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KAWS855JE0 KitchenAid Washer - Instructions

All Instructions for the KAWS855JE0
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Water drips inside washing machine, suspected the inlet valve needs to be replaced
Before ordering part, took the old valve out to make sure it looks similar to the one described online by Partselect. After ordering online, put things back together since I expected delivery would take 5-7 days. That night the water stopped dripping and has been OK ever since. I suspected that there was some rust in the electrical connections. By disconnecting and reconnecting the terminal, the electrical connection is better and water stopped dripping. Still keep the new part just in case (which came overnight after I ordered it).
Parts Used:
Water Inlet Valve with Mounting Bracket
  • PHU from Laguna Hills, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Screw drivers
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The washer wouldn't spin or agitate.
Frist I disconnected the water lines and power cord. Then I leaned the washer back against the wall. Removed the 2 pump retainers and then the pump. Next removed the 2 screws from the motor retainers and pulled off the retainers and motor. Then removed the 3 bolts from the Gear case. Then removed the cap from the top of the agitator with a flat screw driver. Then removed the bolt from the top of the gear shaft. and removed the auger and agitator assembly. Then removed the gear case from the washer. Next removed the slip ring and then the clutch from the top of the gear case. Next removed the 1/4" screws from cover of gear case and removed the cover. Found the top gear bad. Ordered the new gear and pinion kit. Couldn't find any part #'s to match what PartSelect had. Ordered the gear that they should that fit most washers. The pics they had up looked the same as the one that was bad. Had the new gear in 3 days put it back together and it still wouldn't work right. Took it apart again and looked at it and found a small clip on the bottom side of the gear was upside down. Fliped it over put the gear back in and ran the washer with the gear case out and it worked. Put it back together again. And learned a good lesson always watch how you take things apart for when it's time to put it back together!
Parts Used:
Gearcase
  • david from Monroe, MI
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set
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Some of the teeth on the gears within the gear case stripped. And also, some of the agitator clutch parts were warped (they were plastic).
I'm not the one who actually did the repair, so I can't give you a blow-by-blow description. But my friend did the actual repair (I found and ordered the parts from your web site).

There was one almost insurmountable problem, however. The three-pin cog that connects the new gear case to the rest of the washing machine was changed.......the cross-section of each of the cogs was not round.....but teardrop shaped. I ordered the correct gear case, based upon the model number of the machine, but apparently somewhere down the years Whilrlpool must have changed the cog profile design.

So, the man who did the repair simply got out a metal mill file and filed down each of the cogs so that they were round. It wasn't perfect, but it worked.
Parts Used:
Gearcase Agitator Repair Kit
  • John from Upper Montclair, NJ
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers, Wrench (Adjustable), Wrench set
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Washer wouldn't spin or agitate. Made louder-than-usual noise during those cycles.
1. Read many other repair stories for similar symptoms. PartSelect Forum was an excellent resource.

2. Posted my problem on PartSelect Forum and awaited reply. Read replies, and followed provided link to step-by-step guide for the procedure. PartSelect forum moderators were excellent advisors!

3. Performed the first half of the procedure to get to the diagnosed root cause. In some of the stories I had read, people had turned the washer on its back or tilted it up to get at the area from underneath. I am so glad I followed the conventional instructions, and left the washer standing and simply removed the cabinet. It was surprisingly easy. There's a reason why it was designed that way. I am also glad that I chose to remove the pump from the motor. While it is true that you don't *have* to remove the pump from the motor to get at the coupling...it hardly seems to make sense to remove the hoses instead. Removing the pump was incredibly easy, and by doing so, I never had to break any "wet" connections, and not one drop of water spilled over the course of the entire repair. (Even though I forgot to shut the water supply valves before I got started. Ooops! At least I remembered to unplug the power cord.)

4. But despite the open valves, the galoshes came into play not for their ability to repel water, but for their value as an electric insulator. I wrapped the galoshes around the handle of a long screwdriver when I discharged the motor's capacitor. :)

5. Ordered parts. Washed clothes in sink. Waited. Washed more clothes in sink. Waited some more. Washed more clothes in sink. Waited still more. Came very close to stopping payment to PartSelect because the very simple, commonly-requested part I ordered, which was supposedly in stock on the day I ordered it, didn't ship until the day it was supposed to arrive--even though I paid extra for expedited shipping. And I was never sent an e-mail to warn me that the parts were going to be delayed. And then to top it all off, rather than make up for some of the lost time caused by their own error, and ship it overnight, PartSelect chose to ship it 2nd day. All that good will generated by the excellent website completely evaporated by the failure to correctly complete the simple tasks that the business has needed to be good at since before computers were even invented. I will never use PartSelect again.

