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ALE230RCW Amana Dryer - Instructions

All Instructions for the ALE230RCW
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Load Squeaky noise when the dryer is tumbling
To make working on the dryer easier we tipped the dryer back, about 45 degrees, removed the bottom panel, the door panel, note: make sure to mark the inside chassis or case with a sharpie where the wires go by color, etc… note: this makes it easy to place every thing back in order. I removed three screws on the bottom left side, to allow the more room for me to remove the drum. You can not remove the drum just yet but until the rubber belt is removed. I went below where the tension wheel is… it’s back behind the motor… incidental the tension wheel and the arm was the problem, it had warn to one side. Now release the rubber belt around drum. I pulled the drum out. The motor assembly is all one piece so it’s easy to remove. Don’t forget to unplug the plastic Molex plug and mark where you wires go. Two screws in front on the motor assemble and the whole assemble comes out. From here I could do a good job of cleaning the motor assemble and replacing the parts without any difficulty. Re-assembly was really easy, just one issue with placing the rubber belt took some time, and I need some help. I was finished in less than two hours. Bingo fixed!!
Parts Used:
Idler Pulley Wheel with Bearing Idler Pulley Lever and Shaft
  • Antonio from Elk River, MN
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver
39 of 43 people found this instruction helpful.
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Dryer would squeal when drying clothes
Unplugged dryer, turned off gas, raised front of dryer with two 2X4's on edge resting on legs, removed two lower panel screws, removed lower panel. Removed lower blower & filter assembly, screws (3) are on the inside of drum. (Good chance to clean it out) Removed two lower front upper main panel screws. Supported top panel with wood for access. Removed panel slowly, marked wires that go to door switch, set panel aside. Removed tension on belt by reaching in on the right lower side and unhooking the tensioner from belt, look to see how it is installed, for reinstallation on assembly. Pulled drum out slowly as not to damage seals on drum. replaced parts, attached with self tapping screws.(screws all the same size) reassembly in reverse order. Will need to put belt on drum before installing drum. Check drum alignment with rollers and seals. Used very small amount of high pressure grease on roller bracket and shaft assembly where the support roller shaft spins for lubrication. All's quiet. (Vacuumed out inside while dissassembled)
Parts Used:
Drum Support Roller Thrust Washer Drum Support Roller and Shaft Assembly Multi Rib Belt Retaining Ring
  • JOHN from CORPUS CHRISTI, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Nutdriver, Pliers, Screw drivers, Socket set, Wrench (Adjustable), Wrench set
36 of 42 people found this instruction helpful.
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Screaming noise and drum not turning
Removed top, remove front panel, removed drum assembly brace, removed drum and belt . The belt and rotor were shot. I replaced both drum support rollers since i was there. Then replaced the motor and Idler lever and pulley, the put the belt on and put everything back. This unit will last a while longer and the grand total including next day air 175.00. I tried to just by the motor locally but for 242.00 I got every thing listed above.
Thanks
Parts Used:
Dryer Idler Assembly Drum Support Roller Motor Assembly - Threaded Shaft Multi Rib Belt
  • Robyn from Pullallup, WA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers, Socket set
31 of 37 people found this instruction helpful.
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Heating element went bad
I couldn't find any information on the internet on how to fix my dryer, so I took every screw out of it, which I later found was not needed - just 2 in the front. Then I had to figure out WHERE the element was. Turns out, against the back panel with 2 screws. I had to crawl on my belly to get in there with little room to work. Installing the new one didn't take long at all though. I also vacuumed out the inside and cleaned it well, then put all the screws back in it.

