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DG806 Maytag Dryer - Instructions

All Instructions for the DG806
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Stripped leveler screw making impossible to level my washer
Put blocks under the washer where the leveling leg was needed and screwed the part into the washer. Then it was just a matter of moving the washer into place and leveling. Pretty easy.
Parts Used:
Adjustable Leveling Leg Rubber Foot Pad
  • Rebecca from Wylie, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Wrench set
21 of 28 people found this instruction helpful.
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Temperature setting not working
Took off back cover, thermostat was easily identified because of photos I've seen on website. Took 2 connectors off, removed 2 screws and removed old thermostat. That was pretty much it!

NOTE: Replacement thermostat 694674 has an adjustable temperature range setting that MUST be manually set prior to installing! You need to use the enclosed chart to find your original part# and make sure the setting is matched. My original part# 341146 had a "D" setting so I had to change but very easy to do.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Robert from Buffalo, NY
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
17 of 20 people found this instruction helpful.
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bottom rack was starting to rust away and we needed a new one
The dishrack came in one box I opened the box snapped on the rollers and the bumpers and put it in the dishwasher, could not have been easier Thank you partselect
Parts Used:
Lower Dishrack Kit
  • pat from muncy, PA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
19 of 26 people found this instruction helpful.
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Dryer not heating
First let me say that this dryer is at least 30 years old. The only repairs it has needed up to this point were a set of belts and lint screen holder.

I researched and found a list of items to check for dryer not heating. Only 3 items were listed as possible causes, the Heating Element, Cycling Thermostat, and Heating Element Terminal & Insulator.

First and most important step - UNPLUG THE DRYER FROM THE WALL

To access the cycling thermostat, I removed the back panel. The thermostat is located on top of the blower housing and is easily accessable. I was unable to test the old part.

Accessing the heating element and terminal insulators is a bit more difficult as they are located in the fron of the dryer around the door opening. Further research showed the way to access these parts was to remove the cabinet from the chassis. After photographing the wiring connections, I disconnected the cycling thermostat and motor connections. Next, I removed the 3 screws at the bottom of each side panel. With the dryer door removed (it lifts off when open), I simply lifted the cabinet up over the drum. I recommend having someone assist with this as it is awkward and a little heavy. Lay the cabinet on its front on a rug to keep from scratching the finish. The heating element and insulators can be inspected at this time.

Having found no breaks in the element or insulators, I assumed the problem was the cycling thermostat and ordered one. When I got it (less than 2 days), I installed it and reassembled the cabinet to the chassis. I plugged the dryer in and set the timer. Still no heat!

After looking at the schematic, I found 2 other possible causes for no heat. The motor contains a centrifugual switch (closes when the motor spins) which I was not able to check. There is also a HIGH LIMIT thermostat on the shroud that holds the heating element. I decided I could test this part by by-passing it. I unplugged the dryer and removed the back once again. I reached past the drum from the back (not easy to do) and disconnected the 2 wires from the thermostat and connected them together. I plugged the dryer back in and started the dryer. It heated up like it should. I then ordered the high limit thermostat. After removing the cabinet once again (easier 2nd time), I installed the high limit thermostat and reassembled the unit.

The Dryer is working fine and hopefully should last another 25-30 years.
Parts Used:
Cycling Thermostat (Limit: 140-20)
  • William from Exmore, VA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Wrench set
18 of 24 people found this instruction helpful.
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The drum wasn't rotating very well, and it made grinding noises
In retrospect, this repair was not diffcult, but it took a long time because I could not find any directions or advice on the internet. The first puzzle was getting inside. The back panel comes off very easily with removal of a handful of panel screws. This exposes the motor, belts, drive pulleys, etc., and while I could rotate the drum by hand, I could not diagnose the grinding noise or why it turned with difficulty.