6. Prying the old coupler halves off of the motor and the washer took some effort, but was not overly difficult. I wound up removing the motor mounting plate in order to get better access to the half that was stuck on / needed to be attached to the drive train of the washing machine. Mounting plate was a breeze to remove and attach with a socket driver. I used one of those stubby flat-head screwdrivers to pry the old parts off. This was the one time where I thought it might have been easier to have the washing machine tilted up or on its back...but I muddled on through without even removing the bottom panel, and it wasn't too awkward. I used a large socket and a full-size hammer to not-so-gently tap the new parts into place. Putting all of the parts back together took a bit longer than it took to break them down, but it was easy. The instructions for putting the electronic control panel into test mode had been rolled up and taped to the cabinet inside the top panel. After I put the cabinet back on, I used those instructions to test all the cycles before fastening the top panel and testing the machine with an actual load. So far, so good...
Parts Used:
Direct Drive Motor Coupling
  • Paul from Boonton, NJ
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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No fabric softener dispenser
Pop the center cap off the agitator and snap the dispenser in. Easy as 1-2-3.
Parts Used:
Fabric Softener Dispenser
  • Dennis from Port Orchard, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Slow hot water, cold water was flowing normal.
First I disconnected power.

Next I turned off the hot and cold water supply hose bibs.

Once that's done, I pulled out the washing machine to get to the hose connections on the back of the machine, removed and drained the residual water in the hoses.

Note: Since the hoses were fairly new, I reused the supply hoses but replaced the rubber washers. However, if your hoses are older than a couple of years, it's cheap insurance to go ahead and replace since you're right there.

Next was to remove the two end caps of the control unit on top of the machine. This exposes the two screws that is then removed so that the control panel can rotate up and back.

Once the panel is open, I removed the single connector attached to the top of the machine. This leads to the lid open switch.

Followed by removing the two spring clips with the help of a flat blade screwdriver and pliers to keep the clips from flying off.

Once the clips are removed, the top/front shell of the washer is free to rotate foward. At this point, it can be removed or just laid to the side (forward).

This opens up the area to be serviced.

Disconnect the quick release wire connectors, taking note that the red connector is for the hot water control valve solenoid. disconnect the mix hose going to the tub from the valve by using pliers to disengage the hose clamp (catch the residual water with a sutable container). Then I removed the old valve assembly by removing the two screws holding the assembly to the back panel.

Follow the instructions enclosed with the part to preassemble and install the valve.

Reassemble by reversing the process. Check for leaks, test hot and cold water cycle and you're done.

It actually took me more time to gather my tools and pull out the washing machine than the actual replacement of the part!