I'm glad I re-did all the screws because now it sounds brand new. It's 3 times quieter than it ever was (it was donated to me), and it feels great that I was able to fix it on my own for about $50.
Parts Used:
Heating Element (Red Dot)
  • Jeff from Conyers, GA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
29 of 32 people found this instruction helpful.
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lint collector plastic holder broken
Un plug the dryer ***
Pulled the top portion of the dryer off
Used socket to undue two nuts to remove the front panel and unhooked the wires.
unscrewed 3 screws and took out the air duct assembly. Cleaned the dryer of all lint and replaced the air duct with a new one.
Reverse the process.
Parts Used:
Lint Duct Assembly
  • Todd from Wappingers Falls, NY
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Screw drivers, Socket set
27 of 32 people found this instruction helpful.
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Original belt finally gave way.....(15yrs old)
Simply remove the front panel screws(2) at the bottom of the dryer. Pull bottom of panel outward until it swings free of the top(taking care not to pull the wires out). Rotate out of the way and remove the two left side screws holding the drum plate and snake the belt around the flange. Reinstall those screws and remove the same ones on the right side. Snake the belt behind that flange and reinstall screws. Then all you have to do is run the belt around the motor sheave and the idler pully and your done. Reinstall the front panel.
Parts Used:
Multi Rib Belt
  • Garrett from Racine, WI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
24 of 25 people found this instruction helpful.
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Dryer lint screen was broken.
Searched Maytag.com and other sources, only partselect.com had what I needed. Three days after my purchase, our dryer lint screen was again fully functional.
Parts Used:
Lint Filter
  • Jack from Tabernacle, NJ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
25 of 28 people found this instruction helpful.
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Drum Not spinning
First, I unplugged the dryer. Then I used a flat screw driver to pop the top open. I removed 2 bolts from the front cover and removed the front door cover. I also took pictures of the electrical connector on the door so I would remember how the wires went back on. Then I removed 4 bolts from the front drum guide and lint screen holder. This allowed me to remove the drum & old belt. While the drum was out, I pried an access panel open on the side of the dryer. I then glued the new back felt piece in place. I put the new belt around the drum and re installed it. I re-installed the front guide and front cover re-connecting the door electrical switch. With the access panel open, I attached the belt to the motor. I then plugged it back in and turned it on to verify operation pryor to snapping the top cover back in place. Very easy repair.
Parts Used:
Multi Rib Belt Cylinder Felt Seal
  • Dann from Claremont, CA
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver, Screw drivers
26 of 31 people found this instruction helpful.
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Taking too long for clothes to dry.
I first unplugged the dryer (don't want to get nailed with 240 volts). I then removed the two screws on the bottom section of the dryer just below the door. I then removed the two screws on the front door assembly and removed the door (make sure you don't break the wires and/or door switch. The wires need to be removed from the door switch prior to removing the door panel completely). I then took a flash light and look inside the dryer towards the back. I could see the heating element in the back. I then removed the two screws holding the heat element and removed the heating element (taking note on the orientation of the element). I then removed the black and orange wires making note which wire fit on which terminal. I then compared the old unit with the new unit to make sure I had the right one. I then assembled the new heating element (heat sensors etc.). I then hooked the black and orange wire to the new element. I then reassembled everything in the reverse order.

Note: I very CAREFULLY used the heating elements support connectors to hold the element in place while I started my screws. Once they were started then I could release the element and fit it properly into the housing as I tightened the screws.

The other thing that you need to check is to make sure that the air-duct is not blocked. If you have a lot of lent on the bottom of the dyer (inside) then you could have a blocked air-duct. This happened to me. I went outside and noticed that we have a door on our vent that flips up to keep mice etc. from coming in. Some of the lint that was blown out got wet from the sprinklers and calcified underneath the vent. This was preventing the vent from opening. This could of been our problem all along but I had already replaced the heating element so I keep it as is.

PartSelect was wonderful. I was able to find my parts quickly and the turn around time was tremendous. I would buy from PartSelect again.
Parts Used:
Heating Element (Red Dot)
  • James from Eagle, ID
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Nutdriver
23 of 27 people found this instruction helpful.
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the door on the unit wouldn't stay closed
removed the dryer female part that was broken with needle nose pliers and inserted the new one, on the door i removed one phillips screw and r/r the male piece with the new one and re-inserted the screw. that was all, very easy repair
Parts Used:
Door Catch Kit Door Strike Bracket
  • john c. from north beach, MD
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Pliers, Screw drivers
22 of 33 people found this instruction helpful.
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The insert-molded nut stripped from the wheel
Because the wheel had stopped and the shaft kept turning (junk from child's pocket got in there), the nut stripped itself away from the wheel causing low RPM and low air movement (lazy flame, vibration and clothes not drying)

I had to use a screwdriver to break the wheel away from the center nut and remove the fan. I then removed the air fan housing (3 bolt behind the fan wheel). I used a small pair of vise grips to hold the motor shaft staionary while I used a pair of channel lock pliers to remove the nut that was molded into the fan from the motor shaft. It was harder to get the nut started then I would have thought.

