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66CB Maytag Dryer - Instructions

All Instructions for the 66CB
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Dryer wouldn't heat
Since the heating coil is right behind the front door I had to remove all panels starting with the back one to get to it. The back has a lot of tech screws that I removed with the nut driver. The side panels were removed with a phillips screwdriver. The top is held in place with the other panels. The base was shifted away from the front and I released the heating coil case with 4 screws in the front and was able to pull it out of the top to replace it. I cut the old one out with wire cutters and snaked the new one through the ceramic insulators. I was careful not to touch the new one without gloves because the oil from your hands can burn them out more quickly. I screwed the new ones to the contact points while trying not to stretch it too much. I vacuumed the whole dryer out before putting it back together.
Parts Used:
Heater Wire - 240V
  • Edith from Grove City, OH
  • Difficulty Level:
    Difficult
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Nutdriver, Screw drivers, Wrench (Adjustable)
59 of 68 people found this instruction helpful.
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Stripped leveler screw making impossible to level my washer
Put blocks under the washer where the leveling leg was needed and screwed the part into the washer. Then it was just a matter of moving the washer into place and leveling. Pretty easy.
Parts Used:
Adjustable Leveling Leg Rubber Foot Pad
  • Rebecca from Wylie, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Wrench set
21 of 28 people found this instruction helpful.
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The drum wasn't rotating very well, and it made grinding noises
In retrospect, this repair was not diffcult, but it took a long time because I could not find any directions or advice on the internet. The first puzzle was getting inside. The back panel comes off very easily with removal of a handful of panel screws. This exposes the motor, belts, drive pulleys, etc., and while I could rotate the drum by hand, I could not diagnose the grinding noise or why it turned with difficulty.

To go further, I had to remove the cabinet, which is easy - once you know what to do. Take out three screws along each side, near the bottom (of course, don't lose or mix up these screws with the ones from the back panel). You'll also have to detach four colored wires from the motor - the connectors are color coded, so there shouldn't be a mix up when you reattach them later. There are also two wires (B & W) that connect to the back of the drum that nneed to be detached - I marked B and W on the metal with a sharpie so as to remember which goes where. I didn't bother to check, but they must be the wires that connect to the door-open switch. After that, the whole cabinet (sides, front panel and door, top and control panel as one unit) can be tilted forward and lifted off to be set aside.

It turns out the grinding was from all the crap that fell through the gap at the front edge of the drum over the years - handfuls of paper clips, hair clips, wadded wrappers, earrings and $3.60 in change.

It mostly landed in the flange, or sheet metal shield, surrounding the coil heating element, which encircles the front of the drum ("Halo of Heat"). I cleaned all the lint and crud off the heater flange, and from the whole cabinet. Be very careful not to break the heating coil wire or the ceramic insulatots that hold itin a circle - they are somewhat fragile. If you ever need to replace the heating coil element, this is how you get there. It's a fairly simple matter of threading the new wire could through the ceramic insulators and making the obvious electrical connections at either end.

But my issues were still with the frame and exposed drum, belts etc. The drum is suspended from bearings at the back; nothing holds it at the front. There are two belts. One runs from a small pulley on an idler wheel (tensioned by a spring) to a large pulley on the back of the drum. The other is the motor belt, which is the longer of the two, that runs from the motor shaft to a small pulley on the back of the drum (inside the large pulley mentioned above), then over to the large pulley portion of the idler wheel (inside the small pulley mentioned above).

I wondered if any of the bearings on any of the parts was going bad, so I took off the belts. I don't remember which belt should come off first to make it any easier, but you'll manage either way Pull the idler wheel to slightly loosen a little tension on the belts and rotate one belt off a small pulley, then the other one. If you're new to this, take a picture, or make a sketch where the belts go - don't trust yourself to remember it later.

The idler wheel is attached to a bar that slides in a bit of a track or bracket. By lifting the wheel (stretching the spring) and moving it to the R side just a little, the bar can drop down the track and take all the tension off the spring. The spring is hooked into the cabinet at the biottom, and fits on the idler wheel shaft at the top, so you can take it off with no problem. Once you do that, you can pull the idler wheel/pulleys right off toward you. I took the bar out of the bracket and washed it off and polished it with steel wool to get rid of rust. similarly, I cleaned the frame bracket it slides in. I lubricated both parts with a litte petro jelly before reassembling. All the parts were covered with lint, and I took the time to clean everything off, especially the motor. We're talking forty years' worth.