Oh, by the way, I've purchased parts from PartSelect.com many times. Each and every time has been an outstanding experience. Quality parts, fast shipping and great prices! It's always been a pleasure!
Parts Used:
Water Inlet Valve with Mounting Bracket
  • David from San Diego, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
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Unbalanced and walk across the floor on spin cycle
Part Select provided the problem determination information and the video on how to install the replacement parts. I ran into one problem, I could not remove the lock nut to remove the inter and outer tub. I should have bought the special wrench for $14, no local DYI or hardware store had the wrench. So, after examination I used a large screwdriver and wood block to lift the tubs up just enough to remove the old pads and replace with the new. The old pads showed only a wear, but was enough to spin the tubs off balance. The new tabs made the washing machine work like new. New washer $500, repair man $150, parts and information from Part Select $20 bucks, priceless.
Parts Used:
Tub Wear Pads - Package of 3 Suspension Pads - Package of 3
  • James M from Elkhart, IN
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set, Wrench (Adjustable)
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machine was out of balance
Removed the washing machine from the wall and found a broken spring on the floor. Began disassembling the unit before accessing your sight. (Later I viewed your video of the more simple dis assembly).Used your parts breakdown to identify the 6 parts I needed (3 springs and 3 retainers),and ordered them. They arrived on time and as per the video, installed them with ease and reassembled the unit. My wife is very happy. Thank you, Rusty
Parts Used:
Suspension Spring Suspension Spring Retainer
  • RUSSELL from SOUTHOLD, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers
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Spin cycle stopped working
Farly easy repair, once I figured out the problem. The clutch assebly plastic part broke (over 15 yrs old), which is the part that engages the drum for the spin cycle. Following the very helpful diagram on Part Select, I removed the agitator cap and bolt from inside the agitator assembly, and pulled the assembly out of the drum. Then I put the washer on its side and removed the three bolts and two hose claps that hold the motor assembly. I pulled the motor assembly along with the drive shaft out to access the clutch/brake assembly area, removed the broken plastic drive piece and re-assembled.
Parts Used:
Clutch Lining Kit
  • Brent from Highlands Ranch, CO
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Screw drivers, Socket set
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Screw agitator would free spin
Job was easy! Just remove the top cap with a screw driver. With a socket and extension, remove the bolt that holds the agitator to the transmission shaft. Pull up on the agitator and lift it off the shaft. I had to use the screw driver to pry off the center piece that held the cogs because it did not what to separate from the rest of the agitator. Removed the pieces of the old, broken cogs, cleaned up the parts and installed the new cogs with the center piece upside down. I then took some silicone lubricant and lubed the area the cogs rub on and the opening the center piece spins in on the rest of the agitator. I then removed the Thrust Spacer on the mail part of the agitator but just lifting off the old one and putting on the new one. Then, with the center piece that holds the cogs upside down I inserted it into the upper corkscrew section of the agitator so that the cogs would not fall out. While holding the two pieces together, I turned it back right-side-up and installed it back onto the other part of the agitator and then on the shaft. Re-installed the bolt and tightened with the socket. That's it! It sounds more complicated then it really was.
Parts Used:
Agitator Directional Cogs Thrust Spacer
  • Charles from San Diego, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
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The motor turned with loud noise ,but nothing else worked
I used "Emley's Cheap and Easy Repair" book to remove,install and reassemble the machine.
A lot of time was used to clean the filthy tub and basket.
While replacing the broken motor coupling I decided to replace some of the seals.
PartSelect got the ordered parts to me in a couple of days.
I wouldn't hesitate to do the job again.
Parts Used:
Seal, Inner Cap Direct Drive Motor Coupling Washer Transmission Stem Seal Centerpost Gasket Spin Pinion Seal Inner Tub Filter Plug Kit
  • Bob from East Palestine, OH
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench set
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sounded out of balance even after shifting clothes
The tub was out of alignment and water fell behind it and onto the floor. My brother-in-law suggested my problem could be the tub balancing spring and when I moved my washing machine, there it was on the ground.
The schematic does not show where it hooks up. So after I did what I thought looked right, the machine still did not work properly. Then I replaced the three suspension springs and that didn't solve the problem.
I found a whirlpool "do-it-yourself" repair book at the library and was prepared to tear into the machine. However, I did not have the tub balancing spring in the correct spot at one end. It hooks up from one of the outer bracket to the back of the housing unit along between the legs. There is a hole that had rusted through. I simply drilled a new hole nearby and low and behold it works!
Easy fix - the frustration was with the poor schematic.
Parts Used:
Tub Spring
  • Lori from Parchment, MI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers
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Upper agitator stopped moving
First, I removed the softner cup from the top of the agitator. Second, I removed the plastic seal by pulling it out. I then used a socket to remove the bolt holding the agitator down. I then removed the agitiator from the machine and seperated the upper and lower agitator by placing my feet on the lower agitator and pulling up. The dog-ears were in the upper agitaotr section and easy to see and replace. I re-assembled in reverse order. The whole process took less than 30 minutes.
Parts Used:
Agitator Directional Cogs
  • Craig from Yadkinville, NC
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
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Leaking water pump where casing halves split.
Replaced pump without disassembling the cabinet or disconnecting motor or any other parts.

Disconnected power, drain, hot and cold water lines. drained lines to pail before taping to top of unit.

Tipped the unit to a 45 Deg. angle, leaning the top side edge onto a stool so that pump presented well at the raised bottom edge.