Once complete, I put the fan housing back on and threaded the new wheel on easily. The motor has external fins on it which turn with the shaft-I held one lightly while I threaded the fan on to keep the shaft from turning. Tighten just slightly more than hand tight-don't go crazy-it's threaded to stay tight with rotation. Works great and very quiet now.
Parts Used:
Blower Wheel
  • Ted from Grayslake, IL
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Screw drivers
18 of 21 people found this instruction helpful.
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Screeching sound coming from back of the dryer.
First removed the bottom access panel, then the then pried the top lid open. Then, I could get to the four screws holding the front of the drum in place. Once that was removed, reached underneath drum and disconnected belt from tensioner pulley and motor. Removed the drum and discovered the problem. One of the two drum rollers had completely disintergrated from the shaft, actually "melting" off of its roller shaft. Removed both of the rollers and shafts by putting a flathead screwdriver on the slot of the shaft, and at the same time holding the locknut behind the bracket with a box wrench. I replaced both shafts and rollers and reused the same washers and snaprings. I used a screwdriver and a vice to remove the snap rings off of the old shafts. The best bet is to use a pair of snap ring pliers, which I didn't have. I used some white silicone grease to lube the new rollers up, reinstalled them and replaced the belt. You MUST route the belt around the drum before you install, then connect the belt to the motor underneath and wrap it around the tensioner. While I had everything opened up, I shop-vac"d the inside of my dryer(filthy). I did this before putting anything back together. Also, when re-installing the front dryer panel, make sure the motor inlet and the lint outlet tube form an airtight seal. All in all, this was a fairly strightforward job. The dryer now works great and is as quiet as a mouse.
Parts Used:
Drum Support Roller Idler Pulley Shaft Multi Rib Belt
  • Brian from Yucaipa, CA
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Screw drivers, Socket set
16 of 16 people found this instruction helpful.
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Dryer making loud squeeking noises
The pully wheel was completely worn down as the belt had cut into it over time. I'm not sure if the lever and shaft needed replacing but since the part was inexpensive I decided to replace it as well as the wheel. The easiest way to access the parts was to turn the dryer on its side and remove the bottom panel of the dryer. This eliminated the need to remove the drum. It was then easy to reach in with a wrench and remove nut and bolt that held on the pulley lever. I also had to remove the spring which was attached to the lever. Next I put the new pully wheel on the shaft of the new pulley lever. The most difficult part of the job was installing retainer clip which holds the wheel on the shaft. This took a little persistance. After this was done it was simple to put the assembly back in place, reattach the spring and tighten the nut and bolt. I then replaced the bottom panel of he dryer, turned it upright and plugged it in. The whole job took just over an hour. One tip: Before removing the old assembly, I took a picture of it with my cell phone camera so I would remember how it went back together.
Parts Used:
Idler Pulley Wheel with Bearing Idler Pulley Lever and Shaft Retaining Ring
  • James from North Kingstown, RI
  • Difficulty Level:
    Easy
  • Total Repair Time:
    1- 2 hours
  • Tools:
    Pliers, Socket set, Wrench set
15 of 15 people found this instruction helpful.
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Dryer drum stopped spinning
Dryer drum stopped but all other elements seemed functional; couldn't afford new dryer. Unplugged appliance & moved it to my garage (more room to move about). Undid base plate w/tools and found belt slack - identified broken idler pully wheel as part to fix. Went online & found part-select, located part & was way happy: $7.00 part + $7.00 shipping; got part 3 days later. Removed broken pully wheel (take off lock-washer, put wheel on, reinstall lock washer). Cleaned out venting elements (huge lint-ball & some sand in blower intake area). Re-attahced base. Back on-line to see "replace dryer belt" instruction sequence; opened lid of machine (while verticle) and positioned belt properly. Located access port (sealed) at base, knocked out the circular metal plate so I could reach in & thread the dryer belt back around motor & idler pulley wheel. Did test spin (manually) to make sure belt properly threaded, in place. Move appliance back to proper location, plugged in & hooked up venting to outside; ran test & SUCCESS!!!! It even seemed to dry better because of the now cleaned venting area. Labor cost = $0, Part cost < $15.00, Time (actual work) bit over 3 hours total.
Parts Used:
Idler Pulley Wheel with Bearing
  • Leif from Brighton, CO
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Pliers, Socket set
15 of 16 people found this instruction helpful.
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Dryer stopped working with no power detected
Based on my research, the thermal fuse could be blown out so I tested it and it was. I've replaced the thermal fuse, high-limit thermostat and cycling thermostat. bam! it's up and running again. I'd highly recommended ordering your parts thru PartSeclect..the order was easy and shipping is quick. Thanks
Parts Used:
Cycling Thermostat High Limit Thermal Fuse
  • Eric from Yorba Linda, CA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Pliers, Socket set
18 of 26 people found this instruction helpful.
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All Instructions for the ALE230RCW
16 - 30 of 538