers and a pair of snap ring pliers.

When working on this dryer, be aware that the heater wires are always "hot", even when the dryer is not running. You are only likely to touch one at a time so the worst you will feel is 120 volts. The shock probably won't hurt you but you may cut yourself jerking your arm out of the dryer. Best to unplug the dryer or open the circuit breaker before sticking your arm in there!
Parts Used:
Blower Wheel with Clamp
  • Russell from ELK GROVE, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
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old was belt stretched and idler pulley gummed up, drum won't tumble a normal sized load
Replaced all the parts per the very good video provided on the website.
I recommend watching the video very closely several times. BE SURE THE BELT IS NOT IN THE DRUM'S GROOVE. The video mentions this very very briefly; I caught it on my third viewing. If your belt is not the correct location, it may still turn the drum for you - and eat the belt up in about an hour.
Parts Used:
Tumbler and Motor Belt Idler Pulley Shaft Washer Idler Pulley Wheel Idler Pulley Arm Idler Arm Screw Sleeve
  • William from ORANGEBURG, SC
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Screw drivers, Socket set
3 of 3 people found this instruction helpful.
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All Instructions for the LDE7304ACE
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