Removed hose clamps at pump suction and discharge ports and drained water into a shallow soaking pan. Kept clamps on hoses to facilitate reinstallation of pump.

Removed spring clamps at front and rear of pump housing.

Wiggled motor shaft away from coupling in pump. This is a friction fit, so no parts removal was required and no parts "come loose" in the process.

Wiggled new pump housing onto the motor shaft after checking square shaft alignment with respect to square female coupling on pump.

Pushed and twisted hose ends onto pump suction and discharge ports, then pulled spring clamps down over hose ends at pump ports.

Reset spring clamps so that they were aligned and square with pump ports. Reconnected power, drain, hot and cold water line connections.

Washer ran as before but without leaks this time.
Parts Used:
Direct Drive Water Pump
  • David from Washington Crossing, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers
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leaking from tub
First I turned off the water and unplugged the washer from the outlet. I took the two screws off the console and turned it up to undo the clips that hold the cabinet to the back. I took out the 2 phillips screws at the top corners of the back. I was then able to pull cabinet off and not have to remove the console, but carefully slid it to the side, as ther wires were still attached.
Pried off agitator cap & reached into agitator to pry out another cap to access 7/16 bolt. Checked over the agitator parts for wear (dogs) Took agitator, top outer (white) and inner (brown) tub rings off.
Sprayed lots of liqid wrench around spanner nut and drive block and gave it time to work. Used spanner tool to get spanner nut off. Hard work. Pounded and pounded and pounded and pounded with hammer. It gave a tiny bit. Then I got an idea: I pounded it back the other way, as you would to tighten. This helped. I then pounded back the other way and did this again. It worked amazingly well.
Got to drive block and it was rusted out along the bottom and also hard to get off. The diagram showed a "lock" (horseshoe shaped thing) on top of it, but mine was all in one piece but I couldn't tell that. I sprayed and pryed and pounded from the bottom and it split in half. It needed to be replaced anyway.
The inner tub was also hard to get out and I used some dish liquid. I pushed down, (using the rags here, the edges can cut you). I twisted, I pulled. I pushed, I pulled, I cussed, and begged. I then went to bed and then next day I pushed backwards and forwards and side to side & finally it came off. Then I undid the brackets on the bottom of the outer tub along the bottom and disconnected the clear hose in back. When loosening the black hose clamp in front to the pump, water started to come out of the hose so I grabbed a cool whip container to catch it. It smelled yucky. Once I had the outer tub off I put the new seal in, using some plumber's grease to help get ithe tub over the shaft..Then I hooked up the hoses & brackets on the bottom of the outer tub. I cleaned out the outer tub, as there was crud in the bottom. Then I poured about 5 gallons of water in it to see if the seal was set in right. Make sure the drain hose hasn't fallen out! (You can leave this water in the tub, you'll find out why) I cleaned up the rust on tube of the inner tub with steel wool and inspected everything else. Something didn't look quite right about the outer shaft that goes around the spin tube. It looked like something should go there. I discovered there SHOULD have been a seal there but one was never put in. So I put one in. I used a little grease to help put the new drive block on, and tightened the spanner nut with the spanner wrench. I put everything else back on EXCEPT for the cabinet-with the console attached. Ha Ha All the other directions I read wrote to take the console off first. If I had done that I wouldn't have been able to do the most important part of the job: testing the result. I finished filling the tub to the lowest water level to watch it go thru it's cycles and checked for leaks. If the console was "flopped over" the back how can you check? (I don't play with wiring)
I turned off the water & unplugged the washer and slid the cabinet on.. I tipped the console back to access the large gold squiggly brackets that hold the cabinet to the back and reattached them to the back, by removing them, hooking them onto the back, and snapping them into place. I double-DOUBLE checked to see if anything had come loose, then slid the console first on top of the back and put the two screws back in. The screws on my machine are not covered up by the end caps, but they are at a wierd angle, so I held the console up slighly and started the screws first. As they tightened down the console slid into the holes on the cabinet.
There is a small sppliance shop in my town & the guy loaned me the spanner wrench. It was very nice of him.I guess I will have to give his & his famil
Parts Used:
Centerpost Gasket
  • Debra from Milton - Freewater, OR
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Screw drivers, Socket set
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All Instructions for the KAWS855JE0
31 - 45 of 1598