To go further, I had to remove the cabinet, which is easy - once you know what to do. Take out three screws along each side, near the bottom (of course, don't lose or mix up these screws with the ones from the back panel). You'll also have to detach four colored wires from the motor - the connectors are color coded, so there shouldn't be a mix up when you reattach them later. There are also two wires (B & W) that connect to the back of the drum that nneed to be detached - I marked B and W on the metal with a sharpie so as to remember which goes where. I didn't bother to check, but they must be the wires that connect to the door-open switch. After that, the whole cabinet (sides, front panel and door, top and control panel as one unit) can be tilted forward and lifted off to be set aside.

It turns out the grinding was from all the crap that fell through the gap at the front edge of the drum over the years - handfuls of paper clips, hair clips, wadded wrappers, earrings and $3.60 in change.

It mostly landed in the flange, or sheet metal shield, surrounding the coil heating element, which encircles the front of the drum ("Halo of Heat"). I cleaned all the lint and crud off the heater flange, and from the whole cabinet. Be very careful not to break the heating coil wire or the ceramic insulatots that hold itin a circle - they are somewhat fragile. If you ever need to replace the heating coil element, this is how you get there. It's a fairly simple matter of threading the new wire could through the ceramic insulators and making the obvious electrical connections at either end.

But my issues were still with the frame and exposed drum, belts etc. The drum is suspended from bearings at the back; nothing holds it at the front. There are two belts. One runs from a small pulley on an idler wheel (tensioned by a spring) to a large pulley on the back of the drum. The other is the motor belt, which is the longer of the two, that runs from the motor shaft to a small pulley on the back of the drum (inside the large pulley mentioned above), then over to the large pulley portion of the idler wheel (inside the small pulley mentioned above).

I wondered if any of the bearings on any of the parts was going bad, so I took off the belts. I don't remember which belt should come off first to make it any easier, but you'll manage either way Pull the idler wheel to slightly loosen a little tension on the belts and rotate one belt off a small pulley, then the other one. If you're new to this, take a picture, or make a sketch where the belts go - don't trust yourself to remember it later.

The idler wheel is attached to a bar that slides in a bit of a track or bracket. By lifting the wheel (stretching the spring) and moving it to the R side just a little, the bar can drop down the track and take all the tension off the spring. The spring is hooked into the cabinet at the biottom, and fits on the idler wheel shaft at the top, so you can take it off with no problem. Once you do that, you can pull the idler wheel/pulleys right off toward you. I took the bar out of the bracket and washed it off and polished it with steel wool to get rid of rust. similarly, I cleaned the frame bracket it slides in. I lubricated both parts with a litte petro jelly before reassembling. All the parts were covered with lint, and I took the time to clean everything off, especially the motor. We're talking forty years' worth.