I also went inside the drum and took out the lint filter and a plastic guard, and used a little brush and a vacuum to clean out the caked
Parts Used:
Dryer Motor Belt
  • Jon from Salem, OR
  • Difficulty Level:
    Easy
  • Total Repair Time:
    More than 2 hours
  • Tools:
    Screw drivers
14 of 16 people found this instruction helpful.
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Dryer of elderly relative was very hot and dried clothes slowly.
The lint filter was torn in a couple of places. This let lint go into the dryer vent pipe over a period of years. I ordered a new lint filter and replaced it. I also pulled out the plastic piece the filter sits against and cleaned out behind it. The vent went to the roof. I pulled off the rain shield and found that the vent pipe was almost completely packed with lint. I pulled out all I could reach and nailed a 2x2 inch and 1x2 inch together and used it to scrape out the vent pipe. I placed a flashlight in the bottom and checked to see it was clean. I replaced the rain shield and carefully reconnected the dryer to the vent. Now the dryer runs cool as it should.
Parts Used:
Lint Filter
  • John from Sante Fe, NM
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    More than 2 hours
16 of 27 people found this instruction helpful.
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Clothes won't dry due to broken drive belt.
Turn off gas valve, unplug electrical cord; take back cover off. Take spring off the drive pulley; slip the drive belt on; put tension spring back on and put back cover back. The spring tension is strong so there is a little trouble to put it back.
Parts Used:
DRIVE BELT
  • tony from Deer Park, TX
  • Difficulty Level:
    A Bit Difficult
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers
12 of 19 people found this instruction helpful.
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Threads on old legs had been damaged in moving to new location.
Removed the damaged legs, replaced with parts from this site and leveled the washer .
Parts Used:
Adjustable Leveling Leg
  • Wayne from SEDONA, AZ
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Wrench (Adjustable)
2 of 2 people found this instruction helpful.
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worn roller wheel and bearing
replaced worn parts
Parts Used:
Drum Roller Shaft Washer
  • David from Chadds Ford, PA
  • Difficulty Level:
    Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Screw drivers, Socket set, Wrench set
0 of 1 people found this instruction helpful.
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Leg was mssing after move into new home.
Purchased x4 new adjustable legs. Leaned the washer back and held in place with block of wood. Loosened the two older front legs with an adjustable wrench because they had a locking nut and replaced with new legs. Repeated process on back side of washer. Once all the new legs were installed leveled the machine adjusting the legs if necessary.
Parts Used:
Adjustable Leveling Leg
  • Matthew from The Woodlands, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    Less than 15 mins
  • Tools:
    Wrench (Adjustable)
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rumbling noise
Remove dryer back,release spring tension to remove belts. Clean lint and pulleys. Replace belts,spring tension and back and LEVEL Dryer. NOTE: The back is part of the frame, make sure all screws tighten DO NOT omit any.
Parts Used:
Dryer Motor Belt DRIVE BELT Drum Roller Shaft Washer
  • John from Follansbee, WV
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    30 - 60 mins
  • Tools:
    Nutdriver, Pliers
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Lint screen had holes
New lint screen
Parts Used:
Lint Filter
  • Mary from Cudahy, WI
  • Difficulty Level:
    Really Easy
  • Total Repair Time:
    Less than 15 mins
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Replaced both belts.
Bought a house and inherited an ancient set of appliances. I figured that they dont make em like they use to so why get rid of them. Noticed the dryer tub wasnt spinning one day after running through three cycles. I took the back off and realized the belt that made the tub spin was broke. Went ahead and ordered both belts (old age catches us all) so i wouldnt have to order the other a few weeks later. Pulled the spring took the old belt off put on the new ones like ya would a bike chain. Used the pliers to put the spring back on and voila.
Parts Used:
Dryer Motor Belt DRIVE BELT
  • Dane from Brookeland, TX
  • Difficulty Level:
    Easy
  • Total Repair Time:
    15 - 30 mins
  • Tools:
    Pliers, Socket set
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All Instructions for the 66CB
1 - 11 of 11