I also went inside the drum and took out the lint filter and a plastic guard, and used a little brush and a vacuum to clean out the caked
Parts Used:
Dryer Motor Belt
  • Jon from Salem, OR
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers
14 of 16 people found this instruction helpful.
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rollers and clips on botton dishrack were broken
I pulled off the old clips and easily replaced them with the new clips and popped on the wheels.
I replaced 8 clips and 8 wheels in less than 15mins
Parts Used:
Lower Dishrack Kit
  • Diane from Waltham, MA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers
20 of 37 people found this instruction helpful.
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Dryer of elderly relative was very hot and dried clothes slowly.
The lint filter was torn in a couple of places. This let lint go into the dryer vent pipe over a period of years. I ordered a new lint filter and replaced it. I also pulled out the plastic piece the filter sits against and cleaned out behind it. The vent went to the roof. I pulled off the rain shield and found that the vent pipe was almost completely packed with lint. I pulled out all I could reach and nailed a 2x2 inch and 1x2 inch together and used it to scrape out the vent pipe. I placed a flashlight in the bottom and checked to see it was clean. I replaced the rain shield and carefully reconnected the dryer to the vent. Now the dryer runs cool as it should.
Parts Used:
Lint Filter
  • John from Sante Fe, NM
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
16 of 27 people found this instruction helpful.
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Coating on the rack has worn exposing the metal underneath
There were no instructions with the part, but looking at the old rack it was simple to see how the parts should be assembled. Took the center part from the old rack, twisted off, and applied it to the center of the new rack. Snapped on the wheels and was done. Very simple assembly.
Parts Used:
Lower Dishrack Kit
  • Susan from Shelby Township, MI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
12 of 17 people found this instruction helpful.
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Clothes won't dry due to broken drive belt.
Turn off gas valve, unplug electrical cord; take back cover off. Take spring off the drive pulley; slip the drive belt on; put tension spring back on and put back cover back. The spring tension is strong so there is a little trouble to put it back.
Parts Used:
DRIVE BELT
  • tony from Deer Park, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
12 of 19 people found this instruction helpful.
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No heat in dryer
Took off the lower front panel, removed duct piece from filter to blower fan, removed two screws and two wires to thermostat in exhaust ducting, then replaced thermostat with new one. Very easy job and everything worked like new when I reassembled it.
Parts Used:
Cycling Thermostat - Limit 135/155
  • Noah from Maiden, NC
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
10 of 14 people found this instruction helpful.
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No Heat in my ancient Maytag Dryer
I had a repairman come by to take a look at my 20+ year old dryer because it wasn't working properly, NO HEAT. He said it was the cycling thermostat and wanted to charge me $190 to fix this problem. He left me the paperwork for this diagnose and charged me $49.50 for looking at the dryer. I called a friend of mine and told him what the repairman had said. He went into your website and found the part, the first time around we ordered the wrong part. No problem, I sent the wrong part back and reordered the proper one. It took him no more than 20 minutes to install this part. I received credit for the wrong part within 2 weeks. The dryer is working great. It’s good to know of a company that still can provide you with parts for a dryer as old as mine, thanks. It worked and it' still working!
Parts Used:
Cycling Thermostat (Limit: 140-20)
  • GAIL from WOODBRIDGE, VA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
9 of 15 people found this instruction helpful.
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Old rack rusting
This is the second time I have replaced a rack. You just pop on the new rollers and you're good to go!
Parts Used:
Lower Dishrack Kit
  • Lynn from Schenectady, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
5 of 6 people found this instruction helpful.
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light bulb in water ice freezer door went bad
I didn't. Don't know how to get to light bulb to change it for this specific model
Parts Used:
Light Bulb - 40W
  • Carl from RIVERSIDE, CA
  • Difficulty Level:
    Very Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers
7 of 13 people found this instruction helpful.
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Took too long to dry
After replacing the cycling thermostat failed to fix the problem, I jumped the Dampness sensor, overtemp sensor and flame sensor - no change, flame went out after 15 to 30 seconds. Ordered the replacement coils for the gas control and reconnected all sensors: solved!
Parts Used:
Cycling Thermostat (Limit: 140-20)
  • Ronald from Chardon, OH
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers
5 of 7 people found this instruction helpful.
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worn and rusted lower dishrack
First, I checked the ripped box for damage to the dishrack. Fortunately, there was none. Then I looked for the instruction booklet. Unfortunately, there was none. And the parts bag was ripped and I did not know what was supposed to be in it. So, I rechecked the photo of the dishrack on the website and found that either parts were missing or the dishrack was different than illistrated. After a few moments of thought, I realized the latter was the case. I then figured I would have to use some deep thought to do the installation since neither the missing instruction booklet nor the unzoomable photo would help. So, I pulled out the tall thin thingamabob from the old dishrack and put it in the new one though it did not secure as tightly. Then I put the wheel units on just like the old one. What I could not immediately figure out was where the collapsible rack row was mounted. I eventually realized that the rod went into a hole in the wheel units and the latch mounted above one unit. I still have no idea where the two other tan clips go. Though the dishrack is different and thus requires different science to fill it, it appears to do the job.

Thanks for asking.

By the way, it was not blue.
Parts Used:
Lower Dishrack Kit
  • Greg from Royal Oak, MI
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    15 - 30 mins
4 of 5 people found this instruction helpful.
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All Instructions for the DG806
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